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Kaizen in Qc Microbiology – Kaizen Institute India

In this documents we are revealing Kaizen Institute role in QC MicorBiology for various Jobs. To find more details check out: http://in.kaizen.com/

In this documents we are revealing Kaizen Institute role in QC MicorBiology for various Jobs. To find more details check out: http://in.kaizen.com/

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SEPTEMBER 2013<br />

1


Project: POTABLE WATER SAMPLING FREQUENCY REDUCTION<br />

Production units : Gemba :QCM Lab Location : campus<br />

Status : Before <strong>Kaizen</strong><br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

31 potable water sampl<strong>in</strong>g po<strong>in</strong>ts tested for Total<br />

viable count and pathogens {number of tests-6] once<br />

<strong>in</strong> 15 days<br />

Evidence on the possible risk <strong>in</strong>volved <strong>in</strong><br />

reduc<strong>in</strong>g the test<strong>in</strong>g frequency was gathered and<br />

recommendation of any control measure<br />

required on the risk identified for 31 potable<br />

water sampl<strong>in</strong>g po<strong>in</strong>ts located at SFP, IFP, PFP<br />

and other facility was identified.<br />

2


Risk assessment be<strong>in</strong>g performed by assess<strong>in</strong>g the mode of failure with control measures.<br />

Risk rat<strong>in</strong>g be<strong>in</strong>g evaluated by multiply<strong>in</strong>g the risk level (severity) with available control measures.<br />

Based on the assessment sampl<strong>in</strong>g po<strong>in</strong>ts was recommended for a sampl<strong>in</strong>g frequency of once a month<br />

Results & Benefits Summary<br />

Previous<br />

Total sampl<strong>in</strong>g po<strong>in</strong>ts analyzed = 31 po<strong>in</strong>ts analyzed for every 15<br />

days<br />

Media Cost : for each analysis 160/- Rs.<br />

160 * 31 (sampl<strong>in</strong>g po<strong>in</strong>ts) = 4960/- * 2 (monthly twice) = 9920/-<br />

Filter paper: For Each analysis 10/- Rs<br />

10* 155(no. of filter papers for 31 sampl<strong>in</strong>g po<strong>in</strong>ts) = 1550/- (for 15<br />

days) * 2 = 3100/- per month<br />

Man Power : For each analysis 20m<strong>in</strong>utes<br />

20 * 31 (sampl<strong>in</strong>g po<strong>in</strong>ts) = 620 m<strong>in</strong>utes for 15 days<br />

620 * 2 = 1240 m<strong>in</strong>utes per month or 20.6 hr.<br />

HDPE Sampl<strong>in</strong>g Bottles : For each analysis 1 bottle per sampl<strong>in</strong>g<br />

po<strong>in</strong>t = 12/- per bottle<br />

12 * 31 = 372/- Rs. For 15 days , 372*2 = 744/-<br />

Total Cost = 1,65,168/-<br />

Total Time = 247.2 hr. per year<br />

After kaizen<br />

Total sampl<strong>in</strong>g po<strong>in</strong>ts analyzed = 31 po<strong>in</strong>ts analyzed<br />

for every one month<br />

4960/- per month<br />

Process Map Before & After <strong>Kaizen</strong><br />

1550/- per month<br />

10.3 hours per month<br />

372/- per month<br />

Total Cost = 82,584/-<br />

Total Time = 123.6 hr. per year<br />

3


Project :BMR REVISION<br />

Production units : NA Gemba :QCM Lab Location : campus<br />

Status : Before <strong>Kaizen</strong><br />

BMR is lengthy and time consum<strong>in</strong>g to fill them<br />

Repetitive entries<br />

Signatures required <strong>in</strong> many place<br />

Media preparation activity stage wise<br />

Sterilization chart pasted <strong>in</strong> BMR -duplication of<br />

autoclave log book<br />

Results & Benefits Summary<br />

Park BMR’s revised<br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

Campus BMR’s - 16 numbers<br />

Reduction <strong>in</strong> number of pages, consolidation of raw<br />

material entry, media preparation activity for SF and IF<br />

comb<strong>in</strong>ed, number of signatures reduced. Repetitive text<br />

removed<br />

Expected to be complete by 15/09/2013<br />

Biological BMR’s -7 numbers<br />

Documentation time reduced by 60%; Prepr<strong>in</strong>t<strong>in</strong>g of<br />

entries, number of signatures reduced<br />

Process Map Before & After <strong>Kaizen</strong><br />

Cost sav<strong>in</strong>gs for paper & pr<strong>in</strong>t<strong>in</strong>g <strong>–</strong> to be estimated<br />

Before<br />

After<br />

Reduction <strong>in</strong> Autoclave cycle therefore sav<strong>in</strong>gs of<br />

power<br />

Lengthy BMR<br />

Reduced pages<br />

Manual entries reduced, thereby reduc<strong>in</strong>g errors, time.<br />

Eg <strong>–</strong> Tacrolimus Seed <strong>in</strong>oculum development checklist<br />

will be reduced from 27 pages to about 16-17 pages<br />

Media preparation<br />

separate for each<br />

stage<br />

Comb<strong>in</strong>ed media<br />

preparation for all<br />

stages<br />

Reduced<br />

documentation<br />

4


Project :CLOSED INOCULATION PROCEDURE FOR FERMENTERS<br />

Production units : SFP, IFP Gemba :QCM Lab Location : campus<br />

Status : Before <strong>Kaizen</strong><br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

Small Molecules & Biologicals- Inoculation of fermenters<br />

was done us<strong>in</strong>g <strong>in</strong>oculation needle, which was<br />

essentially an open setup which required flam<strong>in</strong>g before<br />

<strong>in</strong>oculat<strong>in</strong>g the fermenter<br />

Introduction of closed system, compris<strong>in</strong>g of male<br />

and female connectors which are connected <strong>in</strong> a<br />

sterile manner, no exposure to the surround<strong>in</strong>g<br />

environment<br />

Biological- Replaced the glass transfer flask with the<br />

Heavy duty vacuum bottle with sterile connectors<br />

s<strong>in</strong>ce <strong>in</strong>oculum volume is less<br />

Results & Benefits Summary<br />

• Inoculum which is the basis for the start up for fermentation is not exposed to the<br />

external non clean environment<br />

• Removal of flame- safety aspect<br />

• Presence of sterile filter assures sterility<br />

5


Process Map Before & After <strong>Kaizen</strong><br />

6


Project :REPLACEMENT OF COTTON PLUGS WITH SCREW CAPS<br />

Production units : NA Gemba :QCM Lab Location : campus<br />

Status : Before <strong>Kaizen</strong><br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

• Cotton plugs were used for all the flasks<br />

and bottles used<br />

Replaced the cotton with the screw cap<br />

bottles<br />

• Cost for Cotton usage annually <strong>–</strong> 55508<br />

INR<br />

Results & Benefits Summary<br />

Process Map Before & After <strong>Kaizen</strong><br />

• Cost sav<strong>in</strong>gs 1 st year <strong>–</strong> 35252 INR<br />

• Cost sav<strong>in</strong>gs 2 nd year onwards - ~ 1 lakh<br />

INR<br />

• chok<strong>in</strong>g of the return air grills of the<br />

Biosafety cab<strong>in</strong>et with cotton fibers is<br />

avoided<br />

7


Project :FILTER INTEGRITY TESTING TRANSFERRED TO PRODUCTION<br />

Production units : SFP Gemba :QCM Lab Location : campus<br />

Status : Before <strong>Kaizen</strong><br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

• QC <strong>Microbiology</strong> was test<strong>in</strong>g <strong>in</strong>tegrity of filters<br />

used <strong>in</strong> the fermentation as well as downstream<br />

process <strong>in</strong> production<br />

• Total Number of filters tested -450 <strong>in</strong> five months<br />

• Documentation <strong>in</strong>volved<br />

• One analyst used to be completely deputed for<br />

this activity<br />

Transferred the filter <strong>in</strong>tegrity test<strong>in</strong>g to production s<strong>in</strong>ce it<br />

does not <strong>in</strong>volve any microbiology science<br />

Tra<strong>in</strong><strong>in</strong>g of production personnel<br />

Results & Benefits Summary<br />

Reduced one man power requirement which resulted <strong>in</strong><br />

sav<strong>in</strong>g 1.98 Lakhs<br />

Documentation reduced<br />

8


Project :HARMONIZATION OF PCG SOP’s<br />

Production units : NA Gemba :QCM Lab Location : campus<br />

Status : Before <strong>Kaizen</strong><br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

20 SOP’s for the MCB and WCB were be<strong>in</strong>g<br />

ma<strong>in</strong>ta<strong>in</strong>ed<br />

Procedure was common but the documents<br />

were ma<strong>in</strong>ta<strong>in</strong>ed stra<strong>in</strong> wise<br />

SOP’s reduced to 3 numbers<br />

Stra<strong>in</strong> details entered <strong>in</strong> Annexure<br />

Results & Benefits Summary<br />

SOP preparation for new stra<strong>in</strong>s can be avoided<br />

Change controls reduced<br />

Ma<strong>in</strong>tenance of documents becomes simpler and<br />

easier to track<br />

9


Project :STOP IN USAGE OF FLAME IN BIOSAFETY CABINETS<br />

Production units : NA Gemba :QCM Lab Location : campus/PARK<br />

Status : Before <strong>Kaizen</strong><br />

Actions Taken Dur<strong>in</strong>g <strong>Kaizen</strong><br />

Used flame for all the aseptic activities<br />

handled <strong>in</strong> the BSC<br />

Complete removal of usage of flame <strong>in</strong>side the<br />

BSC<br />

Results & Benefits Summary<br />

Process Map Before & After <strong>Kaizen</strong><br />

• Safety compliance<br />

• No disturbance <strong>in</strong> the air flow, no<br />

turbulence caused because there will be<br />

no heat generated <strong>in</strong> the cab<strong>in</strong>et<br />

• Usage of gas cyl<strong>in</strong>ders reduced<br />

10


QC MICROBIOLOGY<br />

Thank you<br />

11

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