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A Review of Criticality Accidents A Review of Criticality Accidents

A Review of Criticality Accidents A Review of Criticality Accidents

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heater and stirrer were turned <strong>of</strong>f again, leading to a<br />

second excursion at 01:10. This was apparently no<br />

larger than the first, as it did not trip detectors that had<br />

not tripped during the first excursion.<br />

After this second excursion the plant and building<br />

managers arrived at the accident site along with the<br />

manager <strong>of</strong> the safety organization and supporting<br />

physicists. They then directed further recovery operations.<br />

Attempts to remotely drain vessel 2 by various<br />

means continued until a third and final excursion<br />

occurred at 01:55. Detectors which had not previously<br />

tripped (some as far away as 150 m) were activated,<br />

indicating that this third excursion was the largest. At<br />

this time the stirrer and heater were once again turned<br />

on (to keep the system subcritical) and left on until the<br />

solution could finally be transferred from vessel 2.<br />

The final draining <strong>of</strong> the vessel was a two–part<br />

process. First, about one–half <strong>of</strong> the solution in<br />

vessel 2 was transferred to an aqueous collection vessel<br />

and then from there partitioned into several bottles.<br />

This procedure was then repeated with the remaining<br />

solution in vessel 2. All the bottles were stored in an<br />

isolated room, and the contents were reprocessed only<br />

after the radiation levels decreased to acceptable levels.<br />

The trip level <strong>of</strong> the criticality alarm detectors was<br />

110 mR/h. They were spaced a maximum <strong>of</strong> 30 m<br />

apart but were commonly much closer. Fifteen minutes<br />

after the first excursion the exposure rate in the vicinity<br />

<strong>of</strong> the glovebox was about 2.2 R/h. Thirty minutes after<br />

the third excursion the exposure rate in the vicinity <strong>of</strong><br />

the glovebox was about 1.8 R/h.<br />

Ultimately it was determined that there had been a<br />

total <strong>of</strong> 1,324 g <strong>of</strong> plutonium in the dissolution vessel<br />

Stirrer Motor<br />

Water<br />

Nitric Feed<br />

Reagent Addition Line<br />

Product Discharge Line<br />

Inspection Light<br />

Stirrer<br />

Steam/Water Jacket<br />

Dissolution Vessel #1 Dissolution Vessel #2<br />

Figure 17. Layout <strong>of</strong> glovebox equipment.<br />

at the time <strong>of</strong> the accident. This was about three times<br />

the criticality safety limit. The recovered nitric solution<br />

contained 933 g <strong>of</strong> plutonium and a very rich precipitate<br />

was found in the bottom <strong>of</strong> vessel 2. It contained<br />

391 g <strong>of</strong> plutonium in 660 g <strong>of</strong> solids; the remainder<br />

was mostly graphite pulp from molds. Using approximate<br />

techniques, the energy release for all three<br />

excursions was estimated at 2 × 1017 fissions. The<br />

excursion history was not recorded. There was minor<br />

ejection <strong>of</strong> solution from the vessel onto the glovebox<br />

floor, likely from the third excursion.<br />

Several factors contributed to the accident:<br />

• Unfavorable geometry equipment.<br />

• The charging <strong>of</strong> high grade residues into the dissolution<br />

vessel when the criticality controls were<br />

based on residues with an average 1% plutonium<br />

content.<br />

• Inadequate isolation <strong>of</strong> high grade residues from the<br />

more common low grade residues in the staging<br />

glovebox.<br />

• Unclear and difficult to read labels on the residue<br />

cans.<br />

• Procedural violations on the sequence <strong>of</strong> reagent<br />

additions.<br />

• Inadequate supervisory monitoring <strong>of</strong> operations;<br />

inadequate attention to the completion <strong>of</strong> accountancy<br />

documents.<br />

• Lack <strong>of</strong> real time fissile material accounting instrumentation.<br />

No equipment damage occurred and only a short<br />

downtime was needed to clean up the spilled solution.<br />

29

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