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U.S. STEEL DUQUESNE WORKS<br />

HAER No. PA-115<br />

(Page 100)<br />

The rotating nozzles at the top of the scrubber were<br />

replaced by two sets of seven upward pointing nozzles which were<br />

positioned across the diameter of the scrubber and inserted one<br />

above the other. Incoming water entered the scrubber through a<br />

cut off valve located at each set of nozzles and was forced<br />

upwards through two screens, placed at six foot intervals, before<br />

falling back through them in the form of droplets. The 5 hp<br />

motor driven cut off valves were composed of a series of openings<br />

or ports, one for each nozzle, which were successively blocked by<br />

a revolving core located inside of the valve. Consequently, the<br />

valves shut off the water leading to each nozzle in turn, making<br />

an area of low resistance over the temporarily dormant nozzle.<br />

As the gas was naturally directed to the area of low resistance,<br />

the water was turned on again thereby deflecting it to the next<br />

nozzle. In this manner a spiral motion was created which gave a<br />

larger exposure of the gas area to the washing water than would<br />

normally result. As such, the principle of using water to guide<br />

the passage of the gas in the scrubbers, in what became known as<br />

the Diehl spray gas washer, became one of the standard methods<br />

employed in industry-wide wet systems over the next half-century.<br />

After four years of meticulous documentation the results of<br />

the experiment markedly favored the wet gas cleaning system.<br />

While the hot blast stoves using gas from the more traditional<br />

cleaning system continued to be taken off line every two months<br />

for cleaning, the stoves which used gas from the wet system<br />

operated continuously over the course of the experiment. Lower<br />

moisture levels in the gas emanating from the wet system resulted<br />

in higher burning efficiency when compared to the gas flowing<br />

from the more traditional system. Furthermore, when comparing<br />

the cost of constructing and maintaining the equipment used in<br />

the wet system to the cost of maintaining the hot blast stoves<br />

operating under the old system it was found that gas cleaned by<br />

the wet system saved the plant 0.1591 cents per ton of iron. An<br />

additional advantage of the wet system was that the relatively<br />

clean gas it produced allowed furnace men to decrease the<br />

openings in the checkerwork of the hot blast stoves thereby<br />

substantially increasing the total heating surface of each stove,<br />

which resulted in the production of higher hot blast<br />

temperatures. As a result, the experiment not only substantiated<br />

the value of the wet gas cleaning system for the production and<br />

delivery of combustion air at the Duquesne blast furnace plant<br />

but proved its merit for the entire industry as well.<br />

Between 1908 and the early 1940s the physical features of<br />

the combustion air and production system at Duquesne remained<br />

constant. Between 1943 and the early 1980s, however, the system<br />

became the focal point of a number of significant experiments.<br />

Moreover, the period witnessed installation of major pieces of

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