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A Review of Criticality Accidents A Review of Criticality Accidents

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21. Novosibirsk Chemical Concentration Plant, 15 May 1997<br />

Uranium oxide slurry and crust, U(70), in the lower regions <strong>of</strong> two parallel vessels; multiple excursions;<br />

insignificant exposures.<br />

This accident occurred in Building 17 where highly<br />

enriched U(90) fuel rods were fabricated from UO 2<br />

and aluminum, using the powder metallurgy method.<br />

The final process prior to placing a rod into its aluminum<br />

cladding was chemical etching. The objective <strong>of</strong><br />

this operation was to remove microscopic defects on<br />

the rod surfaces to ensure tight contact between the rod<br />

and its cladding. The major components <strong>of</strong> the process<br />

equipment are shown in Figure 32.<br />

The etching process involved consecutively immersing<br />

a batch <strong>of</strong> rods into three separate vessels filled<br />

with sodium hydroxide (alkali), water, and nitric acid,<br />

respectively. As a result <strong>of</strong> a chemical reaction with the<br />

sodium hydroxide, some <strong>of</strong> the aluminum particles on<br />

the surface <strong>of</strong> the rods formed the precipitates, NaAlO 3<br />

and Al(OH) 3 . The etching process leached a small<br />

fraction <strong>of</strong> the uranium dioxide from the rods which<br />

was also deposited on the bottom <strong>of</strong> the alkali vessel.<br />

The rods were then washed in the second vessel with<br />

water to remove as much alkali as possible. In the final<br />

vessel <strong>of</strong> nitric acid, any traces <strong>of</strong> alkali were neutralized<br />

and the rods were etched to their final size by<br />

dissolving UO 2 particles from their surfaces.<br />

50<br />

Alkali Water Acid<br />

59-A<br />

Receiver<br />

Vessels<br />

59-B<br />

Collection<br />

Vessel<br />

To Recovery<br />

Figure 32. Major components <strong>of</strong> the chemical-etching<br />

process.<br />

Once the etching process with one batch <strong>of</strong> rods<br />

was completed, the contents from all three immersion<br />

vessels was gravity drained to a 130 mm diameter<br />

cylindrical collection vessel. As the collection vessel<br />

filled, the etching solution was pumped to receiver<br />

vessels 59-A and 59-B through a 64 mm diameter pipe<br />

that was about 100 m in length. Eventually, the etching<br />

solution would be transferred from the receiver vessels<br />

to the uranium recovery section <strong>of</strong> the building.<br />

The etching process had been standardized 13 years<br />

before the criticality accident. During this 13 year<br />

period, the controlled parameters were the number <strong>of</strong><br />

rods per batch, the temperature, the concentration <strong>of</strong><br />

the reagents, and the duration <strong>of</strong> the immersion<br />

operations. Uranium content in the etching solutions<br />

was not measured. In fact, since all <strong>of</strong> the equipment,<br />

with the exception <strong>of</strong> the immersion vessels, was <strong>of</strong><br />

favorable geometry (according to design and records),<br />

there was no capability within the building to determine<br />

the uranium content <strong>of</strong> the etching solutions.<br />

Precipitate formation and uranium deposition in the<br />

service piping was also not monitored.<br />

In 1996 a solid UO 2 deposit was discovered in the<br />

collection vessel when it was opened and inspected.<br />

The 5.5 kg deposit (uranium mass fraction <strong>of</strong> ~69%)<br />

was gradually removed by dissolving it with nitric<br />

acid. Analyses showed that the deposit had been<br />

forming for over 10 years since it contained some<br />

uranium enriched to only 36% by weight. Uranium<br />

enriched to 36% by weight had not been processed<br />

since around 1986 when a switch to U(90) was made.<br />

Despite the discovery <strong>of</strong> this deposit, the logical<br />

search for similar deposits in the service piping and in<br />

the receiver vessels was not initiated, primarily<br />

because the criticality safety limits for those components<br />

did not include requirements to monitor for<br />

uranium accumulation. In fact, for the purposes <strong>of</strong> the<br />

annual material inventory, the entire building was<br />

designated as one fissile material balance area.<br />

Therefore, the small fraction <strong>of</strong> uranium being deposited<br />

in the receiver vessels per batch <strong>of</strong> rods went<br />

unnoticed because <strong>of</strong> the large size <strong>of</strong> the fissile<br />

material balance area.<br />

The receiver vessels were <strong>of</strong> slab geometry, with<br />

common inlet and outlet lines for the transfer <strong>of</strong><br />

solutions. Each vessel was 3.5 m in height and 2 m in<br />

length, with a design thickness <strong>of</strong> 100 mm and an<br />

operating volume <strong>of</strong> ~650 l. Both vessels were made<br />

from 4 mm thick stainless steel. The distance between<br />

the vessels was 0.8 m, and they were mounted ~0.75 m<br />

above the concrete floor. Dimensional control <strong>of</strong> the<br />

thickness was provided by internal steel rods welded

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