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3.6M north10.pdf - Dean-O's Toy Box

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198 High-Power Microwave-Tube Transmitters<br />

Table 10-1. Operating parameters of 18-MW hard-tube modulator shown in Fig. 10-37<br />

Parameter<br />

Value<br />

Pulse voltage to klystron<br />

130 kV<br />

Pulse output current<br />

140A<br />

Peak-power output<br />

18MW<br />

Pulse duration<br />

3-28 us<br />

Burst mode<br />

32 pulses, max.,<br />

4-@ duration,<br />

7-28-Ks spacing<br />

Pulse-Dair mode<br />

10-LLSduration,<br />

13-”1.lspacing<br />

-,—– .,---,<br />

t-me rfme<br />

1.2@<br />

Duty ~Iabd)t’ ‘-n”<br />

0.03, max.<br />

Pulse-lup- ‘-- I-:-pie lpi O.l”/O (dl’w;ngRF) Jill<br />

Pulse-to-pulse<br />

.- ..-”:-x----- Ian >1<br />

Vdrlttllw[IS I USE.<br />

I<br />

I<br />

at the side-to-side endings of the parallel plates. Merely extending the dielectric<br />

material between the plates far beyond the ends of the plates did nothing to<br />

prevent corona discharges, which rather quickly punctured the dielectric material.<br />

Reducing fall-time di/di did not completely cure EOPSTA, however. Other<br />

effects were also at work. The temperature of the control grids, which were<br />

subject to power dissipation throughout each output pulse, reached transient<br />

maxima at the end of each pulse. This made them more likely to emit secondary<br />

electrons and less likely to establish zero-current conditions within the tubes<br />

when their voltages were brought to the negative voltage that should have been<br />

adequate for current cutoff. Experiments were performed where grid drive voltage<br />

and conduction-anode-voltage dmp were interchanged between so-called<br />

hard-drive and soft-drive conditions. Unfortunately reducing intrapulse grid<br />

drive voltage and increasing anode supply voltage to compensate for it produced<br />

a statistically insignificant difference in spark-down rate. The only thing that<br />

really worked was operating the circuit at lower voltage and lower power.<br />

The suggestion that the problem may have been caused by the tubes’ “hot<br />

grids” gave rise to an experiment that replaced the eight triodes with eight tetrodes<br />

of roughly comparable capability (type 4CW250,000). It turned out, however,<br />

that “hot screens” produced much the same effect as “hot grids.” VMually<br />

no improvement was noted.<br />

This modulator experiment did, however, lead to a successful 60-MW pulse<br />

modulator, which used six parallel-connected WL-8461 triodes that pulsed a 20-<br />

MW-peak-power UHF klystron in the transmitter of an instrumentation radar.<br />

The system worked well for many years.<br />

10.7.2 An 18-MW hard-tube modulator using the L-5097 beam-switch tube<br />

Waveform versatility and both pulse-top and pulse-to-pulse precision are the<br />

salient features of the hard-tube modulator shown in Fig. 10-37. A broad-band<br />

high-performance S-band klystron, the VKS-8250, is directly cathode pulsed by a<br />

group of three paralleled L-5097 BSTS. The pulsed cathode voltage, which is 130<br />

kV, is driven by a power supply with maximum dc output of 160 kV. The total

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