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—Continued from previous page<br />
Then we waited for the epoxy to set, but something wasn’t right. As we watched,<br />
the West System 309 epoxy mixture continued to run out of the bottom of the rudder<br />
sleeve — it wouldn’t harden. As happy hour approached, we decided to drop the<br />
rudder and try again the next day with a 306 mix.<br />
After morning coffee and crosswords, we started in again. The rudder shaft was<br />
thoroughly cleaned and re-waxed. The sleeve was sanded with 60-grit sandpaper<br />
wrapped around a broom handle and washed with acetone. The rudder was inserted<br />
and the process repeated. This time the epoxy hardened. The rudder was broken<br />
free and exercised back and forth while a solution of dish soap was poured from the<br />
top to act as a lubricant. Back and forth, back and forth — for hours, but the action<br />
was much too tight. It was so tight that it’s doubtful I would be able to steer the boat<br />
for a three-hour watch, and Freeman the autopilot would burn itself out right away.<br />
It looked like we’d made a worse problem than the one we were trying to fix!<br />
We didn’t have much time to be depressed over this situation. When you live in the<br />
same boatyard every year for a month or two, you become part of the local community,<br />
and it didn’t take long for word of our situation to become general knowledge.<br />
Typical of the spirit that guides this organization, help soon arrived in the person of<br />
Donald Stollmeyer, Operations Manager and a General Partner in Power Boats in<br />
Chaguaramas, Trinidad, and a builder of custom catamarans in his spare time.<br />
Donald’s presence soon attracted the neighboring yachties and before we knew it,<br />
our rudder became an interesting problem to solve rather than a catastrophe.<br />
Some special K.I.S.S.<br />
ingredients: part of<br />
an old acetone bottle,<br />
a hunk of foam and<br />
a plastic mailing tube<br />
for charts<br />
The first step was to take the rudder out again, clean it up and see just how bad<br />
the problem was. To our relief, we were able to work the rudder slowly out — in fact,<br />
it was easy because the heavy rudder was held so tightly that no blocks were needed<br />
to keep it from dropping suddenly into its hole! It’s strange to see a rudder literally<br />
hanging in mid-air. After washing and microfining, the rudder action was much<br />
better. A little sanding and we would be able to steer normally, but there was still<br />
the same slop in the rudder. The epoxy had not migrated more than halfway down<br />
the sleeve, and the greatest area of wear was at the bottom.<br />
The Captain wasn’t about to settle for anything less than making it right. Our<br />
“committee” got to work. Using a pair of red plastic calipers, it was determined that<br />
the sleeve was three millimeters larger than the shaft, with a deeper groove at the<br />
very bottom. Looking around under the boat, an empty plastic acetone bottle was<br />
found and measured. It was slightly fatter than the shaft. Using blue masking tape<br />
as a straight edge, a thin slice was cut out of the bottle and the excess cut out. This<br />
was inserted into the rudder sleeve at the top of the deeper groove as a guide for<br />
where the first fill of epoxy would stop. Using a stick found under the boat, Donald<br />
mixed the epoxy, troweled it into the groove and removed the guide strip. A four-inch<br />
section of the cut-down acetone bottle with a hunk of foam rubber inside was inserted<br />
to push the epoxy against the sides of the groove. A piece of wood was taped over<br />
To make manhandling<br />
the<br />
heavy rudder<br />
easier, one of the<br />
thick scaffold<br />
boards was used<br />
as a lever<br />
the bottom of the hole to keep it all in place, and everybody went to lunch while the<br />
epoxy hardened. The groove was now filled evenly with the rest of the sleeve.<br />
For the next application of epoxy, graphite was added to make a slippery surface<br />
to allow the rudder shaft to move more easily in the tightened sleeve. The sleeve was<br />
wet sanded and washed with acetone. Looking around, a stiff plastic mailing tube<br />
for charts was found under a neighboring boat. It was two millimeters smaller than<br />
the final rudder sleeve needed to be. Using two-inch plastic tape, the tube was built<br />
up to the desired final thickness and coated with the mold-release wax. The epoxy<br />
mixture was troweled up into the sleeve, the mailing tube was inserted and turned<br />
gently to help distribute the graphite epoxy around the walls of the sleeve. It was<br />
then taped in place and left to harden overnight.<br />
Next morning, the tube was removed. It was time to see if the rudder shaft would go into<br />
the sleeve. To make manhandling the heavy rudder easier, one of the thick scaffold boards<br />
was used as a lever. Two men would lift the rudder, one would stand on the board to hold<br />
it up while the fourth shifted the heavy wooden blocks across the water-filled hole.<br />
Of course, the rudder would not go in the first time. There were some high places,<br />
especially around the very bottom, that needed to be smoothed down. Flipping the<br />
mailing tube around, 220-grit wet sandpaper was attached to the tube with spray<br />
adhesive. This was used to sand the inside of the sleeve. After several rounds of sanding<br />
and re-inserting the rudder, a proper fit was achieved — no more slop and no<br />
more thumps. The rudder moved easily.<br />
Thanks to Donald and the committee of yachties at Power Boats, Forever Young<br />
was ready to go back in the water with her crew of three: Captain, First Mate and<br />
Freeman the autopilot.<br />
JANUARY 2008 CARIBBEAN COMPASS PAGE 33