Case studies in steam system auditing

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CASE STUDIES OF STEAM SYSTEM AUDIT IN SOME PLANTS By K.K.Parthiban, Venus Energy Audit System Introduction This article outlines the outcome of auditing of steam system conducted in process Industries. The details of modifications / improvements carried out may be of use to other boiler users. During the audit the operating staff had exchanged all their experiences and this had resulted in benefit of their plant. Case 1: Steam system auditing in a process industry Interaction & listing of the problems A detailed interaction with various level personnel in the plant resulted in a long list of the problems that could be addressed in order to improve the plant efficiency. The list was quite exhaustive and it included the finer details of the problems as experienced. The studies included both the boiler and the entire steam & condensate system of the plant. For photos refer annexure. The problem, causes & Remedial actions Problem Cause Remedial action Gauge glass There was excess chemical dosage. thinning down. The boiler water pH used to go up 11.8. The normal pH recommended was 9.5 to 10.5. See photo 3 & 4. Replacement at an interval of 10 days. See photo 1. Excess condensate drainage at the first trap itself along the steam line. Frequent choking of the flue tubes in the boiler. Air choking preheater On inspection of the boiler steam drum internal, it was found that there was scope for turbulence of boiler water at the level gauge tapping. See photo 2 Excess chemical dosage has led to foaming inside the drum. See photo 6. Steam risers did not have proper baffles to prevent direct passage of water to drier box. See photo 5 & 7. Wood containing sodium / potassium deposit in the tube sheet at the first pass entrance. Such boilers need precollection chamber & reduction flue gas temperature to less than 650 deg C before shell. See photo 7 & 8. Boilers when fired with high moisture fuels experience flue gas condensation in APH tubes. Simultaneously it leads to ash sticking to the moist surface and leads to choking. See photo 11. The plant personnel were educated on the purpose of chemical dosing. The antiscalant dosage was reduced as the plant has very little make up water. Proposed for baffle box in front of water level gauge. Steam separator baffles added to reduce turbulence inside the steam drum. See figure 1. The chemical dosage was restricted to maintain the boiler water pH to 10.5 Extensive modification carried out in the drum as per figure 2. Suggestion was given for an air operated hose for cleaning the tube sheet on line. This was implemented and the benefits obtained. See figure 3 & photo 9 &10. Steam coil preheater is the right solution. When the air is preheated to 65 deg C, the condensation of water can be avoided. But for this plant pressure jet water

CASE STUDIES OF STEAM SYSTEM AUDIT IN SOME PLANTS<br />

By K.K.Parthiban, Venus Energy Audit System<br />

Introduction<br />

This article outl<strong>in</strong>es the outcome of audit<strong>in</strong>g of <strong>steam</strong> <strong>system</strong> conducted <strong>in</strong> process Industries. The<br />

details of modifications / improvements carried out may be of use to other boiler users. Dur<strong>in</strong>g the<br />

audit the operat<strong>in</strong>g staff had exchanged all their experiences and this had resulted <strong>in</strong> benefit of their<br />

plant.<br />

<strong>Case</strong> 1: Steam <strong>system</strong> audit<strong>in</strong>g <strong>in</strong> a process <strong>in</strong>dustry<br />

Interaction & list<strong>in</strong>g of the problems<br />

A detailed <strong>in</strong>teraction with various level personnel <strong>in</strong> the plant resulted <strong>in</strong> a long list of the<br />

problems that could be addressed <strong>in</strong> order to improve the plant efficiency. The list was quite<br />

exhaustive and it <strong>in</strong>cluded the f<strong>in</strong>er details of the problems as experienced. The <strong>studies</strong> <strong>in</strong>cluded<br />

both the boiler and the entire <strong>steam</strong> & condensate <strong>system</strong> of the plant. For photos refer annexure.<br />

The problem, causes & Remedial actions<br />

Problem Cause Remedial action<br />

Gauge glass There was excess chemical dosage.<br />

th<strong>in</strong>n<strong>in</strong>g down. The boiler water pH used to go up<br />

11.8. The normal pH recommended<br />

was 9.5 to 10.5. See photo 3 & 4.<br />

Replacement at an<br />

<strong>in</strong>terval of 10 days.<br />

See photo 1.<br />

Excess condensate<br />

dra<strong>in</strong>age at the first<br />

trap itself along the<br />

<strong>steam</strong> l<strong>in</strong>e.<br />

Frequent chok<strong>in</strong>g<br />

of the flue tubes <strong>in</strong><br />

the boiler.<br />

Air<br />

chok<strong>in</strong>g<br />

preheater<br />

On <strong>in</strong>spection of the boiler <strong>steam</strong><br />

drum <strong>in</strong>ternal, it was found that there<br />

was scope for turbulence of boiler<br />

water at the level gauge tapp<strong>in</strong>g. See<br />

photo 2<br />

Excess chemical dosage has led to<br />

foam<strong>in</strong>g <strong>in</strong>side the drum. See photo 6.<br />

Steam risers did not have proper<br />

baffles to prevent direct passage of<br />

water to drier box. See photo 5 & 7.<br />

Wood conta<strong>in</strong><strong>in</strong>g sodium / potassium<br />

deposit <strong>in</strong> the tube sheet at the first<br />

pass entrance. Such boilers need precollection<br />

chamber & reduction flue<br />

gas temperature to less than 650 deg C<br />

before shell. See photo 7 & 8.<br />

Boilers when fired with high moisture<br />

fuels experience flue gas condensation<br />

<strong>in</strong> APH tubes. Simultaneously it leads<br />

to ash stick<strong>in</strong>g to the moist surface and<br />

leads to chok<strong>in</strong>g. See photo 11.<br />

The plant personnel were educated<br />

on the purpose of chemical dos<strong>in</strong>g.<br />

The antiscalant dosage was reduced<br />

as the plant has very little make up<br />

water.<br />

Proposed for baffle box <strong>in</strong> front of<br />

water level gauge. Steam separator<br />

baffles added to reduce turbulence<br />

<strong>in</strong>side the <strong>steam</strong> drum. See figure 1.<br />

The chemical dosage was restricted<br />

to ma<strong>in</strong>ta<strong>in</strong> the boiler water pH to<br />

10.5<br />

Extensive modification carried out<br />

<strong>in</strong> the drum as per figure 2.<br />

Suggestion was given for an air<br />

operated hose for clean<strong>in</strong>g the tube<br />

sheet on l<strong>in</strong>e. This was<br />

implemented and the benefits<br />

obta<strong>in</strong>ed. See figure 3 & photo 9<br />

&10.<br />

Steam coil preheater is the right<br />

solution. When the air is preheated<br />

to 65 deg C, the condensation of<br />

water can be avoided.<br />

But for this plant pressure jet water


Corrosion of ducts<br />

Excess<br />

consumption<br />

Improvement<br />

process<br />

performance.<br />

fuel<br />

<strong>in</strong><br />

Outside air <strong>in</strong>gress is seen <strong>in</strong> to APH<br />

caus<strong>in</strong>g condensation of flue gas<br />

moisture. See photo 12.<br />

Boilers with biomass fir<strong>in</strong>g need<br />

<strong>in</strong>sulation right up to chimney <strong>in</strong>let to<br />

prevent moisture condensation <strong>in</strong> the<br />

ducts. See photo 13 & 14.<br />

Auto air vents were seen <strong>in</strong>stalled <strong>in</strong><br />

the <strong>steam</strong> pip<strong>in</strong>g. These were not<br />

ma<strong>in</strong>ta<strong>in</strong>ed. The <strong>steam</strong> was mistaken<br />

as air by the operat<strong>in</strong>g staff. See photo<br />

15.<br />

So many valves were not <strong>in</strong>sulated at<br />

all. See photo 16 & 17<br />

Steam loss was very high at the traps.<br />

See 18.<br />

Wrong trap arrangement was seen at<br />

several places. Traps are not located<br />

for easy <strong>in</strong>spection. See photo 19.<br />

clean<strong>in</strong>g was advised.<br />

Tubes fail periodically. It is<br />

necessary to understand the<br />

periodicity of replacement & plan<br />

spare.<br />

The <strong>in</strong>spection door needed<br />

strengthen<strong>in</strong>g. Every time any<br />

<strong>in</strong>spection door is opened only fresh<br />

seal rope must be provided.<br />

It was advised to <strong>in</strong>sulate all the<br />

ducts up to Chimney <strong>in</strong>let and arrest<br />

all <strong>in</strong>gress.<br />

Advised to close the auto air vent.<br />

Air vents are provided only <strong>in</strong> heat<br />

exchangers. These are aga<strong>in</strong><br />

required if there is a possibility of<br />

air trapp<strong>in</strong>g.<br />

Valves are to be <strong>in</strong>sulated with<br />

removable pad <strong>in</strong>sulation. This<br />

br<strong>in</strong>gs down the radiation loss to<br />

surround<strong>in</strong>g.<br />

Traps at unnecessary places were<br />

closed down.<br />

Wherever the traps are required and<br />

the traps had started pass<strong>in</strong>g <strong>steam</strong>,<br />

the bypass l<strong>in</strong>es were cracked<br />

optimally to br<strong>in</strong>g down the loss.<br />

Right trap arrangement was given.<br />

Wrong orientation of traps was<br />

corrected.<br />

Regular <strong>in</strong>spection of traps is a<br />

must. For audit<strong>in</strong>g IR camera &<br />

ultrasonic probe come <strong>in</strong> handy. See<br />

photo 19 & 20.<br />

<strong>Case</strong> 2: Audit of a coal fired unit <strong>in</strong> a paper mill<br />

The customer had requested for an audit of their plant to br<strong>in</strong>g down the coal consumption. The<br />

boiler was orig<strong>in</strong>ally a husk fired. Later due to fuel price escalations, customer switched over to<br />

coal fir<strong>in</strong>g most of the year.<br />

The problem, causes & Remedial actions<br />

Problem Cause Remedial action<br />

High coal Vibratory feeder used <strong>in</strong> place of For coal feeders only rotary / drag<br />

consumption rotary feeder. See photo 22.<br />

The oxygen level was so much<br />

hunt<strong>in</strong>g, ( see figure 24, 25 & 26) hat<br />

cha<strong>in</strong> feeder to be used.<br />

Customer was advised about the art<br />

of fuel feed regulation. The CO


the fuel did not burn <strong>in</strong> the furnace<br />

result<strong>in</strong>g <strong>in</strong> high carbon <strong>in</strong> bed ash<br />

itself. See photo 23.<br />

The surface temperature audit by IR<br />

camera proved that lot of scope exists<br />

<strong>in</strong> reduc<strong>in</strong>g the heat loss to ambient.<br />

See photo 27, 28 & 29.<br />

Process side heat loss was also high.<br />

In the paper <strong>in</strong>dustry, the dry<strong>in</strong>g<br />

cyl<strong>in</strong>ders meant for dry<strong>in</strong>g the paper<br />

was without the end radiation shields.<br />

ppm exceeded 5000 ppm.<br />

Insulation was advised to this<br />

customer.<br />

The surface temperatures between<br />

the case with radiation shield & the<br />

case without the shield were shown<br />

to client. One can see the IR camera<br />

outputs at the annexure. See photo<br />

30 & 31.<br />

<strong>Case</strong> 3: Audit of a biomass fired boiler <strong>in</strong> a paper mill<br />

The customer had requested for an operational audit of their boiler to br<strong>in</strong>g down the fuel<br />

consumption and to address the dust compla<strong>in</strong>t from nearby factories. The boiler was orig<strong>in</strong>ally a<br />

wood fired boiler. Later due to non availability of wood the boiler was converted to FBC fir<strong>in</strong>g<br />

with external refractory furnace walls. The biomass fuels used <strong>in</strong>clude rice husk, tamar<strong>in</strong>d shell,<br />

ground nut shell, coffee husk.<br />

The problem, causes & Remedial actions<br />

Cl<strong>in</strong>ker<br />

<strong>in</strong> bed.<br />

formation<br />

ID fan capacity<br />

<strong>in</strong>adequate<br />

Chimney failure<br />

Dust<br />

from<br />

factory.<br />

compla<strong>in</strong>t<br />

adjourn<strong>in</strong>g<br />

The fuels used have ash fusion<br />

temperatures as low as 750 deg C.<br />

There was cl<strong>in</strong>ker formation above the<br />

bed on the wall due to high free board<br />

temperature excursions & due to<br />

presence of uncooled walls.<br />

It was seen that the air / flue gas<br />

duct<strong>in</strong>g is designed <strong>in</strong> a haphazard<br />

manner. See photo 34.<br />

It was seen that the ID fan is provided<br />

with a damper right at the fan <strong>in</strong>let.<br />

Such obstructions br<strong>in</strong>g down the fan<br />

performance. See photo 33.<br />

This is a common phenomenon <strong>in</strong><br />

many plants. The cause is the high<br />

moisture content <strong>in</strong> fuel & low<br />

exhaust temperature.<br />

Though the ash content is less, due to<br />

improper combustion, improper ash<br />

collection <strong>system</strong> comb<strong>in</strong>ed with<br />

condensation of water vapor has<br />

caused carbon particulate.<br />

Furnace is not provided with over-fire<br />

air arrangement. High volatile fuels<br />

The combustion temperatures were<br />

adjusted for a lower bed<br />

temperature.<br />

The biomass of foul<strong>in</strong>g nature<br />

needs waterwall furnace enclosure.<br />

Only flue gas recycl<strong>in</strong>g is to be<br />

done now to reduce the furnace<br />

temperature.<br />

Duct<strong>in</strong>g reeng<strong>in</strong>eer<strong>in</strong>g was advised<br />

to br<strong>in</strong>g down the draft loss.<br />

Customer was advised to remove<br />

the flap from the damper and to<br />

provide multi flap damper <strong>in</strong> the<br />

MDC outlet duct.<br />

The exhaust temperature at chimney<br />

top should be over 110 deg C. This<br />

can be improved by <strong>in</strong>sulat<strong>in</strong>g the<br />

gas duct<strong>in</strong>g up to chimney <strong>in</strong>let.<br />

Customer was advised for rotary<br />

ash feeder at all ash collection<br />

po<strong>in</strong>ts. In addition unconventional<br />

dust traps as seen <strong>in</strong> photo 32 & 33<br />

were added.<br />

Customer was advised to<br />

<strong>in</strong>corporate secondary air <strong>system</strong>.


Frequent boiler<br />

feed pump failure<br />

Conclusion<br />

need a good turbulence above the bed,<br />

particularly <strong>in</strong> over bed feed <strong>system</strong>.<br />

This is required to burn off the<br />

unburnt gases.<br />

The feed pump suction pip<strong>in</strong>g is with<br />

mistakes that take away the NPSH.<br />

See photo 35, 36 & 37.<br />

See<strong>in</strong>g the CO values <strong>in</strong> the flue gas<br />

at shell outlet the over-fire air has to<br />

be adjusted.<br />

Customer was advised to remove<br />

the thermocouple & flow meter<br />

immediately. If problem persists,<br />

globe valve shall be replaced with<br />

gate valve.<br />

Generally <strong>in</strong> all the plants there rema<strong>in</strong>s a good scope for fuel sav<strong>in</strong>gs & for improv<strong>in</strong>g the <strong>steam</strong><br />

generat<strong>in</strong>g & distribut<strong>in</strong>g <strong>system</strong>. There are numerous cases where plant eng<strong>in</strong>eers & operators<br />

have <strong>in</strong>corporated many improvements. The users could br<strong>in</strong>g out their achievements <strong>in</strong> this boiler<br />

meet <strong>in</strong> the further years.


Photo 1: Gauge glass seen eroded. This failure<br />

took place every week.<br />

Photo 2: Gauge glass located close to risers.<br />

This causes turbulence <strong>in</strong> water level gauge.<br />

Figure 1:<br />

Photo 3: Excess chemicals have led to whitish<br />

deposit seen <strong>in</strong> the shell above the tubes.<br />

Photo 4: Rear tube sheet seen with whitish<br />

deposit. If hardness salts are present, tubes<br />

would be seen with deposits.


Photo 5: A baffle box provided at one end of the<br />

drum did not have level equalizer. The <strong>steam</strong><br />

water mixture would have to climb over the box.<br />

Photo 6: Steam separator seen with foam<strong>in</strong>g<br />

mark <strong>in</strong>dicat<strong>in</strong>g the drum was under turbulent<br />

water level.<br />

Figure 2:<br />

Photo 7: Risers do not have a cap. Thus the<br />

water can go directly to the <strong>steam</strong> pipe nearby.<br />

Photo 8: Inlet of the I pass tubes at shell. A view<br />

after clean<strong>in</strong>g. Old deposits could be seen.


Figure 3:<br />

Photo 9: Compressor l<strong>in</strong>ed up for ash deposit<br />

removal.<br />

Photo 10: Clean<strong>in</strong>g ports <strong>in</strong> the <strong>in</strong>spection door.<br />

Compressed air l<strong>in</strong>e is taken out of port.<br />

Photo 11: Fresh air <strong>in</strong>gress to APH causes gas<br />

condensation lead<strong>in</strong>g to corrosion & chok<strong>in</strong>g.<br />

Photo 12: Improper APH <strong>in</strong>spection door<br />

seat<strong>in</strong>g leads to cold <strong>in</strong>gress.


Photo 13: Shell <strong>in</strong>termittent hopper (not<br />

<strong>in</strong>sulated?)with improper flange seat<strong>in</strong>g<br />

allow<strong>in</strong>g air <strong>in</strong>gress.<br />

Photo 14: MDC cones seen coated with<br />

condensed ash deposits. Insulation is advised.<br />

Photo 15: Unnecessary air vent <strong>in</strong> ma<strong>in</strong> <strong>steam</strong><br />

l<strong>in</strong>e. At high po<strong>in</strong>ts, only a vent is required for<br />

air release dur<strong>in</strong>g hydrotest.<br />

Photo 16:Un<strong>in</strong>sulated valves result <strong>in</strong> heat loss.<br />

Photo 17: Un<strong>in</strong>sulated valves result <strong>in</strong> heat loss.<br />

Photo 18: Steam seen gush<strong>in</strong>g out of trap. There<br />

were traps downstream & hence this was closed.


Photo 19: In accessible traps – not suited for<br />

regular check.<br />

Photo 20: Audit<strong>in</strong>g equipment – Infrared camera<br />

– for identify<strong>in</strong>g defective trap, bear<strong>in</strong>gs &<br />

electrical panels.<br />

Photo 21: Energy audit equipment – ultrasonic<br />

probe for various application<br />

Photo 22: Vibratory feeder be<strong>in</strong>g used for coal<br />

feed<strong>in</strong>g <strong>in</strong> an FBC boiler. Boiler designed for<br />

husk.<br />

Photo 23: Unburnt coal seen <strong>in</strong> the bed ash<br />

itself. It is not practically adjust required coal<br />

feed rate with vibratory feeder. The LOI ranged<br />

to 2% <strong>in</strong> this case.<br />

Photo 24: The Oxygen analyzer is provided to<br />

ensure Oxygen is available for combustion. If<br />

load is vary<strong>in</strong>g then the m<strong>in</strong>imum Oxygen has<br />

to be 3.5%.<br />

.


Photo 25<br />

Photo 26<br />

Photo 27: Un<strong>in</strong>sulated areas <strong>in</strong> a bi-drum boiler<br />

Photo 28: Almost at all sealbox the temperatures<br />

run over the stipulated ambient + 20 deg C. Max<br />

temperature is 197 deg C.<br />

Photo 29: Close to the bottom drum, <strong>in</strong> the<br />

f<strong>in</strong>ned area, temperature is seen to be maximum<br />

of 202 deg C.<br />

Photo 30: In a paper <strong>in</strong>dustry, the dry<strong>in</strong>g<br />

cyl<strong>in</strong>ders are not covered by many. This one is<br />

without a cover. We may see the peak<br />

temperature is 154 deg C.


Photo 31: This cyl<strong>in</strong>der is with a cover. These<br />

dry<strong>in</strong>g cyl<strong>in</strong>ders rotate at a speed. Naturally the<br />

convection heat loss will be predom<strong>in</strong>ant as<br />

compared to radiation mode heat loss.<br />

Photo 32: Ideas to reduce dust emission <strong>in</strong> small<br />

boilers<br />

Photo 33: A way to reduce dust emission.<br />

Further at all ash collection po<strong>in</strong>ts rotary feeders<br />

added.<br />

Photo 34. Haphazard duct<strong>in</strong>g adds up to higher<br />

draft loss. Customer had gone ahead with<br />

replacement of fans.<br />

Photo 35, 36 & 37 show the mistakes made <strong>in</strong> feed pump suction pip<strong>in</strong>g that the frequently the<br />

pumps fails to pump due to cavitation. Thermocouple <strong>in</strong> the l<strong>in</strong>e, flow meter & globe valve <strong>in</strong> pump<br />

suction l<strong>in</strong>e creates loss of NPSH.

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