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Download PDF - Honda of the UK Manufacturing Ltd

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HUM SIGNIFICANT ENVIRONMENTALIMPACTS AND CONTROLS2.1 AIR AND ODOUR (Continued)Emissions from <strong>the</strong> Die Casting Process are controlled by:• Dust suppressors on all <strong>the</strong> furnaces to reduce <strong>the</strong> particulates being emitted to environment• A fume scrubbing system to minimise emissions from <strong>the</strong> sand moulding process• The use <strong>of</strong> low resin sand to minimise odour from <strong>the</strong> process• Daily visual inspections and continuous particulate monitoring• Regular odour checks at <strong>the</strong> boundaryImprovements in <strong>the</strong> die casting operation have focused on establishing <strong>the</strong> root cause <strong>of</strong> <strong>the</strong> odour complaintsreceived in 2009 and 2010. During <strong>the</strong> past year HUM has received 2 substantiated odour complaints from localresidents. A full review <strong>of</strong> <strong>the</strong> physical (equipment) and management systems was carried out and <strong>the</strong> followingconcerns and actions were determined.• Low pressure die casting dust filters were found to be damaged and split, and had contaminated <strong>the</strong> carbon filters.Dust filters were replaced and <strong>the</strong> Environmental Health Officer agreed that in <strong>the</strong> short term <strong>the</strong>re was no need toreplace <strong>the</strong> carbon filters as <strong>the</strong>y were considered ineffective• High pressure casting - manual damper used when drossing <strong>of</strong>f was found to be broken in September and <strong>the</strong>procedure for ensuring it was used was ineffective. The damper was repaired and <strong>the</strong> importance <strong>of</strong> using itreinforced with <strong>the</strong> Associates• Odour testing was updated to establish <strong>the</strong> main odour sources• Action plan developed to define and timetabled improvements for fur<strong>the</strong>r investigationsEmissions from <strong>the</strong> petrol storage process are controlled by:• Use <strong>of</strong> vapour recovery systems to minimise vapour loss during petrol transfer• Documented control systemsEmissions from <strong>the</strong> adhesives and sealers process are controlled by:• Monitoring <strong>of</strong> VOC use using a mass balance approach• Minimisation <strong>of</strong> waste materials• Controlled application methods• Documented control systemsDie Cast Example <strong>of</strong> Operator Permit Awareness Training8SE/D/G/15 - Nov 2011www.hondamanufacturing.co.uk

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