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4"12-Z 1 - part - usaid

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Flue gas samples were also taken at the two LD. fans to compare readmg to see how much<br />

leakage there was from the air heaters. This umt had the LJunstgrom regeneratIve aIr heaters<br />

replaced wIth tubular heaters during reconstructIOn. All readIngs, includmg oxygen and excess<br />

aIr, mdicated sIgmficant aIr mleakage, probably most from ductwork and precIpItator leaks.<br />

Flue gas samples for block 5 were taken at the same extractIOn points where eXIstIng oxygen<br />

analyzers are connected. These boilers were burning 60% natural gas and 40% mazut, at<br />

95 MW load and reduced steam pressure and temperature. The oxygen levels were hIgh due<br />

to somewhat high excess aIr. The high oxygen readmgs correlated wIth the control room<br />

readings from the existIng extractive oxygen analyzers.<br />

Due to the high m-leakage rates m the furnace, the economIzer and the air heater, an on-lIne<br />

calculatIon of the combustion efficiency by Enerac portable combustIOn analyzer proved to be<br />

not feasible. The efficiency calculated IS actually overall bOIler effiCIency as shown on the<br />

pnntout. Direct measurements of 02' CO, combustible gases, NO x , and S02 appeared to be<br />

accurate. Any improvement in the effiCIency of the Burshtyn power plant must come primarily<br />

from an improvement in overall effiCIency of ItS bOIlers. On the steam SIde the Burshtyn power<br />

plant is effiCIent due to a significant thermal load. A copy of the Enerac portable combustIOn<br />

analyzer print-outs can be seen m AppendIX B.<br />

For a detailed descnptIon of the AudIt actIvitIes, see the trip report m AppendIX G.<br />

Burns and Roe engineers estimated an incremental improvement m boiler effiCIency achievable<br />

due to a reduction in excess aIr fed to the bOIlers. Usmg a portable combustion analyzer, 5-7%<br />

excess furnace oxygen was measured at full load whIle finng coal and 7-10% excess furnace<br />

oxygen at 50% load while finng natural gas. CO emIssions were negligible in both cases.<br />

Based on calculations, the excess furnace oxygen at full load while firing coal can be reduced<br />

by 1% O 2 resulting in an mcremental Improvement m bOIler effiCIency of at least 0.24%.<br />

In future the Burshtyn power plant operators should be able to manually adjust the air supply<br />

to determine what magmtude of reductIOn in excess air could be achieved within constraIns<br />

imposed by CO emiSSIOns, smoke, and flame StabIlIty Therefore, It IS recommended that<br />

permanent instruments be mstalled to measure the O 2 and CO content of the flue gas and thus<br />

assist the operators in aVOIding unsafe conditIOns while contmually minimIZIng excess aIr.<br />

4.1.4 Boiler Plant<br />

Block <strong>12</strong> is now under reconstructIOn mcludmg turbine repaIr, new HP and LP cylinders, and<br />

a new 99% effiCIent RussIan electrostatIC precIpItatOr. The next preCIpitators for block 11 and<br />

block 7 reconstruction m 1995 WIll be UkraIman manufacturer. The bOIler has all cntlcal<br />

pressure <strong>part</strong>s and membranes replaced and the steam drum checked, WIth an expected 20-25<br />

year lIfe extenSIOn. This will restore the ratmg of block <strong>12</strong> to upgraded 225 MW deSIgn and<br />

wIll be finished in Apnl 1995.<br />

5906-01/02A/BURSHTYN/5/17/95 9

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