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CTA Report, Draft 1, ISP Review - US Chemical Safety and Hazard ...

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There were indications that the oven 405 burner was operating at a natural gas pressure below the<br />

manufacturer’s minimum recommended level. The <strong>CTA</strong> plant was running the burner (Eclipse) at a<br />

maximum natural gas pressure of 11 inches of water column—which is below the minimum rate of 14 for<br />

this burner model. In addition, the burner’s fixed gas butterfly valve was set at 80 to 90 percent closed to<br />

reduce gas input. Recorded flow rates indicate that the burner, with a maximum output rating of 5.5<br />

million Btu/hr (at a maximum gas pressure of 2 psi at the proportionator inlet), was being operated at only<br />

210,000 Btu/hr.<br />

All timers on the burner control panel were found at their minimum settings—contradictory to the<br />

National Fuel Code, which requires a timed purge cycle prior to burner ignition.<br />

The audible alarm mounted on the cabinet door of the burner control box (presumably for alerting<br />

operating personnel of conditions such as flameouts) was not electrically connected. Particulate matter<br />

was observed on the electronic components <strong>and</strong> the cabinet lip, where the door engages the cabinet. The<br />

amount of particulate matter indicated that the cabinet was open frequently during operation.<br />

The high gas pressure cutoff switch was set too high to control an over-gas pressure situation. This<br />

setting allowed the feeding of excessive amounts of gas into the burner if a high-pressure situation<br />

occurred, such as failure of the pressure regulator.<br />

The main gas line primary or safety valve (2-inch flanged, North American) was found with a loose<br />

actuator cover <strong>and</strong> showed debris accumulation on the upper mechanical parts (see Figure C-1). This<br />

dust, fiberglass, <strong>and</strong> oil contributed to the valve’s failure to adequately close, thereby creating an internal<br />

leak in the gas line. During down time or “burner-off” conditions, the safety valve may have been leaking<br />

natural gas through to the gas vent line at the rate of 7.5 L/min.<br />

In the “burner-on” condition with the gas control valves open <strong>and</strong> the normally open solenoid gas bleed<br />

valve closed, there was still a 0.7 L/min leak-through to the vent system from the bleed valve itself.<br />

114

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