09.12.2012 Views

A Review of Criticality Accidents A Review of Criticality Accidents

A Review of Criticality Accidents A Review of Criticality Accidents

A Review of Criticality Accidents A Review of Criticality Accidents

SHOW MORE
SHOW LESS

You also want an ePaper? Increase the reach of your titles

YUMPU automatically turns print PDFs into web optimized ePapers that Google loves.

12. Siberian Chemical Combine, 30 January 1963<br />

Uranyl nitrate solution, U(90), in a collection vessel; multiple excursions; insignificant exposures.<br />

This accident occurred in a waste recovery line <strong>of</strong> a<br />

uranium metal production building. The waste feed<br />

was a dry precipitate. The first step in recovering the<br />

uranium was a time–intensive, concentrated nitric acid<br />

dissolution process. Two sets <strong>of</strong> identical equipment<br />

were used to increase the throughput and to optimize<br />

the process. Figure 18 is a material flow diagram for<br />

this process.<br />

The solution was vacuum transferred from the<br />

dissolution vessels to the intermediate feed vessels,<br />

through a filter vessel, and then finally to the collection<br />

vessels. The dissolution and intermediate vessels were<br />

320 mm in diameter and 520 mm in height. The<br />

collection vessels were 390 mm in diameter and<br />

500 mm in height. All <strong>of</strong> the vessels had curved ends<br />

and were about 50 l in volume. Since the process<br />

vessels were not favorable geometry, limiting the<br />

fissile material mass was the only control used to<br />

prevent criticality accidents. Compliance with the mass<br />

limit was solely dependent on the reliability <strong>of</strong> the<br />

chemical analysis <strong>of</strong> the dry precipitate.<br />

Despite the importance <strong>of</strong> chemical analysis results<br />

for implementing the criticality safety mass control,<br />

there were two allowed reporting formats:<br />

Intermediate<br />

Vessels<br />

Figure 18. Process vessels and material flow diagram.<br />

30<br />

61-A<br />

62-A<br />

Filter<br />

Vessel<br />

63<br />

Collection<br />

Vessels<br />

62-B<br />

61-B<br />

64-A 64-B<br />

Dissolution<br />

Vessels<br />

1. as grams <strong>of</strong> uranium per kilogram <strong>of</strong> precipitate,<br />

g U(90)/kg, or<br />

2. as a mass fraction, the uranium-to-precipitate mass<br />

ratio.<br />

The bulk amount <strong>of</strong> precipitate to be processed was<br />

calculated using the results <strong>of</strong> the chemical analysis.<br />

The precipitate was then weighed before loading into<br />

the dissolution vessels.<br />

When dissolving consecutive batches <strong>of</strong> precipitate,<br />

the operational procedure allowed for the recycling <strong>of</strong><br />

solution with low uranium concentration from the<br />

collection vessels, as long as the total mass <strong>of</strong> uranium<br />

in the dissolution vessels did not exceed 400 g. The<br />

uranium concentration in the recycled solution was<br />

determined by analyzing samples from the collection<br />

vessels. This concentration was always reported as<br />

grams <strong>of</strong> uranium per liter (g U/ l) and was also used<br />

for compliance with the criticality safety mass limit.<br />

On 30 January 1963, two waste containers were<br />

received at the waste recovery line with the chemical<br />

analysis results attached. These results were reported<br />

as a mass fraction, approximately 0.18 in this case. The<br />

supervisor for the shift erroneously recorded this result<br />

in the work orders as 18 g U/kg <strong>of</strong> dry precipitate<br />

(instead <strong>of</strong> 180). The actual uranium content in this<br />

batch <strong>of</strong> dry precipitate was thus in error and underestimated<br />

by a factor <strong>of</strong> 10.<br />

Using the erroneous work orders, an operator<br />

loaded 2 kg <strong>of</strong> precipitate from one container and 5 kg<br />

from another into dissolution vessel 61-A, believing<br />

the total uranium content to be 126 g when it was<br />

actually about 1,260 g. Because <strong>of</strong> a shift change, a<br />

different operator completed the dissolution process.<br />

The solution was then filtered and transferred to<br />

collection vessel 64-A, where a sample was taken to<br />

determine the concentration. Later during that same<br />

shift, the operator asked for the sample results by<br />

telephone. While this normally would have led to the<br />

discovery <strong>of</strong> the original recording error, the laboratory<br />

erroneously reported the results for a vessel other than<br />

64-A. By an unfortunate coincidence, this other vessel<br />

contained solution with a uranium concentration<br />

10 times lower than that in 64-A, thus reinforcing the<br />

operator’s expectations.<br />

The supervisor for the second shift, relying on this<br />

erroneous information, decided to recycle this supposedly<br />

low concentration solution to dissolve the next<br />

batch <strong>of</strong> dry precipitate. This next batch, still subject to<br />

the original recording error, contained ~1,255 g <strong>of</strong><br />

uranium, about the same as that <strong>of</strong> the preceding batch.<br />

The dry precipitate was loaded into dissolution<br />

vessel 61-A and then the solution from collection

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!