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Loss Prevention<br />

Case Studies


Introduction<br />

Contents<br />

Case studies are summaries <strong>of</strong> claims that have<br />

been notified to <strong>the</strong> Club. We produce <strong>the</strong>se to<br />

raise awareness <strong>of</strong> <strong>the</strong> causation <strong>of</strong> claims and <strong>the</strong>ir<br />

outcome so that o<strong>the</strong>r Members can benefit from <strong>the</strong><br />

misfortune <strong>of</strong> o<strong>the</strong>rs and pass this knowledge on to all<br />

relevant sectors <strong>of</strong> <strong>the</strong>ir organisations.<br />

The case studies within this publication are arranged by vessel type and <strong>the</strong>n<br />

categorised by area <strong>of</strong> claim e.g. Navigation, Personal Injury/Illness and Operations.<br />

We hope that Members will find <strong>the</strong> following compilation <strong>of</strong> case studies useful.<br />

David Heaselden<br />

David Heaselden<br />

Loss Prevention Manager


Section 1<br />

Dry Cargo Vessels<br />

3


Dry Cargo:<br />

Bulk<br />

Personal Injury/Illness<br />

Only Use Equipment for it’s Designated Purpose<br />

The Incident:<br />

In this case <strong>the</strong> barge concerned was secured<br />

alongside, working cargo. A coastal vessel <strong>the</strong>n<br />

entered <strong>the</strong> port and without obtaining permission<br />

from <strong>the</strong> terminal moored alongside (double<br />

banked) to <strong>the</strong> barge. After berthing <strong>the</strong> crew <strong>of</strong><br />

<strong>the</strong> coastal vessel reportedly went ashore by passing<br />

through <strong>the</strong> accommodation <strong>of</strong> <strong>the</strong> barge. It was<br />

at this time (1035 hrs) that <strong>the</strong> crew <strong>of</strong> <strong>the</strong> barge<br />

noticed that a breast line at <strong>the</strong> after end <strong>of</strong> <strong>the</strong><br />

barge had parted and <strong>the</strong>refore proceeded aft to<br />

replace it. Upon arriving at <strong>the</strong> stern <strong>the</strong>y found one<br />

<strong>of</strong> <strong>the</strong> crew members from <strong>the</strong> coastal vessel lying<br />

injured on <strong>the</strong> port side <strong>of</strong> <strong>the</strong> main deck adjacent<br />

to <strong>the</strong> accommodation. It appeared he had been<br />

struck by <strong>the</strong> rope as it parted. The barge’s crew<br />

immediately reported <strong>the</strong> matter to <strong>the</strong>ir shore<br />

<strong>of</strong>fice who in turn informed <strong>the</strong> Hong Kong Marine<br />

Department and o<strong>the</strong>r <strong>of</strong>ficials. Shortly afterwards<br />

police <strong>of</strong>ficers attended <strong>the</strong> barge along with an<br />

ambulance and <strong>the</strong> fire department. Personnel from<br />

<strong>the</strong> ambulance were unable to board <strong>the</strong> barge<br />

on account <strong>of</strong> <strong>the</strong> prevailing heavy sea conditions.<br />

Therefore oxygen equipment was passed to <strong>the</strong><br />

barge’s crew who were duly instructed on its use.<br />

The firemen <strong>the</strong>n boarded <strong>the</strong> barge and hoisted<br />

<strong>the</strong> injured person ashore where he was taken to<br />

hospital. Unfortunately <strong>the</strong> injured person died later<br />

in hospital.<br />

Observations:<br />

The nylon rope (8 inches in circumference) had<br />

been used as a mooring line and was observed in<br />

poor condition. The eye splice had been extensively<br />

cut with only a few strands remaining which were<br />

rust stained. The vessel’s crew noted that <strong>the</strong> rope<br />

had been used for towing prior to being utilised as a<br />

mooring line. It is imperative that ropes are utilised<br />

for <strong>the</strong>ir intended use. Once <strong>the</strong>y have been used<br />

to perform a function <strong>the</strong>y should not be reused<br />

for o<strong>the</strong>r purposes. Ropes should be subject to<br />

regular examination including telltale signs <strong>of</strong> wear<br />

(powdering in <strong>the</strong> case <strong>of</strong> nylon ropes).<br />

Root Cause:<br />

Incorrect use <strong>of</strong> vessel equipment.<br />

Financial Cost:<br />

US$43,362.<br />

Issue Date: 05/02/08<br />

Case No. 50055<br />

4 5


Cargo<br />

Loading During Rain Causes Cargo Claim<br />

The Incident:<br />

A 1,200 ton gearless bulk carrier was discharging her cargo <strong>of</strong> rape seed meal. Shortly<br />

after discharge commenced cargo operations were suspended during a heavy rain<br />

shower. The crew had some difficulties in reopening <strong>the</strong> hatch covers and as a result<br />

discharge was delayed.<br />

Following this incident stevedores requested that discharge continue during periods <strong>of</strong><br />

rain. The Master asked for written authorisation and this was reportedly promised by <strong>the</strong><br />

stevedores. On <strong>the</strong> strength <strong>of</strong> <strong>the</strong> promise <strong>of</strong> a letter <strong>of</strong> authorisation to work in <strong>the</strong><br />

rain <strong>the</strong> Master allowed discharge to continue in <strong>the</strong> rain and made no attempt to cover<br />

<strong>the</strong> hold during lunch breaks.<br />

When a cargo claim for wet damage was presented by <strong>the</strong> consignee <strong>the</strong> stevedores<br />

refuted any knowledge <strong>of</strong> a letter <strong>of</strong> authorisation to permit working during periods <strong>of</strong> rain.<br />

Observations:<br />

The only people with <strong>the</strong> power to authorise <strong>the</strong><br />

discharge <strong>of</strong> water-sensitive cargo during periods <strong>of</strong><br />

rain are <strong>the</strong> shippers or consignees. Stevedores do<br />

not normally have <strong>the</strong> authority to do so.<br />

In many parts <strong>of</strong> <strong>the</strong> world stevedores are paid by<br />

ton <strong>of</strong> cargo loaded or discharged with <strong>the</strong> result<br />

that interruptions to <strong>the</strong> cargo operations because<br />

<strong>of</strong> rain represent a loss <strong>of</strong> income. When requested<br />

to continue loading or discharging water-sensitive<br />

cargoes in <strong>the</strong> rain Masters should ensure that <strong>the</strong>y<br />

have received written authority to do so from <strong>the</strong><br />

shipper or consignee or someone acting with <strong>the</strong>ir<br />

authority. In cases where <strong>the</strong> authorisation is given<br />

by persons o<strong>the</strong>r than <strong>the</strong> shipper or consignee <strong>the</strong><br />

Master should ensure that <strong>the</strong> person authorising<br />

<strong>the</strong> operation has <strong>the</strong> power to do so o<strong>the</strong>rwise<br />

responsibility for damage to <strong>the</strong> cargo may remain<br />

with <strong>the</strong> ship.<br />

Root Cause:<br />

Non compliance with good cargo<br />

operational practices.<br />

Financial Cost:<br />

17.5 tons <strong>of</strong> cargo were damaged with a market<br />

value <strong>of</strong> over US$3,000.<br />

Issue Date: 01/02/02<br />

Case No. 23451<br />

6 7


Navigation<br />

Grounding as a Result <strong>of</strong> Poor Navigational Practices<br />

The Incident:<br />

This case concerns <strong>the</strong> grounding<br />

<strong>of</strong> a vessel in mid-afternoon<br />

during a coastal passage. At <strong>the</strong><br />

time <strong>of</strong> <strong>the</strong> grounding visibility<br />

was good with a light easterly<br />

breeze, smooth sea and no swell.<br />

The Master was on <strong>the</strong> bridge<br />

chatting to <strong>the</strong> <strong>of</strong>ficer <strong>of</strong> <strong>the</strong><br />

watch and <strong>the</strong>re was also a deck<br />

cadet on <strong>the</strong> bridge.<br />

The vessel was on a regular<br />

run between two ports in an<br />

area <strong>of</strong> relatively shallow water,<br />

liberally scattered with coral<br />

reefs. The Admiralty Pilot advises<br />

mariners that charts <strong>of</strong> <strong>the</strong> area<br />

were based on old surveys, (few<br />

systematic surveys have been<br />

carried out), and that much <strong>of</strong><br />

<strong>the</strong> information is derived from<br />

lines <strong>of</strong> soundings taken by vessels<br />

on passage. The working chart<br />

carried <strong>the</strong> following caution:<br />

Unsurveyed Areas<br />

No hydrographic survey has been conducted and<br />

accordingly mariners attempting to enter <strong>the</strong>se<br />

areas should proceed with extreme caution as<br />

unidentified shoals, reefs and o<strong>the</strong>r navigational<br />

hazards may exist.<br />

The chart shows a recommended track for<br />

transiting <strong>the</strong> area which passed to <strong>the</strong> south <strong>of</strong><br />

an <strong>of</strong>fshore reef. The vessel’s course line did not<br />

follow <strong>the</strong> recommended track. Instead <strong>the</strong> Master<br />

inked in a course which cut a corner, passing to <strong>the</strong><br />

north <strong>of</strong> <strong>the</strong> reef through an area clearly marked as<br />

unsurveyed. The Master had apparently regularly<br />

followed that route when a junior <strong>of</strong>fice on a smaller<br />

vessel. His departure from <strong>the</strong> recommended track<br />

was increased by <strong>the</strong> second mate who, after fixing<br />

<strong>the</strong> vessel’s position at 16.00 hrs, decided to alter<br />

course to cut <strong>the</strong> corner even more, taking <strong>the</strong><br />

vessel fur<strong>the</strong>r into unsurveyed waters.<br />

Observations:<br />

The grounding was <strong>the</strong> result <strong>of</strong> sub-standard<br />

navigational practices. The Master and Owners<br />

had allowed a culture <strong>of</strong> corner-cutting to<br />

develop. Subsequent investigation revealed that<br />

recommended tracks were <strong>of</strong>ten ignored when a<br />

straight line between two points would save a little<br />

distance. In many cases this took <strong>the</strong> vessel into<br />

close proximity to shallow water whilst saving only<br />

minimal time and distance.<br />

Numerous o<strong>the</strong>r areas <strong>of</strong> sub-standard navigational<br />

practices were revealed including failure to correct<br />

charts in accordance with <strong>the</strong> latest Notices to<br />

Mariners. This working chart had not been corrected<br />

for over two years and <strong>the</strong> Admiralty Pilot for <strong>the</strong> area<br />

was missing <strong>the</strong> latest supplement which contained<br />

information relevant to <strong>the</strong> area <strong>of</strong> grounding.<br />

In addition it appears that almost total reliance was<br />

placed on GPS despite being in close proximity to<br />

a steep coastline with numerous features, giving a<br />

good clear radar echo and ample opportunity to<br />

take visual bearings. The working chart is endorsed<br />

with <strong>the</strong> caution:<br />

SATELLITE-DERIVED POSITIONS<br />

Positions obtained from satellite navigation<br />

systems are normally referred to <strong>the</strong> WGS Datum;<br />

adjustments for plotting such positions cannot be<br />

determined for this chart. Mariners must determine<br />

<strong>the</strong> position <strong>of</strong> <strong>the</strong>ir vessel in relation to <strong>the</strong> charted<br />

positions <strong>of</strong> dangers and navigational features by<br />

visual or radar means.<br />

Fortunately <strong>the</strong> vessel suffered no major damage in<br />

<strong>the</strong> grounding and was refloated within 12 hours.<br />

The Master was relieved <strong>of</strong> his command.<br />

ROOT CAUSE:<br />

Inadequate navigational practices.<br />

FINANCIAL COST:<br />

Issue Date: 01/02/02<br />

Case No.28862<br />

8 9


Navigation<br />

Intermittent Faults can be more Serious than a Permanent One<br />

The Incident:<br />

The Club has recently dealt with a number <strong>of</strong> claims<br />

that have been caused by known intermittent faults<br />

occurring at <strong>the</strong> wrong time.<br />

This particular incident involved a 500 gt Dry Cargo<br />

vessel fitted with a main engine gearbox.<br />

After loading a cargo <strong>of</strong> stone <strong>the</strong> vessel proceeded<br />

on her laden passage without problem. The discharge<br />

port was located inland from <strong>the</strong> coast requiring<br />

passage through locks and a canal. The vessel entered<br />

<strong>the</strong> lock without event, but upon departing, <strong>the</strong><br />

Master experienced difficulties engaging <strong>the</strong> gearbox<br />

from ahead to astern. After several attempts <strong>the</strong><br />

problem “disappeared” and <strong>the</strong> vessel left <strong>the</strong> lock.<br />

Shortly afterwards <strong>the</strong> decision was taken to<br />

moor <strong>the</strong> vessel alongside a layby berth and whilst<br />

manoeuvring alongside <strong>the</strong> gearbox again failed to<br />

engage astern. As a result <strong>the</strong> vessel made heavy<br />

contact with <strong>the</strong> quay, she came <strong>of</strong>f and after several<br />

fur<strong>the</strong>r attempts <strong>the</strong> gearbox successfully engaged<br />

and <strong>the</strong> vessel was safely ber<strong>the</strong>d.<br />

The damage to <strong>the</strong> vessel was severe enough to<br />

warrant <strong>the</strong> attendance <strong>of</strong> a Class surveyor. As can<br />

be seen from <strong>the</strong> photograph above, <strong>the</strong> quay was<br />

also badly damaged as was a section <strong>of</strong> public road<br />

that ran along it.<br />

Observations:<br />

The Master and Chief Engineer had both recently<br />

joined <strong>the</strong> vessel and were not aware <strong>of</strong> any<br />

previous problems with <strong>the</strong> gearbox. However, <strong>the</strong><br />

vessel’s Superintendent upon hearing <strong>of</strong> <strong>the</strong> incident<br />

advised <strong>the</strong> Master that it was a known problem and<br />

had been experienced on previous occasions.<br />

It is very disappointing to note that <strong>the</strong> previous<br />

Master and Chief Engineer did not consider<br />

problems engaging astern movement <strong>of</strong> <strong>the</strong> vessel<br />

serious enough to warrant advising <strong>the</strong>ir reliefs, or<br />

that <strong>the</strong> ship’s managers via <strong>the</strong> superintendent did<br />

not take any positive action in trying to solve <strong>the</strong><br />

problem. At least <strong>the</strong> relief Master should have been<br />

advised to take suitable precautions until such time<br />

as <strong>the</strong> fault had been rectified.<br />

Root Cause:<br />

Onboard maintenance programme failure.<br />

Financial Cost:<br />

The cost to <strong>the</strong> Member is in excess <strong>of</strong> US$45,000.<br />

Issue Date: 30/07/03<br />

Case No. 39809<br />

The Member was fortunate that <strong>the</strong> incident took<br />

place after entry into <strong>the</strong> lock; if <strong>the</strong> vessel had hit<br />

<strong>the</strong> lock gates <strong>the</strong> incident could have had very<br />

serious repercussions.<br />

Intermittent faults should be considered serious on<br />

two counts. Firstly <strong>the</strong>y are notoriously difficult to<br />

detect and rectify by <strong>the</strong>ir very nature and secondly,<br />

because <strong>the</strong>y are intermittent, complacency arises<br />

and quite <strong>of</strong>ten contingency plans do not take into<br />

account any recurrence, when in fact <strong>the</strong>y should.<br />

10 11


Operations<br />

Crate Dropped During Lowering<br />

The Incident:<br />

Please note that this Case Study<br />

has been provided by The<br />

Nautical Institute’s International<br />

and Confidential Marine Accident<br />

Reporting Scheme (MARS)<br />

- Report No. 200824<br />

On a ship at anchor, a crate<br />

containing machinery spares,<br />

reeved with two webbing<br />

slings, was being lowered into<br />

<strong>the</strong> engine room through <strong>the</strong><br />

engine room hatch using <strong>the</strong><br />

ship’s stores crane. During <strong>the</strong><br />

lowering process, a corner <strong>of</strong><br />

<strong>the</strong> base <strong>of</strong> <strong>the</strong> crate caught on<br />

a section <strong>of</strong> ducting immediately<br />

below <strong>the</strong> hatch coaming,<br />

became unbalanced and tipped<br />

through <strong>the</strong> slings, falling to<br />

<strong>the</strong> deck below. The impact<br />

destroyed <strong>the</strong> crate; however,<br />

<strong>the</strong>re were no injuries or damage<br />

o<strong>the</strong>r than that <strong>the</strong> spares were<br />

rendered unusable.<br />

Root cause/contributory factors<br />

1. Failure to sling <strong>the</strong> crate properly; webbing slings<br />

not tight around <strong>the</strong> top <strong>of</strong> <strong>the</strong> crate;<br />

2. Ship rolling slightly at anchorage, causing <strong>the</strong> crate<br />

to swing during passage through <strong>the</strong> hatch;<br />

3. Failure to conduct/review formal risk assessment<br />

prior to <strong>the</strong> lifting operation;<br />

4. It is thought that <strong>the</strong> spare part was inadequately<br />

secured inside <strong>the</strong> crate and as <strong>the</strong> crate tilted, <strong>the</strong><br />

internal shift <strong>of</strong> weight assisted <strong>the</strong> ‘tipping’ motion;<br />

5. The crate’s height was greater than <strong>the</strong> o<strong>the</strong>r two<br />

dimensions, which made it more prone to tipping;<br />

6. The crate had no fitting to prevent <strong>the</strong> slings from<br />

slipping <strong>of</strong>f in case <strong>the</strong> load became unbalanced;<br />

7. ‘Routine task’ complacency and inadequate<br />

understanding <strong>of</strong> risk assessment among<br />

<strong>the</strong> ratings.<br />

Corrective actions<br />

1. The company issued notices to Masters and<br />

safety bulletins on risk assessment, work planning<br />

and safe lifting techniques.<br />

2. Crane operator familiarisation training was<br />

conducted on board and will be supplemented<br />

by fur<strong>the</strong>r computer based or practical training in<br />

crane operations and rigging/slinging.<br />

3. Permit to work system presently applying only<br />

to lifts within hazardous areas to be extended to<br />

include all lifting tasks.<br />

4. Investigate and solicit vessel proposals for a steel<br />

cage/box to be used for lifting operations into <strong>the</strong><br />

engine room.<br />

Lessons learnt<br />

1. Expensive and relatively fragile components<br />

should be given a higher level <strong>of</strong> planning and<br />

supervision.<br />

2. Although a task review was conducted during<br />

<strong>the</strong> initial work planning, it was not documented<br />

and should have been followed up with a risk<br />

assessment and a tool box meeting.<br />

3. There was a failure to assess <strong>the</strong> risks adequately,<br />

specifically vessel motion and <strong>the</strong> possibility <strong>of</strong> <strong>the</strong><br />

crate contents shifting.<br />

Issue Date: 15/04/08<br />

Case No. 12388<br />

12 13


Miscellaneous<br />

Smoking is Not Good for Your Health<br />

The Incident:<br />

This case involves a vessel on which 1.5 million<br />

cigarettes (150 boxes) were discovered in <strong>the</strong><br />

fore peak hidden under a tarpaulin during a search<br />

by <strong>the</strong> Customs and Federal Police. The search<br />

was thought to be <strong>the</strong> result <strong>of</strong> a ‘tip <strong>of</strong>f’ by <strong>the</strong><br />

European Bureau for Fraud.<br />

During subsequent interviews <strong>the</strong> Master and<br />

Chief Mate denied all knowledge <strong>of</strong> <strong>the</strong> smuggling<br />

but a crew member confessed, admitting full and<br />

sole responsibility. He stated that he purchased <strong>the</strong><br />

cigarettes with money obtained from <strong>the</strong> sale <strong>of</strong><br />

his apartment, transported <strong>the</strong> cigarettes by van<br />

to <strong>the</strong> vessel and brought <strong>the</strong> cigarettes on board<br />

<strong>the</strong> vessel without assistance. He alleged that on<br />

<strong>the</strong> vessel’s arrival in <strong>the</strong> discharge port he was to<br />

liaise with a Russian man only known to him by <strong>the</strong><br />

name <strong>of</strong> ‘Sergei’.<br />

The body was recovered two months later and<br />

despite <strong>the</strong> fact his left ankle was tightly bound<br />

with rope <strong>the</strong> inquest concluded death by<br />

drowning with no obvious signs <strong>of</strong> violence.<br />

Observations:<br />

Criminal charges were initially brought against <strong>the</strong><br />

seaman, <strong>the</strong> Master and our Members. Due to <strong>the</strong><br />

seaman’s death <strong>the</strong> criminal charges against him have<br />

been dropped. No civil charges have been made as<br />

<strong>the</strong> cigarettes have been seized.<br />

Root Cause:<br />

Illegal smuggling.<br />

Financial Cost:<br />

A nominal fine was incurred.<br />

Issue Date: 17/03/08<br />

Case No: 48633<br />

A week later, while <strong>the</strong> authorities were still<br />

investigating <strong>the</strong> case and prior to obtaining an order<br />

to seize <strong>the</strong> vessel or formally make charges, <strong>the</strong><br />

vessel was allowed to depart. During <strong>the</strong> following<br />

voyage <strong>the</strong> seaman concerned went missing. A full<br />

vessel search was immediately made which lead to<br />

<strong>the</strong> discovery <strong>of</strong> a suicide note in his cabin. It stated<br />

again that he was fully and solely responsible.<br />

Article 265 Section 3 <strong>of</strong> <strong>the</strong> Belgian Customs Code<br />

provides that in cases like this Members could be<br />

held vicariously liable for fines and costs which are<br />

imposed on conviction <strong>of</strong> <strong>the</strong> Master. Accordingly, it<br />

may also be possible for Members to be found liable<br />

to pay not only a fine imposed directly on <strong>the</strong>m but<br />

also any fine imposed on <strong>the</strong> Master.<br />

14 15


Dry Cargo:<br />

General<br />

Personal Injury/Illness<br />

Crane Collapse Results in Death <strong>of</strong> Bystander<br />

The Incident:<br />

This incident involves a gearless dry cargo vessel<br />

which had been equipped with a large mobile crane<br />

to enable it to operate at berths without cargo<br />

handling equipment. The crane had been designed<br />

for industrial operations ashore. Its tracks had been<br />

removed and it was temporarily bolted to <strong>the</strong> deck<br />

<strong>of</strong> <strong>the</strong> vessel. The crane was fitted with a jib 120<br />

foot long and had a maximum capacity <strong>of</strong> 136 tons<br />

at an 18 foot radius <strong>of</strong> operation. As a heavy lift was<br />

being discharged <strong>the</strong> vessel listed slightly and <strong>the</strong><br />

crane jib collapsed. The jib fell on a vehicle killing <strong>the</strong><br />

occupant. The ship itself was undamaged but <strong>the</strong><br />

cargo was a total loss.<br />

Observations:<br />

The design <strong>of</strong> <strong>the</strong> crawler crane was typical <strong>of</strong><br />

its type, having a long narrow latticework boom.<br />

These cranes are designed for use on a level steady<br />

surface where <strong>the</strong> boom acts merely as a strut in<br />

compression and is not subjected to sideways or<br />

twisting forces. In this case as <strong>the</strong> load was slowly<br />

swung over <strong>the</strong> vessel’s side, <strong>the</strong> vessel began to<br />

list causing <strong>the</strong> load to swing out <strong>of</strong> <strong>the</strong> plane <strong>of</strong> <strong>the</strong><br />

jib. The list also increased <strong>the</strong> effective radius <strong>of</strong><br />

operation, increasing <strong>the</strong> stress. The combination<br />

<strong>of</strong> increased load and side force caused <strong>the</strong> jib to<br />

fail at its base where it was attached to <strong>the</strong> body <strong>of</strong><br />

<strong>the</strong> crane.<br />

Extreme care must be taken to avoid excessive<br />

side loads on cranes not designed for marine use.<br />

Detailed guidance from <strong>the</strong> crane’s manufacturers<br />

and national authorities should be sought. As a<br />

general rule however <strong>the</strong> vessel should not be<br />

allowed to list more than 5° during <strong>the</strong> discharge<br />

operation and <strong>the</strong> load should never exceed 50% <strong>of</strong><br />

<strong>the</strong> crane’s safe working load for operation on land.<br />

The vessel’s stability was adequate but in order<br />

to counteract <strong>the</strong> anticipated list as <strong>the</strong> load was<br />

swung towards <strong>the</strong> wharf, orders were given to<br />

deballast <strong>the</strong> double bottom tanks on that side.<br />

The deballasting had not been completed at <strong>the</strong><br />

time <strong>the</strong> load was moved horizontally and <strong>the</strong><br />

free surface effect <strong>of</strong> <strong>the</strong> liquid in <strong>the</strong> partially<br />

filled tanks served to increase <strong>the</strong> vessel’s list. The<br />

number <strong>of</strong> slack tanks must be kept to a minimum<br />

when heavy loads are handled.<br />

Financial Cost:<br />

The cargo claim was settled for US$500 in line with<br />

<strong>the</strong> package limitation contained in <strong>the</strong> bill <strong>of</strong> lading.<br />

The claim <strong>of</strong> <strong>the</strong> vehicle driver was covered by his<br />

motor insurers who ra<strong>the</strong>r surprisingly failed to<br />

subrogate <strong>the</strong>ir claim against our Member before it<br />

became time-barred. The owners faced a number<br />

<strong>of</strong> prosecutions brought for alleged breaches <strong>of</strong> <strong>the</strong><br />

Canada Shipping Act and <strong>the</strong> Tackle Regulation,<br />

most <strong>of</strong> which were quashed at trial. Despite a<br />

very favourable resolution <strong>of</strong> <strong>the</strong> claims, <strong>the</strong> costs<br />

incurred in investigating and defending <strong>the</strong> Member<br />

reached US$33,000.<br />

Root Cause:<br />

Incorrect operation <strong>of</strong> equipment.<br />

Issue Date: 01/02/02 Case No. 16415<br />

16 17


Cargo<br />

Flammable Gases Cause Explosion<br />

The Incident:<br />

This incident involved a large explosion on board a<br />

general cargo vessel when flammable gases given<br />

<strong>of</strong>f by <strong>the</strong> cargo were ignited by an electrical spark.<br />

The explosion killed two crew members, injured<br />

several more and caused severe damage to <strong>the</strong> ship.<br />

The vessel’s forward hatch covers were blown <strong>of</strong>f,<br />

landing on and severely damaging two tugs moored<br />

nearby. Extensive damage was caused to surrounding<br />

buildings and a nearby papermill was shut down for a<br />

week following <strong>the</strong> explosion.<br />

Observations:<br />

The vessel was loading a cargo <strong>of</strong> spent pot liner, <strong>the</strong><br />

carbon-based lining <strong>of</strong> an aluminium smelter which<br />

absorbs impurities from <strong>the</strong> metal. It eventually<br />

becomes saturated and has to be replaced. The<br />

impurities in <strong>the</strong> spent pot liner react slowly with<br />

water producing inflammable gases.<br />

Our investigations revealed that <strong>the</strong> cargo loaded<br />

into number 1 hatch had come from two different<br />

storage areas. Wet reacted cargo from an open<br />

stockpile had been mixed with dry unreacted<br />

cargo which had been stored in a closed shed.<br />

Moisture from <strong>the</strong> wea<strong>the</strong>red cargo migrated to<br />

<strong>the</strong> dry, causing it to react with <strong>the</strong> result that an<br />

accumulation <strong>of</strong> inflammable gases built up in <strong>the</strong><br />

hold and fan rooms overnight. These gases were<br />

ignited by an electrical contactor operating <strong>the</strong><br />

hydraulic system for <strong>the</strong> hatch covers.<br />

The shippers, although aware <strong>of</strong> <strong>the</strong> problem<br />

<strong>of</strong> inflammable gases, did not advise owners or<br />

charterers <strong>of</strong> <strong>the</strong> danger, nor did <strong>the</strong>y provide<br />

<strong>the</strong> vessel with a <strong>copy</strong> <strong>of</strong> <strong>the</strong>ir material safety<br />

data sheet. Information on spent pot lining was<br />

not available from <strong>the</strong> IMDG Code, <strong>the</strong> IMO<br />

Code <strong>of</strong> Safe Practice for Solid Bulk Cargoes, <strong>the</strong><br />

Dangerous Bulk Materials Regulations or any o<strong>the</strong>r<br />

<strong>of</strong>ficial publication.<br />

The explosion could have been avoided if all <strong>the</strong> pot lining had been wea<strong>the</strong>red prior to<br />

shipment or proper steps had been taken by <strong>the</strong> shipper to ensure that wet cargo was<br />

kept separate from dry unreacted cargo. The shippers should have provided <strong>the</strong> vessel<br />

with safety data sheets. Appropriate measures could <strong>the</strong>n have been taken to ensure<br />

that <strong>the</strong> cargo was kept adequately ventilated and <strong>the</strong> accumulation <strong>of</strong> explosive gas<br />

could have been avoided.<br />

Root Cause:<br />

Unsafe loading practice.<br />

Financial Cost:<br />

The claims arising out <strong>of</strong> <strong>the</strong> explosion totalled<br />

over US$30 million. In <strong>the</strong> end <strong>the</strong>y were settled<br />

for just under US$11 million with <strong>the</strong> shippers <strong>of</strong><br />

<strong>the</strong> cargo bearing by far <strong>the</strong> greatest proportion.<br />

Never<strong>the</strong>less <strong>the</strong> costs <strong>of</strong> investigation, defending<br />

<strong>the</strong> various legal actions and with a very modest<br />

contribution towards <strong>the</strong> settlements brought<br />

<strong>the</strong> cost to our Members <strong>the</strong> charterers to<br />

US$1.3 million.<br />

Issue Date: 01/01/02<br />

Case No. 15646<br />

18 19


Miscellaneous<br />

Corrosion – The Hidden Enemy<br />

The Incident:<br />

Please note that this case study has been provided<br />

by <strong>the</strong> MAIB Safety Digest 2/2007, Case 6.<br />

After completing <strong>the</strong> weekly planned maintenance<br />

routine on a rescue boat and its crane, it was usual<br />

for <strong>the</strong> crew to lower <strong>the</strong> boat to <strong>the</strong> water for<br />

training purposes while alongside. The boat was<br />

lowered and manoeuvred in <strong>the</strong> water for a short<br />

time and <strong>the</strong>n brought back to be hoisted on board.<br />

As <strong>the</strong> boat was being hoisted, <strong>the</strong> wire rope parted<br />

and <strong>the</strong> boat fell into <strong>the</strong> sea.<br />

Fortunately, <strong>the</strong> company had al<strong>read</strong>y identified this<br />

as a high risk operation and had stopped <strong>the</strong> practice<br />

<strong>of</strong> having <strong>the</strong> crew in <strong>the</strong> boat while hoisting or<br />

lowering during training exercises. There were no<br />

injuries, and <strong>the</strong> boat was not damaged.<br />

On investigation, it was found that a new wire rope<br />

had been fitted 14 months previously, and it had<br />

passed a thorough examination about five months<br />

before <strong>the</strong> incident. It was also inspected/greased<br />

on a weekly basis as part <strong>of</strong> <strong>the</strong> ship’s planned<br />

maintenance programme. Despite <strong>the</strong> checks, <strong>the</strong><br />

incipient corrosion had not been discovered and<br />

<strong>the</strong> wire eventually failed at <strong>the</strong> top <strong>of</strong> <strong>the</strong> steel ball<br />

counter weight.<br />

The accelerated corrosion was partly due to <strong>the</strong><br />

harsh environment in which <strong>the</strong> rescue boat and<br />

its crane were located, at <strong>the</strong> aft end <strong>of</strong> <strong>the</strong> vessel.<br />

The ball weight had a crevice at <strong>the</strong> top where <strong>the</strong><br />

wire passed through, and this formed an ideal trap<br />

for sea water, salt and sulphur deposits from nearby<br />

exhaust outlets to accumulate and obstruct regular<br />

inspection.<br />

The investigation discovered that unsuitable grease<br />

had been applied, and this had not been effective in<br />

lubricating <strong>the</strong> wire core and served to obscure <strong>the</strong><br />

underlying corrosion (see photograph <strong>of</strong> wire and<br />

crane ball indicating <strong>the</strong> point <strong>of</strong> failure).<br />

The failed segments <strong>of</strong> <strong>the</strong> wire rope were sent<br />

to a laboratory for testing, and <strong>the</strong> subsequent<br />

report confirmed that <strong>the</strong> wire rope had failed<br />

through ductile tensile fractures <strong>of</strong> wires wasted<br />

by corrosion. The laboratory was also able to<br />

confirm that a contributory cause <strong>of</strong> <strong>the</strong> failure was<br />

inadequate maintenance greasing over a significant<br />

period <strong>of</strong> time.<br />

The body was recovered two months later and<br />

despite <strong>the</strong> fact his left ankle was tightly bound<br />

with rope <strong>the</strong> inquest concluded death by<br />

drowning with no obvious signs <strong>of</strong> violence.<br />

Conclusion:<br />

1. The inspection <strong>of</strong> all wire ropes should be<br />

thorough, and should include <strong>the</strong> removal <strong>of</strong> old<br />

grease to assess <strong>the</strong> condition <strong>of</strong> <strong>the</strong> wire rope<br />

before re-coating with fresh wire lubricant.<br />

2. Senior staff should regularly monitor planned<br />

maintenance procedures which are carried out<br />

by crew.<br />

3. Consideration should be given to <strong>the</strong> use <strong>of</strong> a<br />

thinner self penetrating lubricant on seldom used<br />

wire ropes, especially where <strong>the</strong>y are used or<br />

stored in a harsh corrosive environment.<br />

Issue Date: 09/12/07<br />

Case No: 12377<br />

20 21


Dry Cargo:<br />

Containers<br />

Cargo<br />

Capsize During Loading<br />

The Incident:<br />

As <strong>the</strong> last few containers were being loaded on <strong>the</strong><br />

deck <strong>of</strong> a 3,000 gross ton inter-island cargo vessel<br />

she capsized and sank alongside <strong>the</strong> dock, damaging<br />

<strong>the</strong> dock as she went down. The Port Authority<br />

issued a wreck removal order. The Club invited<br />

tenders for <strong>the</strong> removal operation and a contract<br />

was finally agreed with a Singapore-based salvage<br />

company. The wreck removal was effected using a<br />

large sheerlegs which had to be towed over 2,000<br />

miles to <strong>the</strong> site <strong>of</strong> <strong>the</strong> accident. The wreck was cut<br />

up into manageable sections and dumped at sea.<br />

The berth was finally cleared some five months<br />

after <strong>the</strong> ship went down. The majority <strong>of</strong> <strong>the</strong> cargo<br />

was a total loss.<br />

Observations:<br />

Our investigations revealed that <strong>the</strong> cause <strong>of</strong> <strong>the</strong> loss was an error in<br />

calculating <strong>the</strong> vessel’s stability. The Chief Officer had failed to make<br />

proper allowance for <strong>the</strong> height <strong>of</strong> a stow <strong>of</strong> bagged cement in <strong>the</strong><br />

lower hold when calculating <strong>the</strong> vessel’s vertical centre <strong>of</strong> gravity. As<br />

a result his calculations produced an over-optimistic prediction <strong>of</strong> <strong>the</strong><br />

vessel’s stability on completion <strong>of</strong> loading. There was no established<br />

procedure on this ship for an independent check <strong>of</strong> <strong>the</strong> Chief Officer’s<br />

calculation. Had <strong>the</strong>re been one it is highly likely that <strong>the</strong> mistake<br />

would have been noticed and <strong>the</strong> loss <strong>of</strong> <strong>the</strong> vessel avoided.<br />

Root Cause:<br />

Error in stability calculation.<br />

Financial Cost:<br />

Cargo claims totalling over US$3 million were submitted to <strong>the</strong><br />

owners. By using package limitation and defences available to <strong>the</strong><br />

owners under <strong>the</strong> Hague Rules, those claims were finally settled for<br />

less than US$500,000.<br />

The costs <strong>of</strong> removing <strong>the</strong> wreck <strong>of</strong> <strong>the</strong> vessel approached<br />

US$1.5 million.<br />

Claims by <strong>the</strong> Port Authority and individual crew members brought<br />

<strong>the</strong> total cost <strong>of</strong> <strong>the</strong> claim to almost US$2.2 million.<br />

Issue Date: 01/01/02 Case No. 18006<br />

22 23


Cargo<br />

Stability Needs Careful Attention<br />

The Incident:<br />

A Feeder Container vessel had completed cargo<br />

operations at one berth and was in <strong>the</strong> process<br />

<strong>of</strong> shifting to a second berth. A harbour tug<br />

commenced pushing <strong>the</strong> vessel towards <strong>the</strong> berth<br />

when <strong>the</strong> Member’s vessel began to heel over.<br />

When heeled over to approximately 10 to 15<br />

degrees, containers began to fall <strong>of</strong>f <strong>the</strong> vessel; <strong>the</strong><br />

tug stopped pushing, and this action in conjunction<br />

with <strong>the</strong> loss <strong>of</strong> containers enabled <strong>the</strong> vessel to<br />

return to near upright.<br />

Observations:<br />

The subsequent investigations showed that poor<br />

operational practices were allowed on board,<br />

with very little regard given to <strong>the</strong> safety <strong>of</strong> <strong>the</strong><br />

vessel. The centre <strong>of</strong> gravity (KG) <strong>of</strong> <strong>the</strong> vessel<br />

was determined to be well above <strong>the</strong> maximum<br />

permitted and no account had been taken <strong>of</strong> <strong>the</strong><br />

numerous free surfaces in <strong>the</strong> ballast tanks. To<br />

make matters worse, it was calculated that <strong>the</strong><br />

vessel was in fact 400t overloaded, resulting in a<br />

reduction in <strong>the</strong> freeboard <strong>of</strong> 30cms less than <strong>the</strong><br />

minimum permitted.<br />

These factors combined to result in a drastic<br />

reduction <strong>of</strong> transverse stability which was<br />

insufficient to withstand <strong>the</strong> forces created by <strong>the</strong><br />

pushing tug.<br />

Ironically, <strong>the</strong> top tiers <strong>of</strong> containers had not been<br />

secured but this allowed <strong>the</strong> containers to fall <strong>of</strong>f<br />

and <strong>the</strong> vessel returned to <strong>the</strong> upright.<br />

One <strong>of</strong> <strong>the</strong> contributing factors to <strong>the</strong> overloading<br />

was <strong>the</strong> under declaration <strong>of</strong> <strong>the</strong> containers<br />

weights by <strong>the</strong> shipper. This case highlights <strong>the</strong><br />

need to monitor <strong>the</strong> vessel’s condition at all times.<br />

By observing <strong>the</strong> drafts, <strong>the</strong> overloading would<br />

have been noted at an early stage and <strong>the</strong> vessel’s<br />

lack <strong>of</strong> adequate stability detected.<br />

Root Cause:<br />

Failure to observe stability requirements.<br />

Financial Cost:<br />

The total cost <strong>of</strong> this claim was in excess <strong>of</strong><br />

US$660,000; a great deal <strong>of</strong> this was accounted for<br />

in recovering containers that sank in <strong>the</strong> approach<br />

channel to <strong>the</strong> berth.<br />

Issue Date: 01/08/07<br />

Case No. 42200<br />

24 25


Cargo<br />

Be Prepared<br />

The Incident:<br />

This incident occurred on a 316 TEU feeder container vessel/bulk carrier immediately<br />

after loading had been completed.<br />

On completion <strong>of</strong> loading <strong>the</strong> vessel had a 1° list to starboard. This slowly increased.<br />

Corrective action was taken, but despite this <strong>the</strong> list continued to increase. By <strong>the</strong> time<br />

it had reached approximately 15°, a number <strong>of</strong> containers fell <strong>of</strong>f <strong>the</strong> top tier into <strong>the</strong><br />

harbour waters. The vessel <strong>the</strong>n violently rolled to port. The list increased until <strong>the</strong><br />

water line had reached <strong>the</strong> hatch coamings and progressive flooding started to take<br />

place. Fortunately more containers fell <strong>of</strong>f <strong>the</strong> top tier, reducing <strong>the</strong> list. The situation<br />

was eventually brought under control by discharging cargo and <strong>the</strong> vessel returned to<br />

an even keel.<br />

Observations:<br />

This incident was caused by a poorly prepared<br />

stow plan resulting in <strong>the</strong> vessel having negative<br />

stability upon completion <strong>of</strong> loading. The onboard<br />

calculations were incorrectly executed, as <strong>the</strong>y<br />

appear not to have taken <strong>the</strong> effects <strong>of</strong> free surface<br />

into account, so masking <strong>the</strong> true stability condition<br />

<strong>of</strong> <strong>the</strong> vessel.<br />

Feeder container vessels are renowned for<br />

<strong>the</strong>ir short turn round times and frequent cargo<br />

changes. Operators <strong>of</strong> <strong>the</strong>se vessels should ensure<br />

procedures are in place to minimise <strong>the</strong> potential<br />

for errors. Shore prepared stow plans must be<br />

checked for accuracy, preferably by a second<br />

person before <strong>the</strong>y are issued. Means should<br />

be provided to assist ship’s staff in assessing <strong>the</strong><br />

stability condition <strong>of</strong> <strong>the</strong> vessel so as to reduce<br />

<strong>the</strong> possibilities <strong>of</strong> errors being made in hastily<br />

completed calculations. This could take <strong>the</strong> form <strong>of</strong><br />

computers or encouragement to use prepared pro<br />

forma. Owners should satisfy <strong>the</strong>mselves that <strong>the</strong><br />

senior <strong>of</strong>ficers on board are fully familiar with <strong>the</strong><br />

stability requirements <strong>of</strong> <strong>the</strong>ir vessel.<br />

Root Cause:<br />

Inadequate lashing.<br />

Financial Cost:<br />

This turned out to be a very expensive claim as<br />

enormous efforts had to be made to locate <strong>the</strong><br />

sunken containers that fell overboard. The final<br />

cost was in <strong>the</strong> region <strong>of</strong> US$580,000.<br />

Issue Date: 01/01/02<br />

Case No. 34857<br />

26 27


Cargo<br />

Complacency Rules<br />

The Incident:<br />

This claim arose on a river craft specifically designed<br />

for a container feeder service between two<br />

terminals.<br />

Whilst manoeuvring <strong>of</strong>f one <strong>of</strong> <strong>the</strong> terminals with<br />

a cargo <strong>of</strong> 92 twenty and forty foot containers, <strong>the</strong><br />

vessel experienced a squall and started rolling as she<br />

turned beam on to <strong>the</strong> wind.<br />

A number <strong>of</strong> containers moved as <strong>the</strong> vessel rolled,<br />

striking adjacent containers. The lashings on two <strong>of</strong><br />

<strong>the</strong> containers struck consequently failed and two<br />

forty foot units were lost overboard.<br />

Observations:<br />

This claim arose because <strong>of</strong> poor operational<br />

practices on board. Investigations showed that <strong>the</strong><br />

lashing system employed was far from satisfactory.<br />

Local regulations did not require operators to have<br />

approved securing manuals and <strong>the</strong> operators did<br />

not have any requirements or guidelines <strong>of</strong> <strong>the</strong>ir<br />

own. Consequently <strong>the</strong> securing <strong>of</strong> <strong>the</strong> containers<br />

was left to <strong>the</strong> crew who relied on <strong>the</strong>ir experience.<br />

No procedures had been established requiring<br />

calculation <strong>of</strong> <strong>the</strong> vessel’s stability and <strong>the</strong>refore <strong>the</strong><br />

Master had no indication <strong>of</strong> <strong>the</strong> stability condition <strong>of</strong><br />

<strong>the</strong> vessel (e.g. too large or too small a GM) when<br />

she sailed.<br />

The lashing system did not follow normal acceptable<br />

practices and a number <strong>of</strong> deficiencies came to light<br />

during <strong>the</strong> Club’s investigations:<br />

• <strong>the</strong> lashing gear was not certified or provided<br />

with identification marks;<br />

• <strong>the</strong> amount <strong>of</strong> lashing gear used was insufficient.<br />

Where used, twist locks were only applied to<br />

two corners <strong>of</strong> each container and not all four<br />

and only minimal wire lashings were used<br />

(see pictures)<br />

• in-board containers were not secured at all;<br />

• <strong>the</strong> leads for <strong>the</strong> lashing wires were totally<br />

inappropriate and bulldog wire rope grips were<br />

insufficient in number, positioning and size;<br />

• it is doubtful whe<strong>the</strong>r <strong>the</strong> lashing gear utilised was<br />

in fact <strong>of</strong> sufficient strength for <strong>the</strong> task required<br />

<strong>of</strong> it;<br />

• no account appeared to have been taken <strong>of</strong> <strong>the</strong><br />

differences in height between standard and high<br />

cube units, which prevented <strong>the</strong> satisfactory use<br />

<strong>of</strong> bridge fittings;<br />

• no maintenance programme was in place for <strong>the</strong><br />

upkeep <strong>of</strong> <strong>the</strong> lashing gear.<br />

Root Cause:<br />

Inadequate lashing.<br />

Financial Cost:<br />

Salvage teams fortunately were able to recover<br />

<strong>the</strong>se containers <strong>the</strong>refore <strong>the</strong> Members have only<br />

been liable for <strong>the</strong>ir salvage and loss <strong>of</strong> contents.<br />

This is estimated to cost US$7,000.<br />

Issue Date: 18/06/03<br />

Case No. 37556<br />

28 29


Operations<br />

It will be Alright – But it Wasn’t<br />

The Incident:<br />

This incident involved loading containers into a hold<br />

that contained water and was compounded by <strong>the</strong> fact<br />

that <strong>the</strong> bilge pumping system was not operational.<br />

On completion <strong>of</strong> discharging, water was noted<br />

lying on <strong>the</strong> tank top and efforts to remove it failed<br />

because <strong>the</strong> bilge pumping system was found to be<br />

inoperative. Time constraints apparently prevented<br />

any o<strong>the</strong>r means to remove <strong>the</strong> water to be utilised.<br />

Loading was <strong>the</strong>n commenced and <strong>the</strong> vessel<br />

subsequently sailed.<br />

During <strong>the</strong> course <strong>of</strong> <strong>the</strong> voyage <strong>the</strong> hold bilge levels<br />

were reportedly monitored although some doubt<br />

exists as to whe<strong>the</strong>r or not <strong>the</strong> bilge sounding pipes<br />

were clear enabling soundings to be taken. It would<br />

appear that during <strong>the</strong> voyage, <strong>the</strong> bilge levels did in<br />

fact rise.<br />

Once <strong>the</strong> hold in question was discharged, <strong>the</strong><br />

majority <strong>of</strong> <strong>the</strong> lower tier <strong>of</strong> containers were found<br />

to have had <strong>the</strong>ir bases immersed in water.<br />

Observations:<br />

Notwithstanding <strong>the</strong> source <strong>of</strong> <strong>the</strong> water leak into<br />

<strong>the</strong> hold, <strong>the</strong> prime cause <strong>of</strong> this claim was <strong>the</strong> poor<br />

condition <strong>of</strong> <strong>the</strong> hold bilge pumping system. Access<br />

to bilge wells can be restricted due to <strong>the</strong> compact<br />

nature <strong>of</strong> container stowage and it is not always<br />

possible to use portable pumps to remove cargo<br />

hold bilge water if <strong>the</strong> main system fails. Therefore<br />

it is <strong>of</strong> <strong>the</strong> utmost importance to ensure that <strong>the</strong><br />

bilge pumping arrangement is regularly tested<br />

and maintained in full working order. Similarly <strong>the</strong><br />

sounding pipes must be kept clear at all times.<br />

The water entered <strong>the</strong> hold through cracks which<br />

had developed at <strong>the</strong> base <strong>of</strong> <strong>the</strong> cell guides where<br />

<strong>the</strong>y connect with <strong>the</strong> tank top. During <strong>the</strong> course<br />

<strong>of</strong> loading and discharging, <strong>the</strong>se guides suffer<br />

considerable physical stress and if <strong>the</strong> bases are<br />

weakened through corrosion at all, cracks will<br />

eventually occur. It is important <strong>the</strong>refore that <strong>the</strong>se<br />

areas are inspected regularly and repairs carried out<br />

promptly.<br />

It is apparent that <strong>the</strong> amount <strong>of</strong> water noted in <strong>the</strong><br />

hold on completion <strong>of</strong> discharging and during <strong>the</strong><br />

voyage was not considered significant, but obviously<br />

no allowance was made for <strong>the</strong> fact that <strong>the</strong> level<br />

will rise and fall when <strong>the</strong> vessel rolls and pitches in<br />

a seaway. Any water in a cargo hold is unacceptable<br />

and should be removed as soon as it is detected.<br />

Root Cause:<br />

Insufficient maintenance.<br />

Financial Cost:<br />

This claim was settled for US$60,000.<br />

Issue Date: 17/06/03<br />

Case No. 38930<br />

30 31


Operations<br />

Free Water and Poor Maths Result in Delays<br />

The Incident:<br />

This incident took place on a 25 year old 370 TEU<br />

feeder container ship. Shortly before arriving at<br />

<strong>the</strong> pilot station, an unexplained port list suddenly<br />

developed. The list was corrected and “sounding<br />

round” showed <strong>the</strong>re to be about 100 cm <strong>of</strong> water in<br />

her hold.<br />

Until ber<strong>the</strong>d, <strong>the</strong> vessel had flopped one way<br />

or ano<strong>the</strong>r on a number <strong>of</strong> occasions, each time<br />

corrected by moving ballast. Alongside she lay with<br />

a 15° list against <strong>the</strong> quay.<br />

The Chief Officer carried out an assessment <strong>of</strong> <strong>the</strong> stability and deemed<br />

<strong>the</strong> vessel to be unstable. The port authority subsequently refused to give<br />

permission for cargo operations to commence until <strong>the</strong> vessel was upright,<br />

<strong>the</strong> cause <strong>of</strong> <strong>the</strong> listing was determined and stability was confirmed by <strong>the</strong><br />

Classification Society.<br />

Efforts to pump out <strong>the</strong> hold bilge were thwarted by choked suctions.<br />

The services <strong>of</strong> a local salvage company were engaged to pump out <strong>the</strong><br />

hold and remove <strong>the</strong> top tier <strong>of</strong> containers in order to regain positive<br />

stability. The ballast tanks were closely monitored during this operation<br />

and it became apparent that water from two ballast tanks was entering<br />

<strong>the</strong> hold. The stability calculations were reworked and showed <strong>the</strong> vessel<br />

to have positive stability. This was later confirmed by <strong>the</strong> Classification<br />

Society.<br />

Permission for cargo operations to commence was given nearly three days<br />

after <strong>the</strong> vessel’s arrival at <strong>the</strong> port.<br />

Observations:<br />

The incident was caused by free water in <strong>the</strong> cargo<br />

hold.<br />

Choked hold bilge suctions prevented <strong>the</strong> water<br />

being pumped out by <strong>the</strong> ship’s staff.<br />

Investigations showed that <strong>the</strong> vessel had sustained<br />

two fractures in <strong>the</strong> tank top. These were believed<br />

to have been caused by <strong>the</strong> heavy landing <strong>of</strong><br />

containers during loading. The problem was fur<strong>the</strong>r<br />

exacerbated by <strong>the</strong> fact that <strong>the</strong> heeling tank filling<br />

pipe had corroded through. Ironically <strong>the</strong>refore,<br />

ballast water used to correct <strong>the</strong> list increased <strong>the</strong><br />

leakage into <strong>the</strong> hold, aggravating <strong>the</strong> problem.<br />

The Master was criticised for not conducting a<br />

more thorough investigation at <strong>the</strong> time <strong>of</strong> <strong>the</strong> initial<br />

listing.<br />

A regular systematic daily sounding programme is<br />

a well established procedure <strong>of</strong> good seamanship<br />

and would give an early indication <strong>of</strong> any problem.<br />

It would do away with <strong>the</strong> need to engage in <strong>the</strong><br />

dangerous practice <strong>of</strong> entering enclosed spaces to<br />

visually check <strong>the</strong> hold.<br />

The difficulties in pumping out <strong>the</strong> hold once <strong>the</strong><br />

water had entered were reportedly due to <strong>the</strong><br />

suctions being choked with debris. This highlights <strong>the</strong><br />

need for <strong>the</strong> holds to be kept free <strong>of</strong> rubbish and <strong>the</strong><br />

regular proving <strong>of</strong> <strong>the</strong> pumping arrangements. The<br />

provision <strong>of</strong> a hold bilge alarm would have given a<br />

very early indication <strong>of</strong> <strong>the</strong> water entering <strong>the</strong> hold.<br />

The original erroneous stability calculation was a<br />

major contributing factor to <strong>the</strong> delay suffered by<br />

<strong>the</strong> vessel. This should have been carried out prior<br />

to leaving <strong>the</strong> load port. Third party calculations can<br />

not be relied upon.<br />

The base <strong>of</strong> cell guides which carry <strong>the</strong> brunt <strong>of</strong><br />

heavy container movements, should be inspected<br />

on a regular basis so that corrosion and weakness<br />

can be detected at an early stage.<br />

Root Cause:<br />

Inadequate maintenance procedures.<br />

Financial Cost:<br />

The total claim is expected to be in <strong>the</strong> region <strong>of</strong><br />

US$75,000 to US$100,000.<br />

Issue Date: 01/01/02<br />

Case No. 32771<br />

32 33


Dry Cargo:<br />

Ro-Ro<br />

Cargo<br />

Premature Signing for Cargo Consignment Causes Hangover<br />

The Incident:<br />

This case involves cargo <strong>the</strong>ft within <strong>the</strong> port area. A brewery shipped<br />

a consignment <strong>of</strong> 282 cartons <strong>of</strong> beer on three shrink wrapped pallets<br />

between two depots in south east Asia. There was no direct shipping<br />

service between <strong>the</strong> depots. The beer was <strong>the</strong>refore shipped to an<br />

intermediate port where it was discharged for trans-shipment. The<br />

beer was loaded onto trucks for delivery to our Member’s vessel. As<br />

was <strong>the</strong>ir custom, our Member signed for receipt <strong>of</strong> <strong>the</strong> beer at <strong>the</strong>ir<br />

dock gate <strong>of</strong>fice. The truck and its consignment <strong>of</strong> beer disappeared<br />

somewhere between <strong>the</strong> dock gate <strong>of</strong>fice and <strong>the</strong> ship’s side. As a<br />

result <strong>of</strong> poor communications between <strong>the</strong> ship and <strong>the</strong> dock <strong>of</strong>fice,<br />

<strong>the</strong> disappearance <strong>of</strong> <strong>the</strong> beer was not noticed and it was only after<br />

<strong>the</strong> voyage was completed and a claim for non-delivery was received<br />

from <strong>the</strong> brewery that <strong>the</strong> circumstances came to light. The brewery<br />

was able to produce <strong>the</strong> road hauliers documents signed by <strong>the</strong><br />

shipowner showing that <strong>the</strong> beer had been delivered and had been<br />

accepted into <strong>the</strong> care <strong>of</strong> <strong>the</strong> shipowner. As a result <strong>the</strong> owners had to<br />

pay for <strong>the</strong> loss.<br />

Observations:<br />

<strong>Shipowners</strong> accepting cargo into <strong>the</strong>ir custody<br />

must take reasonable precautions to prevent loss<br />

or damage <strong>of</strong> <strong>the</strong> cargo. The custom and practice<br />

at <strong>the</strong> load port was for shipowners to accept<br />

consignments at <strong>the</strong> dock gate ra<strong>the</strong>r than at <strong>the</strong><br />

ship’s side. There was however no system for<br />

controlling or monitoring <strong>the</strong> progress <strong>of</strong> <strong>the</strong> cargo<br />

from <strong>the</strong>re to <strong>the</strong> ship. In this case <strong>the</strong> loss could<br />

have been avoided ei<strong>the</strong>r by only signing for <strong>the</strong><br />

cargo when it had been actually delivered to <strong>the</strong><br />

vessel itself or ensuring that proper procedures<br />

were in place for monitoring <strong>the</strong> progress <strong>of</strong> <strong>the</strong><br />

cargo after acceptance at <strong>the</strong> dock gate.<br />

Root Cause:<br />

Lack <strong>of</strong> shore procedures.<br />

Financial Cost:<br />

The cost to <strong>the</strong> shipowner exceeded US$5,000.<br />

Issue Date: 01/01/02<br />

Case No. 17180<br />

34 35


Cargo<br />

Poor Lashing Procedures Cause Destruction<br />

The Incident:<br />

During a voyage across <strong>the</strong> English Channel in<br />

heavy wea<strong>the</strong>r some vehicles on <strong>the</strong> car decks<br />

broke <strong>the</strong>ir lashings with <strong>the</strong> result that 18 lorries,<br />

<strong>the</strong>ir cargoes and three cars were damaged,<br />

resulting in many claims.<br />

Observations:<br />

Surveyors appointed by <strong>the</strong> Club reported that <strong>the</strong><br />

principal cause <strong>of</strong> <strong>the</strong> damage was <strong>the</strong> ship’s crew’s<br />

failure to properly lash <strong>the</strong> articulated vehicles. Our<br />

surveyors reported that <strong>the</strong>re was no company<br />

operating manual on board giving <strong>the</strong> crew guidance<br />

on car deck operations and safety. M-Notices and<br />

IMO publications were also unavailable. The Master<br />

had given no standing orders relating to car deck<br />

safety, nor had he set wea<strong>the</strong>r criteria above which<br />

cargo should be lashed.<br />

Root Cause:<br />

Inadequate lashing.<br />

Financial Cost:<br />

The damage to <strong>the</strong> vehicles amounted<br />

to US$128,150.<br />

Issue Date: 01/01/02<br />

Case No. 21978<br />

The majority <strong>of</strong> <strong>the</strong> damage was caused by a<br />

number <strong>of</strong> articulated vehicles which were only<br />

secured by four lashings, one at each corner <strong>of</strong> <strong>the</strong><br />

combined vehicles. This lashing system was totally<br />

inadequate for vehicles that did not form a rigid<br />

unit. In each case <strong>the</strong> damage was caused by <strong>the</strong><br />

vehicles jack-knifing, i.e. hinging at <strong>the</strong> joint between<br />

<strong>the</strong> tractor and trailer units. The jack-knifing<br />

resulted in <strong>the</strong> general slackening <strong>of</strong> <strong>the</strong> lashings<br />

which were <strong>the</strong>n subjected to shock loadings<br />

from <strong>the</strong> movement <strong>of</strong> ship and vehicles, with <strong>the</strong><br />

consequence that <strong>the</strong>y eventually parted.<br />

The claims that resulted from this incident were<br />

completely avoidable. Lashing <strong>the</strong> vehicles in<br />

accordance with IMO guidelines would have<br />

prevented <strong>the</strong> jack-knifing and consequent damage.<br />

Companies operating ro-ro ferries are now required<br />

to provide <strong>the</strong>ir vessels with a comprehensive cargo<br />

securing manual and Masters should issue standing<br />

instructions on when lashing is required and who<br />

has responsibility for ensuring that it is done.<br />

36 37


Section 2<br />

Tankers<br />

39


Tankers:<br />

Petroleum<br />

Personal Injury/Illness<br />

Explosion in Dockyard<br />

The Incident:<br />

A small tanker went into a repair yard to have damage to her<br />

starboard bow repaired. The vessel habitually carried premium<br />

motor spirit in all her cargo tanks and prior to arriving at <strong>the</strong> yard<br />

had cleaned and gas freed <strong>the</strong> tanks by filling <strong>the</strong>m to overflowing<br />

with seawater. Before hot work commenced <strong>the</strong> owners brought<br />

in a surveyor to test for explosive atmosphere and issue a gas free<br />

certificate. The certificate declared <strong>the</strong> vessel fit for hot work and<br />

indicated that all cargo tanks had been tested and found gas free.<br />

As shipyard workers started to cut away <strong>the</strong> damaged section an<br />

explosion occurred in <strong>the</strong> fore peak tank, severely damaging <strong>the</strong><br />

vessel and badly injuring two workers.<br />

Observations:<br />

The explosion almost certainly occurred as a result<br />

<strong>of</strong> an accumulation <strong>of</strong> explosive vapours in <strong>the</strong> fore<br />

peak tank. The reason for <strong>the</strong> accumulation was<br />

never discovered. The c<strong>of</strong>fer dam separating <strong>the</strong><br />

fore peak tank from <strong>the</strong> cargo tanks was found<br />

to be clean, dry and free <strong>of</strong> cargo vapours. The<br />

incident highlights <strong>the</strong> desirability <strong>of</strong> testing <strong>the</strong><br />

atmosphere in all enclosed spaces on tankers prior<br />

to commencing hot work.<br />

In this case <strong>the</strong>re was no formal contract between<br />

<strong>the</strong> vessel’s owners and <strong>the</strong> repair yard. The<br />

question <strong>of</strong> responsibility for ensuring that <strong>the</strong><br />

vessel was fit for hot work to be carried out was<br />

not clear. We would recommend that owners<br />

ensure this subject is addressed in every repair<br />

contract and that where possible <strong>the</strong> shipyard be<br />

given this responsibility.<br />

Root Cause:<br />

Insufficient safety procedures.<br />

Financial Cost:<br />

The entire fore part <strong>of</strong> <strong>the</strong> vessel had to be replaced<br />

at a cost <strong>of</strong> US$200,000. Claims by <strong>the</strong> injured<br />

workers were met by <strong>the</strong> shipyard’s insurers. In<br />

addition to this surveyor’s fees exceeding US$4,000<br />

were incurred.<br />

Issue Date: 01/01/02<br />

Case No. 20590<br />

40 41


Personal Injury/Illness<br />

Injury During Unmooring Operation<br />

The Incident:<br />

This accident involves a serious injury during<br />

unmooring operations as <strong>the</strong> vessel prepared to<br />

sail. The crew had been sent to stations and <strong>the</strong><br />

vessel had been singled up while awaiting customs<br />

clearance. The last two lines on <strong>the</strong> foredeck were<br />

those permanently stored on <strong>the</strong> windlass drums.<br />

At 08.30 customs clearance was obtained and<br />

<strong>the</strong> order was given to let go forward. When <strong>the</strong><br />

foredeck crew tried to slack down <strong>the</strong> line on <strong>the</strong><br />

starboard drum for letting go it would not do so.<br />

During efforts to free <strong>the</strong> rope <strong>the</strong> chief <strong>of</strong>ficer’s<br />

foot was caught in <strong>the</strong> machinery, resulting in very<br />

serious injuries to his toes.<br />

Observations:<br />

The berth had been exposed to a heavy swell<br />

which had caused <strong>the</strong> vessel to surge continually<br />

whilst alongside. The surging action had resulted<br />

in <strong>the</strong> mooring rope on <strong>the</strong> starboard windlass<br />

drum becoming buried in itself. When it became<br />

necessary to slacken down <strong>the</strong> line it jammed. The<br />

chief <strong>of</strong>ficer attempted to pull <strong>the</strong> line clear and<br />

in <strong>the</strong> process put his foot on <strong>the</strong> winch-bearing<br />

A-frame support forward <strong>of</strong> <strong>the</strong> starboard drum.<br />

The A-frame support is close to <strong>the</strong> drum face<br />

which had four flat bar stiffeners welded to it. The<br />

stiffeners passed close to <strong>the</strong> support, creating a<br />

guillotine-like effect. The mate’s foot was caught in<br />

<strong>the</strong> gap when <strong>the</strong> drum rotated and despite wearing<br />

steel-capped safety boots he was severely injured.<br />

The mate was fortunate as immediate hospitalisation and extensive microsurgery<br />

managed to save his toes.<br />

Following this incident <strong>the</strong> winch drums were modified to prevent a recurrence.<br />

This accident highlights <strong>the</strong> dangers <strong>of</strong> working too close to winches. The accident would<br />

have been avoided if <strong>the</strong> chief <strong>of</strong>ficer had employed a method <strong>of</strong> freeing <strong>the</strong> rope which<br />

did not involve close proximity to <strong>the</strong> machinery. One possible method might have been<br />

to put a stopper on <strong>the</strong> mooring rope while continuing to veer, thus using <strong>the</strong> power <strong>of</strong><br />

<strong>the</strong> winch to free <strong>the</strong> rope without creating <strong>the</strong> necessity for personnel to be in close<br />

proximity to it.<br />

Root Cause:<br />

Defect with equipment design.<br />

Financial Cost:<br />

Issue Date: 01/01/02<br />

Case No. 28781<br />

42 43


Personal Injury/Illness<br />

Severe Injuries Result From Failure to Follow Proper Procedures.<br />

The Incident:<br />

This incident occurred on board a tanker lying at anchor in<br />

sheltered waters. The vessel had been having trouble with its SSB<br />

radio and <strong>the</strong> radio <strong>of</strong>ficer had been instructed to investigate this<br />

problem.<br />

Shortly after lunch <strong>the</strong> Master was awakened from his afternoon<br />

nap by a loud thump. When he investigated he found <strong>the</strong> radio<br />

<strong>of</strong>ficer lying injured on <strong>the</strong> deck having fallen 18 metres from <strong>the</strong><br />

mast. The radio <strong>of</strong>ficer who had broken both legs, an arm, a rib and<br />

sustained internal injuries, was evacuated immediately to hospital<br />

where he was placed in intensive care.<br />

This company had compiled and provided <strong>the</strong> ship with a safety<br />

manual which included detailed instructions for working al<strong>of</strong>t. In<br />

addition several copies <strong>of</strong> <strong>the</strong> Code <strong>of</strong> Safe Working Practices for<br />

Merchant Seamen were available on board for <strong>the</strong> crew’s use. The<br />

radio <strong>of</strong>ficer had not complied with <strong>the</strong> requirements <strong>of</strong> ei<strong>the</strong>r <strong>the</strong><br />

Code or <strong>the</strong> safety manual. He was working alone and had not<br />

advised <strong>the</strong> duty deck <strong>of</strong>ficer that he would be working al<strong>of</strong>t. He<br />

was not wearing a safety harness.<br />

Observations:<br />

Although <strong>the</strong> owners had provided <strong>the</strong> vessel with a considerable<br />

quantity <strong>of</strong> safety documentation, that in itself was insufficient to<br />

instil a safety-conscious attitude amongst <strong>the</strong> crew. Unless senior<br />

management take a close interest in enforcing a proper safety<br />

regime on board, a safety culture will not develop within <strong>the</strong><br />

company. If safety consciousness had been highly developed, <strong>the</strong><br />

radio <strong>of</strong>ficer would probably not have considered working al<strong>of</strong>t<br />

without taking <strong>the</strong> proper precautions.<br />

Root Cause:<br />

Insufficient safety environment.<br />

Financial Cost:<br />

The owners had to pay substantial compensation to <strong>the</strong> radio <strong>of</strong>ficer<br />

even though he was primarily responsible for <strong>the</strong> accident occurring.<br />

The total cost to <strong>the</strong> company after costs were taken into account<br />

was almost US$40,000.<br />

Issue Date: 01/01/02<br />

Case No. 23194<br />

44 45


Cargo<br />

Deviation from Agreed Discharge Plan Leads to Cocktail<br />

The Incident:<br />

The vessel involved in this case is a coastal tanker carrying a full cargo <strong>of</strong> four grades <strong>of</strong><br />

lubricating oil. The vessel arrived at <strong>the</strong> discharge berth where she was due to discharge<br />

into both shore tanks and barges moored alongside. After <strong>the</strong> ship was ullaged and samples<br />

taken, a written discharge plan was agreed between <strong>the</strong> ship and <strong>the</strong> terminal. The plan<br />

was signed by <strong>the</strong> ship’s <strong>of</strong>ficers but retained by <strong>the</strong> terminal with no <strong>copy</strong> being left on<br />

board. The details <strong>of</strong> <strong>the</strong> plan were recorded in <strong>the</strong> duty <strong>of</strong>ficer’s note<strong>book</strong>. It had been<br />

agreed that initially two parcels, 500 SN and 100 SN, would be discharged to <strong>the</strong> shore<br />

followed by 200 SN and 150 SN.<br />

The 500 SN and 100 SN manifolds were prepared for <strong>the</strong> cargo hoses. After <strong>the</strong> 500 SN<br />

hose had been connected <strong>the</strong> jetty operator asked whe<strong>the</strong>r <strong>the</strong> second open manifold<br />

was for 150 SN. The duty <strong>of</strong>ficer advised him that it was <strong>the</strong> 100 SN manifold. The jetty<br />

operator told <strong>the</strong> duty <strong>of</strong>ficer that he wanted <strong>the</strong> 150 SN not <strong>the</strong> 100 SN. The duty<br />

<strong>of</strong>ficer reminded <strong>the</strong> jetty operator that it had been agreed in writing that <strong>the</strong> 100 SN<br />

would be discharged before <strong>the</strong> 150 SN. Despite this <strong>the</strong> jetty operator continued to insist<br />

that he wanted 150 SN and as a result <strong>the</strong> manifolds were changed over and <strong>the</strong> hose<br />

connected to <strong>the</strong> 150 SN manifold. After approximately 1½ pumping <strong>the</strong> shore asked <strong>the</strong><br />

vessel to stop despite <strong>the</strong> fact <strong>the</strong>re was approximately 70 metric tons left on board. On<br />

investigation it turned out that despite what <strong>the</strong> jetty operator had said, <strong>the</strong> terminal had<br />

been adhering to <strong>the</strong> original discharge plan with <strong>the</strong> result that 180 tons <strong>of</strong> 150 SN had<br />

been pumped into <strong>the</strong> wrong tank, contaminating <strong>the</strong> 220 tons <strong>of</strong> 100 SN it contained.<br />

Observations:<br />

The vessel had followed <strong>the</strong> correct procedure up<br />

until <strong>the</strong> time <strong>the</strong> second cargo hose was connected.<br />

At that point <strong>the</strong> duty <strong>of</strong>ficer agreed to deviate from<br />

<strong>the</strong> written plan without proper authorisation. If<br />

<strong>the</strong> <strong>of</strong>ficer on watch had insisted that a new cargo<br />

discharge plan had been drawn up or <strong>the</strong> original<br />

one amended in writing, <strong>the</strong> confusion within <strong>the</strong><br />

terminal would have become apparent and <strong>the</strong><br />

contamination would have been avoided.<br />

Root Cause:<br />

Non compliance with procedures.<br />

Financial Cost:<br />

The shipowners and terminal operators negotiated<br />

a commercial settlement with <strong>the</strong> owners <strong>of</strong> <strong>the</strong> oil.<br />

The cost <strong>of</strong> investigating this incident and obtaining<br />

<strong>the</strong> legal advice on which negotiations were based<br />

amounted to US$17,000.<br />

Issue Date: 01/01/02<br />

Case No. 20662<br />

46 47


Cargo<br />

The Cost <strong>of</strong> Ensuring <strong>the</strong> Vessel’s Turnaround<br />

Time can be Outweighed by <strong>the</strong> Final Overall Cost<br />

The Incident:<br />

This claim involved a 5000gt products tanker<br />

discharging two grades <strong>of</strong> cargo simultaneously.<br />

During <strong>the</strong> course <strong>of</strong> <strong>the</strong> discharge cross grade<br />

contamination occurred.<br />

The vessel is designed so that she can carry<br />

a maximum <strong>of</strong> three grades <strong>of</strong> cargo whilst<br />

maintaining two valve separation and on this<br />

particular occasion two grades were carried.<br />

Loading was completed without incident.<br />

Discharge <strong>of</strong> <strong>the</strong> two grades was commenced<br />

simultaneously utilising No.1 pump for one grade<br />

and No.3 for <strong>the</strong> second grade. During <strong>the</strong><br />

course <strong>of</strong> <strong>the</strong> discharge, No.1 pump developed<br />

a leak at <strong>the</strong> forward seal and <strong>the</strong> pump became<br />

unserviceable. The pump was stopped and<br />

<strong>the</strong> pipelines set up to discharge <strong>the</strong> unleaded<br />

gasoline via No.2 cargo pump. The discharge was<br />

continued. At some stage <strong>the</strong>reafter <strong>the</strong> terminal<br />

advised <strong>the</strong> vessel that contamination between<br />

grades had been noted ashore.<br />

Observations:<br />

The design <strong>of</strong> <strong>the</strong> vessel is such that two valve<br />

separation can only be maintained when each <strong>of</strong> <strong>the</strong><br />

three pumps is used on its own designated tanks<br />

or <strong>the</strong> two outside pumps (nos 1 & 3) are utilised;<br />

whenever consecutive pumps are lined up on tanks<br />

<strong>of</strong> one <strong>of</strong> <strong>the</strong> o<strong>the</strong>r systems <strong>the</strong>n only one valve<br />

separation is possible. Unfortunately in this incident,<br />

<strong>the</strong> decision to utilise No.2 pump on No.1 system<br />

cargo tanks resulted in single valve separation<br />

between <strong>the</strong> two grades. (It is believed that during<br />

<strong>the</strong> stripping phase <strong>of</strong> discharging one <strong>of</strong> <strong>the</strong> grades,<br />

<strong>the</strong> pressure differential across <strong>the</strong> valve allowed <strong>the</strong><br />

contamination to take place).<br />

Two valve separation between grades is considered<br />

<strong>the</strong> minimum acceptable by <strong>the</strong> petroleum industry<br />

as <strong>the</strong> likelihood <strong>of</strong> two valves failing at <strong>the</strong> same<br />

time is considered to be acceptably less than <strong>the</strong><br />

failure <strong>of</strong> a single valve. [Failure can be caused by: i)<br />

a defective seal; ii) debris lying in <strong>the</strong> valve seat; and<br />

iii) <strong>the</strong> valve not being closed fully].<br />

In this incident, <strong>the</strong> decision to continue discharging<br />

both grades simultaneously after <strong>the</strong> pump<br />

failure was wrong, however it is not known what<br />

commercial pressures, if any, were placed upon <strong>the</strong><br />

vessel to expedite <strong>the</strong> discharge.<br />

In such circumstances if shore terminals insist on<br />

ships continuing operations, <strong>the</strong> representative<br />

making <strong>the</strong> request should be made fully aware<br />

<strong>of</strong> <strong>the</strong> possible consequences and requested to<br />

accept <strong>the</strong> responsibility for any adverse effects. If<br />

responsibility is to lie with <strong>the</strong> Master and vessel,<br />

<strong>the</strong>n <strong>the</strong> operation should be continued within <strong>the</strong><br />

limitations <strong>of</strong> <strong>the</strong> vessel’s design.<br />

Root Cause:<br />

Failure to comply with vessel design.<br />

Financial Cost:<br />

The cost <strong>of</strong> this claim is US$110,000.<br />

Issue Date: 01/01/02<br />

Case No. 37817<br />

48 49


Cargo<br />

Two Valves are Better than One<br />

The Incident:<br />

This vessel was a small parcel tanker time chartered to an oil major,<br />

plying between two <strong>of</strong> <strong>the</strong>ir terminals. The vessel was fitted with five<br />

sets <strong>of</strong> cargo wing tanks, fed by a ring main pipeline system. On <strong>the</strong><br />

voyage in question <strong>the</strong> vessel was ordered to load two grades <strong>of</strong> motor<br />

spirit. The first, unleaded petrol, was loaded into 2 and 4 wing tanks.<br />

This was followed by leaded petrol being loaded into 1 and 5 wing tanks.<br />

Number 3 wing tanks remained empty.<br />

On arrival at <strong>the</strong> discharge berth both grades were to be discharged<br />

ashore simultaneously, <strong>the</strong> leaded petrol was to be discharged using<br />

<strong>the</strong> portside pump/line system and <strong>the</strong> unleaded via <strong>the</strong> starboard<br />

side pump/line system. Shortly after discharge commenced <strong>the</strong><br />

starboard pump broke down. As a consequence 1 and 5 wing tanks<br />

were completely discharged whereafter <strong>the</strong> line was flushed with fresh<br />

water and disconnected. The unleaded hose was <strong>the</strong>n connected to <strong>the</strong><br />

portside pump/line system which was <strong>the</strong>n used to discharge <strong>the</strong> second<br />

parcel. Shortly after discharge resumed terminal personnel informed<br />

<strong>the</strong> vessel that measurement <strong>of</strong> shore tanks indicated that an additional<br />

90 cubic metres <strong>of</strong> product had been discharged with <strong>the</strong> first parcel <strong>of</strong><br />

leaded petrol. Discharge operations were stopped and an investigation<br />

was mounted. The investigation revealed that a crossover gate valve in<br />

number 2 port cargo tank had not been properly closed, with <strong>the</strong> result<br />

that unleaded petrol had been drawn from <strong>the</strong> starboard line system<br />

and discharged with <strong>the</strong> leaded petrol.<br />

Observations:<br />

The tanker’s ring main system only permitted single valve separation<br />

between <strong>the</strong> two grades <strong>of</strong> cargo with <strong>the</strong> result that <strong>the</strong> failure <strong>of</strong><br />

a valve or operator error in <strong>the</strong> manipulation <strong>of</strong> <strong>the</strong> valves would<br />

inevitably result in cross contamination. Subsequent to this incident<br />

<strong>the</strong> vessel’s pipeline system was modified to give proper segregation<br />

between cargo grades.<br />

Root Cause:<br />

Failure to comply with vessel design requirement.<br />

Financial Cost:<br />

On this occasion <strong>the</strong> oil company was able to resolve <strong>the</strong> problem<br />

<strong>of</strong> <strong>the</strong> contaminated fuel by blending and no cargo claim was made.<br />

Never<strong>the</strong>less <strong>the</strong> costs <strong>of</strong> investigating <strong>the</strong> matter amounted to<br />

approximately US$1,000.<br />

Issue Date: 01/01/02<br />

Case No. 19597<br />

50 51


Cargo<br />

Poor Tanker Practices Leads to Expensive Delay for Member.<br />

The Incident:<br />

This tanker had been chartered to a company which had a contract <strong>of</strong><br />

affreightment with a major oil company. The vessel was ordered to load<br />

premium motor spirit and automotive diesel oil at two separate berths.<br />

The motor spirit was loaded in 2 wings and 4 wings at <strong>the</strong> first berth<br />

and <strong>the</strong> automotive diesel oil was loaded in 1 and 3 wings at <strong>the</strong> second<br />

berth. On arrival at <strong>the</strong> discharge port <strong>the</strong> cargo in 2 wings was rejected<br />

by <strong>the</strong> consignee as being <strong>of</strong>f-spec. The remaining cargo was found<br />

to be within <strong>the</strong> specification and was discharged. After discharge <strong>the</strong><br />

shore tank was sampled and it was discovered that not only were both<br />

parcels <strong>of</strong>f-specification but <strong>the</strong> outturn <strong>of</strong> volume <strong>of</strong> <strong>the</strong> motor spirit<br />

had apparently increased by over 100 tons while <strong>the</strong> volume <strong>of</strong> diesel<br />

oil had decreased by a similar figure. The contaminated oils could not be<br />

reprocessed at <strong>the</strong> discharge port and <strong>the</strong> vessel was delayed for over<br />

seven weeks while owners, charterers and <strong>the</strong> oil company argued over<br />

<strong>the</strong> disposal <strong>of</strong> <strong>the</strong> contaminated oil. The terminal lodged a claim for<br />

US$420,000, this being <strong>the</strong> value <strong>of</strong> <strong>the</strong> entire cargo.<br />

Observations:<br />

A thorough investigation by surveyors appointed<br />

by <strong>the</strong> Club revealed that <strong>the</strong> vessel had only been<br />

designed to carry a single grade <strong>of</strong> cargo, with<br />

<strong>the</strong> result that it was impossible to follow normal<br />

tanker practice in separating different grades <strong>of</strong><br />

product by two or more valves. The surveyors also<br />

discovered that after completing loading at <strong>the</strong> first<br />

berth, certain valves were left open, allowing <strong>the</strong><br />

cargo in 2 wings to become contaminated with<br />

diesel oil. The surveyor’s investigation also showed<br />

that during <strong>the</strong> discharge operation some more<br />

valves were opened in error, contaminating <strong>the</strong><br />

remainder <strong>of</strong> <strong>the</strong> cargo. The surveyors were critical<br />

<strong>of</strong> <strong>the</strong> method and effectiveness <strong>of</strong> line-clearing at<br />

<strong>the</strong> discharge port.<br />

Root Cause:<br />

Failure to comply with ship design requirements.<br />

Financial Cost:<br />

In this case <strong>the</strong> owners were extremely fortunate<br />

as <strong>the</strong> provisions <strong>of</strong> <strong>the</strong> charter party enabled <strong>the</strong>m<br />

to pass responsibility for cargo contamination on<br />

to <strong>the</strong> charterers. Never<strong>the</strong>less <strong>the</strong> costs <strong>of</strong> <strong>the</strong><br />

investigation alone amounted to US$17,000. In<br />

addition to this <strong>the</strong> owners were unable to trade<br />

<strong>the</strong> vessel for approximately two months.<br />

This vessel is no longer entered in <strong>the</strong> Club.<br />

Issue Date: 01/01/02<br />

Case No. 18724<br />

52 53


Cargo<br />

Master’s Commercial Awareness could have Reduced Claim<br />

The Incident:<br />

The claim arose on board a coastal tanker carrying<br />

premium motor spirit. The bill <strong>of</strong> lading was issued<br />

using <strong>the</strong> shore terminal’s figures. As this figure was<br />

greater than <strong>the</strong> quantity calculated a letter <strong>of</strong> protest<br />

was issued by <strong>the</strong> Master to <strong>the</strong> loading terminal.<br />

At <strong>the</strong> discharge port <strong>the</strong> vessel’s cargo pumps<br />

lost suction before <strong>the</strong> tanks were completely<br />

dry. It proved impossible to regain suction and <strong>the</strong><br />

cargo remaining on board was considered to be<br />

unpumpable. On completion <strong>of</strong> discharge <strong>the</strong> vessel<br />

was heavily trimmed by <strong>the</strong> stern with <strong>the</strong> result<br />

that <strong>the</strong> cargo residues lay in wedges at <strong>the</strong> ends <strong>of</strong><br />

<strong>the</strong> cargo tanks aft <strong>of</strong> <strong>the</strong> sounding pipes. The actual<br />

quantity remaining on board could not <strong>the</strong>refore be<br />

accurately assessed.<br />

The receiving terminal claimed short delivery <strong>of</strong><br />

over 50 metric tons based solely on <strong>the</strong> difference<br />

between <strong>the</strong> bill <strong>of</strong> lading figure and <strong>the</strong> shore outturn<br />

figure.<br />

At <strong>the</strong> next berth surveyors appointed by <strong>the</strong> Club<br />

attended on board and by reducing <strong>the</strong> vessel’s trim<br />

were able to accurately establish <strong>the</strong> amount <strong>of</strong><br />

cargo remaining on board. It was found to be just<br />

under 22 metric tons and not over 50 as alleged<br />

by <strong>the</strong> consignee. The value <strong>of</strong> <strong>the</strong> difference was<br />

approximately US$7,000. The evidential value <strong>of</strong> our<br />

surveyor’s report was however seriously weakened<br />

because <strong>the</strong> survey took place some time after<br />

discharge had been completed, when consignee’s<br />

representatives were not in attendance.<br />

Observations:<br />

If <strong>the</strong> vessel’s Master had reduced <strong>the</strong> vessel’s trim and properly<br />

quantified <strong>the</strong> unpumpable ROB before leaving <strong>the</strong> discharge berth<br />

while <strong>the</strong> consignee’s surveyor was still in attendance, <strong>the</strong> owners<br />

would have been in a much stronger position to resist <strong>the</strong> short<br />

delivery claim.<br />

Root Cause:<br />

Insufficient operation procedures.<br />

Financial Cost:<br />

It was possible to negotiate a settlement <strong>of</strong> <strong>the</strong> short landing claim<br />

however <strong>the</strong> total cost including surveyor’s fees exceeded US$9,000.<br />

Issue Date: 01/01/02<br />

Case No. 19772<br />

54 55


Cargo<br />

Out <strong>of</strong> Sight Really Can Mean Out <strong>of</strong> Mind<br />

The Incident:<br />

This claim involved a products tanker delivering<br />

contaminated cargo on three consecutive voyages.<br />

On <strong>the</strong> first two occasions <strong>the</strong> terminal accepted <strong>the</strong><br />

cargo, but although finally accepting it <strong>the</strong> third time<br />

it was with some reluctance.<br />

During <strong>the</strong> course <strong>of</strong> each <strong>of</strong> <strong>the</strong> three discharges<br />

<strong>the</strong> products to varying degrees were found to<br />

be contaminated with water. Blending or fur<strong>the</strong>r<br />

refining was required to return <strong>the</strong> products to <strong>the</strong><br />

original specifications.<br />

The cause <strong>of</strong> <strong>the</strong> contamination proved difficult<br />

to find because <strong>the</strong> water was noted to have very<br />

low chlorides which indicated (incorrectly) that<br />

<strong>the</strong> contamination was not caused by seawater. In<br />

addition, during <strong>the</strong> final discharge <strong>the</strong> contamination<br />

was noted to be intermittent.<br />

It was finally assumed that <strong>the</strong> water was entering<br />

<strong>the</strong> cargo tanks through defective valve glands –<br />

although <strong>the</strong> cargo sample from <strong>the</strong> tanks was within<br />

specification!<br />

Upon completion <strong>of</strong> <strong>the</strong> third discharge <strong>the</strong> vessel<br />

sailed and anchored <strong>of</strong>f <strong>the</strong> port.<br />

Fur<strong>the</strong>r investigation by <strong>the</strong> crew at this time<br />

determined that “several years” prior to this spate<br />

<strong>of</strong> contaminations, <strong>the</strong> vessel had experienced cargo<br />

leaking out through a sea valve. As a result a 6mm<br />

blank was inserted on <strong>the</strong> outboard side <strong>of</strong> <strong>the</strong> sea<br />

valve, and unfortunately this had been forgotten. As<br />

time passed <strong>the</strong> blank had corroded through and<br />

when ballasting, unbeknown to <strong>the</strong> ship’s crew, a<br />

section <strong>of</strong> <strong>the</strong> pipeline filled with water. When cargo<br />

was subsequently being discharged, this water was<br />

<strong>the</strong>n drawn into <strong>the</strong> cargo.<br />

Observations:<br />

Whenever a blank is inserted into a pipeline it<br />

should be made as conspicuous as possible and all<br />

staff associated with cargo operations made aware<br />

<strong>of</strong> its existence, including subsequent crews.<br />

In addition, a blank inserted in a pipeline as a result<br />

<strong>of</strong> a leaking valve is only a temporary measure and<br />

should not be left in place for years on end. The<br />

efficiency <strong>of</strong> <strong>the</strong> overhaul <strong>of</strong> ship side valves during<br />

dry docking must also be questioned.<br />

Root Cause:<br />

Insufficient maintenance procedures.<br />

Financial Cost:<br />

Because <strong>the</strong> receivers accepted most <strong>of</strong> <strong>the</strong><br />

contaminated cargoes without complaint, <strong>the</strong> overall<br />

cost <strong>of</strong> this claim is US$5,000.<br />

Issue Date: 01/01/02<br />

Case No. 38847<br />

56 57


Cargo<br />

Poor Line Washing Probably Caused Contamination<br />

The Incident:<br />

This is a case <strong>of</strong> cargo contamination on board a parcel tanker. On its previous voyage <strong>the</strong><br />

tanker carried a full cargo <strong>of</strong> gas oil. After discharge <strong>the</strong> tanks were washed in preparation<br />

for carrying a number <strong>of</strong> high quality products. Prior to loading <strong>the</strong> tanks were inspected<br />

by an independent inspector and passed as being clean, dry and suitable for <strong>the</strong> products<br />

to be loaded. A number <strong>of</strong> products were <strong>the</strong>n loaded including a parcel <strong>of</strong> solvent C9 in<br />

4 wings. On arrival at discharge port <strong>the</strong> samples <strong>of</strong> <strong>the</strong> solvent taken by <strong>the</strong> consignees’<br />

surveyor showed a slight change in colour. Gas chromatography analysis revealed that <strong>the</strong><br />

product had been contaminated by very small quantities <strong>of</strong> gas oil. Consignees claimed that<br />

<strong>the</strong> slight change in colour was sufficient to render <strong>the</strong> product unmarketable and rejected<br />

<strong>the</strong> entire consignment. The contaminated cargo was eventually sold to a salvage buyer for<br />

less than half its original value.<br />

Observations:<br />

This incident highlights <strong>the</strong> importance <strong>of</strong> tank cleaning and line washing in preparation<br />

for <strong>the</strong> carriage <strong>of</strong> high grade products and chemicals. In this case <strong>the</strong> cause <strong>of</strong> <strong>the</strong><br />

contamination was never properly determined. The vessel’s tank coatings were in good<br />

condition and <strong>the</strong> tanks had been passed by an independent surveyor. The most likely<br />

source <strong>of</strong> contamination seems to be inadequate or incomplete line washing, with <strong>the</strong><br />

result that a plug <strong>of</strong> <strong>the</strong> previous cargo became trapped in <strong>the</strong> pipeline system. It is vital<br />

that line washing be arranged in such a way as to ensure that every section <strong>of</strong> <strong>the</strong> pipeline<br />

system is thoroughly flushed through during <strong>the</strong> process.<br />

Root Cause:<br />

Inadequate line washing.<br />

Financial Cost:<br />

The total cost <strong>of</strong> this claim after <strong>the</strong> proceeds <strong>of</strong> <strong>the</strong> salvage sale had been taken into<br />

account exceeded US$73,000.<br />

Issue Date: 01/01/02<br />

Case No. 24249<br />

58 59


Navigation<br />

With <strong>the</strong> Tide is Against Convention<br />

The Incident:<br />

This incident occurred when a 1,500 GRT tanker was berthing at an<br />

oil jetty. During <strong>the</strong> berthing manoeuvre <strong>the</strong> vessel’s bow came into<br />

contact with <strong>the</strong> hose gantry on <strong>the</strong> jetty, damaging both <strong>the</strong> gantry and<br />

two cargo hoses. In his statement <strong>the</strong> Master alleged that <strong>the</strong> cause <strong>of</strong><br />

<strong>the</strong> contact was <strong>the</strong> vessel failing to respond to an astern engine order.<br />

Observations:<br />

According to both <strong>the</strong> Chief Engineer and Engineering Officer <strong>of</strong><br />

<strong>the</strong> watch, <strong>the</strong>re was no mechanical problem during <strong>the</strong> berthing<br />

operation. Subsequent investigation by a surveyor revealed that <strong>the</strong><br />

Master had been attempting to berth with <strong>the</strong> tide under his stern. It<br />

is highly likely that <strong>the</strong> Master simply misjudged <strong>the</strong> effect <strong>of</strong> <strong>the</strong> tide<br />

when applying astern power. This accident would probably have been<br />

avoided if <strong>the</strong> Master had adopted a conventional uptide approach to<br />

<strong>the</strong> berth.<br />

Root Cause:<br />

Human error.<br />

Financial Cost:<br />

The costs <strong>of</strong> repairs to <strong>the</strong> jetty exceeded US$46,000.<br />

Issue Date: 01/01/02<br />

Case No. 20910<br />

60 61


Navigation<br />

Member’s Involvement with Delay to Deep Sea Vessel Proves Expensive.<br />

The Incident:<br />

This incident involved a small bunker barge which had<br />

been engaged to supply lube oil to an ocean going<br />

vessel at anchor. During <strong>the</strong> bunkering operation <strong>the</strong><br />

deep sea vessel’s gangway had been lowered and<br />

used to provide access to and from <strong>the</strong> bunker barge.<br />

After bunker operations had been completed <strong>the</strong><br />

crew did not hoist <strong>the</strong> gangway before casting <strong>of</strong>f<br />

<strong>the</strong> barge’s mooring lines. As <strong>the</strong> barge manoeuvred<br />

away from <strong>the</strong> side <strong>of</strong> <strong>the</strong> ocean going vessel it came<br />

into contact with, and damaged, <strong>the</strong> ship’s gangway.<br />

Although <strong>the</strong> negligence <strong>of</strong> <strong>the</strong> deep sea vessel’s crew<br />

was a major contributing factor in this loss, <strong>the</strong> Club<br />

was advised that <strong>the</strong> barge would be held liable for<br />

not exercising sufficient care while manoeuvring away<br />

from <strong>the</strong> vessel’s side.<br />

Observations:<br />

This claim illustrates how a relatively minor incident<br />

can be greatly inflated if <strong>the</strong> damage causes delay to<br />

a large vessel. In this case <strong>the</strong> problem could have<br />

been avoided if <strong>the</strong> bunker barge had insisted on <strong>the</strong><br />

gangway being raised clear before departing.<br />

Root Cause:<br />

Failure to comply with procedures.<br />

Financial Cost:<br />

Repairs to <strong>the</strong> accommodation ladder took four<br />

days and cost US$13,000. In addition to <strong>the</strong> cost <strong>of</strong><br />

repairs <strong>the</strong> owners <strong>of</strong> <strong>the</strong> deep sea vessel claimed<br />

four days’ loss <strong>of</strong> hire which when combined<br />

with additional port dues, survey fees and o<strong>the</strong>r<br />

miscellaneous expenses brought <strong>the</strong> total claim<br />

against our Member to almost US$36,000. Although<br />

we were successful in negotiating a settlement at a<br />

reduced figure, <strong>the</strong> total cost to <strong>the</strong> barge owners<br />

after surveyors’ and correspondents’ fees had been<br />

paid exceeded US$27,000.<br />

Issue Date: 01/01/02<br />

Case No. 20339<br />

62 63


Navigation<br />

Rushed Approach Results in Collision<br />

The Incident:<br />

In <strong>the</strong> early hours a bunker tanker finished loading a cargo <strong>of</strong> fuel oil<br />

and left <strong>the</strong> berth bound for <strong>the</strong> anchorage to await <strong>the</strong> arrival <strong>of</strong> <strong>the</strong><br />

deep sea vessel she was to service. The anchorage was crowded and<br />

<strong>the</strong> vessel worked through <strong>the</strong> moored vessels at slow speed looking for<br />

a suitable spot to drop <strong>the</strong> anchor. The vessel came upon a clear area<br />

and <strong>the</strong> Master made a snap decision to anchor in that spot. The tanker<br />

had <strong>the</strong> wind on her starboard quarter and a 2 knot following tide. To<br />

bring <strong>the</strong> vessel head to wind and tide <strong>the</strong> helm was put hard aport and<br />

<strong>the</strong> engine full astern. Unfortunately <strong>the</strong> Master totally misjudged <strong>the</strong><br />

strength <strong>of</strong> <strong>the</strong> tide and <strong>the</strong> vessel was swept broadside onto <strong>the</strong> bows<br />

<strong>of</strong> an anchored vessel. Number 3 cargo oil tank was breached and over<br />

20 cubic metres <strong>of</strong> heavy fuel oil spilled into <strong>the</strong> water.<br />

Observations:<br />

This incident would probably have been avoided if<br />

<strong>the</strong> Master had not been in such a hurry to anchor<br />

and had adopted a more conventional approach.<br />

Instead <strong>of</strong> trying to swing <strong>the</strong> vessel immediately<br />

he should have continued on until he could turn his<br />

vessel safely and approach <strong>the</strong> anchorage position<br />

heading into wind and tide. The method <strong>of</strong> approach<br />

adopted prevented him properly assessing <strong>the</strong><br />

effects <strong>of</strong> wind and tide on his vessel and as a result<br />

he completely misjudged his approach.<br />

Root Cause:<br />

Human error.<br />

Financial Cost:<br />

In addition to <strong>the</strong> cost <strong>of</strong> repairs to <strong>the</strong> anchored<br />

tanker <strong>the</strong> owners received a substantial claim from<br />

<strong>the</strong> Port Authority for oil pollution monitoring and<br />

clean up operations. This brought <strong>the</strong> total cost<br />

excluding <strong>the</strong> cost <strong>of</strong> damage to his own vessel to<br />

over US$82,000.<br />

Issue Date: 01/01/02<br />

Case No. 19193<br />

64 65


Navigation<br />

But We’ve Always Done it That Way<br />

The Incident:<br />

We have been advised <strong>of</strong> <strong>the</strong> following case,<br />

featured in <strong>the</strong> Marine Accident Investigation Branch<br />

(MAIB) safety digest No1/2007 (see below link for<br />

<strong>the</strong> document) that we feel will be <strong>of</strong> great interest<br />

to our Members.<br />

“Poor bridge team management practices while<br />

approaching and entering a narrow channel led<br />

directly to <strong>the</strong> grounding <strong>of</strong> a 1,845gt tanker. It had<br />

been <strong>the</strong> early hours <strong>of</strong> <strong>the</strong> morning and <strong>the</strong> vessel<br />

was returning to her usual load port, in ballast. The<br />

bridge watch consisted <strong>of</strong> an <strong>of</strong>ficer <strong>of</strong> <strong>the</strong> watch, a<br />

lookout and <strong>the</strong> Master.<br />

The vessel had passed through <strong>the</strong> same channel a<br />

few days earlier on her loaded passage, and reciprocal<br />

courses had been chosen for <strong>the</strong> return passage.<br />

The planned track involved a 40 degree alteration<br />

<strong>of</strong> course just one ship’s length before <strong>the</strong> entrance<br />

to <strong>the</strong> channel. The bridge that spanned <strong>the</strong> narrow<br />

passage at its entrance had a white transit light which<br />

marked <strong>the</strong> centre <strong>of</strong> <strong>the</strong> bridge and <strong>the</strong> channel.<br />

As <strong>the</strong> vessel approached <strong>the</strong> channel at full speed,<br />

<strong>the</strong> Master took <strong>the</strong> con, switched <strong>the</strong> helm to hand<br />

steering and, against company instructions, started<br />

to steer <strong>the</strong> vessel himself towards and through<br />

<strong>the</strong> narrow entrance. The <strong>of</strong>ficer <strong>of</strong> <strong>the</strong> watch<br />

was looking on without a defined monitoring role.<br />

However, he had plotted a position on <strong>the</strong> chart,<br />

which showed <strong>the</strong> vessel to be north <strong>of</strong> <strong>the</strong> charted<br />

course line, and <strong>the</strong> Master had altered <strong>the</strong> vessel’s<br />

heading slightly in an attempt to partly compensate.<br />

Before <strong>the</strong> vessel had moved far towards her track,<br />

<strong>the</strong> Master decided to steer directly for <strong>the</strong> white<br />

light which indicated <strong>the</strong> centre <strong>of</strong> <strong>the</strong> bridge’s span.<br />

The vessel had recently been fitted with an<br />

electronic chart system following a similar accident<br />

on ano<strong>the</strong>r <strong>of</strong> <strong>the</strong> company’s ships. The Master<br />

could see <strong>the</strong> electronic chart display, but was not<br />

using it o<strong>the</strong>r than to give him a rough indication<br />

<strong>of</strong> her position. He had never received any formal<br />

training in <strong>the</strong> use <strong>of</strong> this equipment.<br />

As <strong>the</strong> vessel passed under <strong>the</strong> centre <strong>of</strong> <strong>the</strong> bridge,<br />

<strong>the</strong> Master used 10 degrees <strong>of</strong> port helm to bring<br />

her around 40 degrees to <strong>the</strong> required heading for<br />

passage. No allowance, mental or o<strong>the</strong>rwise, had<br />

been made for <strong>the</strong> vessel’s advance and, unsurprisingly,<br />

she grounded on <strong>the</strong> sou<strong>the</strong>rn edge <strong>of</strong> <strong>the</strong> channel.<br />

The vessel sustained significant hull damage. She was<br />

holed in one segregated ballast tank but, fortunately,<br />

<strong>the</strong>re was no pollution as a result <strong>of</strong> <strong>the</strong> incident.<br />

Observations:<br />

1. The MAIB has frequently heard it argued that it<br />

is unrealistic to expect coastal shipping to adopt<br />

<strong>the</strong> navigational practices that would normally be<br />

found on deep sea vessels, because <strong>of</strong> <strong>the</strong> nature<br />

<strong>of</strong> <strong>the</strong> trade and <strong>the</strong> size <strong>of</strong> crews. Owners and<br />

Masters must ensure that <strong>the</strong>y do not use this<br />

argument to justify bad practice and complacency.<br />

2. The wheelhouse was well manned with qualified<br />

personnel, but <strong>the</strong> team was not used effectively<br />

to ensure <strong>the</strong> vessel’s safe passage. In this case,<br />

a better arrangement would have been for <strong>the</strong><br />

seaman to have steered <strong>the</strong> vessel while <strong>the</strong><br />

OOW plotted positions and <strong>the</strong> Master oversaw<br />

<strong>the</strong> whole safe operation.<br />

3. Passage planning was ineffective. A planned track<br />

that allowed <strong>the</strong> vessel to alter course and steady<br />

up on <strong>the</strong> new heading well before <strong>the</strong> entrance<br />

to <strong>the</strong> channel would have ensured this accident<br />

was avoided. Reciprocal courses were chosen<br />

for expediency, without consideration <strong>of</strong> this and<br />

possibly o<strong>the</strong>r factors. The use <strong>of</strong> parallel indexing<br />

techniques would have helped to ensure <strong>the</strong><br />

vessel was on, and maintaining, <strong>the</strong> correct track.<br />

4. Some <strong>of</strong> <strong>the</strong>se lessons had been discovered by<br />

<strong>the</strong> company as a result <strong>of</strong> a very similar accident<br />

a few months previously. However, <strong>the</strong> lessons<br />

had not been effectively communicated to this<br />

vessel or her Master. It is an unfortunate truth<br />

that accidents are a key source <strong>of</strong> useful safety<br />

advice, and every effort should be taken to learn<br />

and promulgate <strong>the</strong> lessons so that recurrence<br />

can be avoided”.<br />

Source <strong>of</strong> information - Marine Accident<br />

Investigation Branch (MAIB) safety digest No1/2007<br />

- http://www.maib.gov.uk/publications/safety_<br />

digests/2007/safety_digest_1_2007.cfm<br />

Root Cause:<br />

Insufficient navigation procedures.<br />

Issue Date: 18/04/07<br />

Case No. 12480<br />

66 67


Navigation<br />

Insufficient Ballast Causes Loss <strong>of</strong> Control While Berthing<br />

The Incident:<br />

This incident involved damage to a loading arm<br />

at a small oil jetty. The oil jetty in question was<br />

specifically designed for small vessels and is typical <strong>of</strong><br />

many in <strong>the</strong> region. The berth consisted <strong>of</strong> a central<br />

section containing <strong>the</strong> loading arms on ei<strong>the</strong>r side<br />

<strong>of</strong> which was a mooring dolphin connected to <strong>the</strong><br />

berth by walkways.<br />

The incident occurred as <strong>the</strong> tanker was<br />

manoeuvring alongside <strong>the</strong> berth. The tanker was<br />

berthing in a light condition without tug assistance.<br />

The forward draft was only 0.6 metres. The wind<br />

was blowing onto <strong>the</strong> berth as <strong>the</strong> Master made<br />

his approach into <strong>the</strong> current. As he stopped<br />

his vessel parallel to <strong>the</strong> berth, <strong>the</strong> high windage<br />

forward caused <strong>the</strong> bows to fall <strong>of</strong>f. The bow <strong>of</strong><br />

<strong>the</strong> vessel entered <strong>the</strong> space between <strong>the</strong> dolphin<br />

and <strong>the</strong> berth, coming to rest with <strong>the</strong> vessel’s bow<br />

in contact with <strong>the</strong> central section. To extricate<br />

himself <strong>the</strong> Master put his engines astern and in <strong>the</strong><br />

process <strong>the</strong> fo’c’sle railing caught <strong>the</strong> end loading<br />

arm, severely damaging it.<br />

Observations:<br />

Cargo loading arms on small jetties are particularly<br />

susceptible to damage by ships as <strong>the</strong>y are usually<br />

mounted close to <strong>the</strong> edge <strong>of</strong> <strong>the</strong> berth. This<br />

incident could have been avoided by ballasting <strong>the</strong><br />

forward end <strong>of</strong> <strong>the</strong> tanker to reduce <strong>the</strong> windage<br />

and increase <strong>the</strong> grip <strong>of</strong> <strong>the</strong> forefoot in <strong>the</strong> water.<br />

If operational considerations made this undesirable<br />

<strong>the</strong>n <strong>the</strong> assistance <strong>of</strong> a tug should have been sought.<br />

Root Cause:<br />

Inadequate operational considerations.<br />

Financial Cost:<br />

The cost <strong>of</strong> repairs to <strong>the</strong> loading arm exceeded<br />

US$100,000.<br />

Issue Date: 01/01/02<br />

Case No. 20614<br />

68 69


Navigation<br />

Know Your Ship<br />

The Incident:<br />

This accident occurred as a 3,000 GRT tanker attempted to berth alongside an oil jetty in<br />

marginal conditions without tug assistance. The vessel was trying to berth for <strong>the</strong> fourth<br />

time, <strong>the</strong> three prior approaches had to be aborted because <strong>of</strong> <strong>the</strong> effects <strong>of</strong> wind and<br />

current. On this occasion <strong>the</strong> approach to <strong>the</strong> berth was going well with <strong>the</strong> vessel due<br />

to dock portside to. As she approached <strong>the</strong> berth <strong>the</strong> helm was put hard astarboard,<br />

<strong>the</strong> forward spring sent way and <strong>the</strong> engines put astern. The vessel did not respond to<br />

<strong>the</strong> helm and <strong>the</strong> ship’s port bow landed heavily on <strong>the</strong> jetty, damaging <strong>the</strong> concrete<br />

structure and <strong>the</strong> fendering system.<br />

Observations:<br />

The Club appointed a surveyor to investigate <strong>the</strong> occurrence. The surveyor discovered<br />

that <strong>the</strong> vessel was fitted with a lefthanded propeller. The transverse thrust generated<br />

when a lefthanded propeller is run astern tends to cant <strong>the</strong> bow to port ra<strong>the</strong>r than<br />

to starboard as is <strong>the</strong> case with <strong>the</strong> more usual righthanded propeller. It is likely that in<br />

<strong>the</strong> marginal circumstances <strong>the</strong> transverse thrust generated when <strong>the</strong> engines were put<br />

astern was sufficient to counteract <strong>the</strong> effect <strong>of</strong> putting <strong>the</strong> helm hard astarboard.<br />

Root Cause:<br />

Crew unfamiliar with <strong>the</strong>ir vessel.<br />

Financial Cost:<br />

The cost <strong>of</strong> repairs to <strong>the</strong> jetty including survey costs totalled US$15,500.<br />

Issue Date: 01/01/02<br />

Case No. 22217<br />

70 71


Navigation<br />

Good Seamanship is Still as Important as Ever<br />

The Incident:<br />

This case involves damage to a deep sea vessel while unberthing a bunkering barge.<br />

The deep sea vessel was lying head to tide which was running at approximately 1 knot.<br />

The wind was blowing on her starboard bow at about force 3 to 4. The bunker barge<br />

was secured alongside her starboard side. After delivering <strong>the</strong> fuel <strong>the</strong> Captain <strong>of</strong> <strong>the</strong><br />

bunker barge gave instructions to single up to one headline and <strong>the</strong> forward spring. By<br />

steaming gently ahead into <strong>the</strong> spring and heaving on <strong>the</strong> headline <strong>the</strong> stern was sprung<br />

<strong>of</strong>f to an angle <strong>of</strong> about 30°. The lines were let go and <strong>the</strong> engines put slow astern. With<br />

<strong>the</strong> bunker barge in a light condition <strong>the</strong> bows were high in <strong>the</strong> water and as she moved<br />

away <strong>the</strong> wind caught <strong>the</strong> bows, swinging <strong>the</strong>m towards <strong>the</strong> deep sea vessel. The Captain<br />

<strong>of</strong> <strong>the</strong> bunker barge stopped his engines in <strong>the</strong> hope <strong>of</strong> s<strong>of</strong>tening <strong>the</strong> contact, <strong>the</strong> wind<br />

however continued to push <strong>the</strong> vessel’s bows to leeward with increasing speed until she<br />

collided with <strong>the</strong> deep sea vessel, scraping down her side.<br />

Observations:<br />

In conditions such as <strong>the</strong>se it is essential that full<br />

account is taken <strong>of</strong> <strong>the</strong> effects <strong>of</strong> wind and tide.<br />

Bold and decisive action must be taken and full use<br />

made <strong>of</strong> engine and rudder. If <strong>the</strong> Captain <strong>of</strong> <strong>the</strong><br />

bunker barge had put his engines to full astern after<br />

springing his stern out it is quite possible that he<br />

would have gained sufficient stern way to carry his<br />

ship clear <strong>of</strong> <strong>the</strong> ocean going vessel before much<br />

damage was done. In stopping his engines he left his<br />

vessel at <strong>the</strong> mercy <strong>of</strong> <strong>the</strong> wind and rendered <strong>the</strong><br />

collision inevitable.<br />

With <strong>the</strong> prevailing wind and current <strong>the</strong> Master<br />

<strong>of</strong> <strong>the</strong> bunker barge should have let go forward<br />

and held onto his stern spring, steaming astern as<br />

necessary to spring <strong>the</strong> bow <strong>of</strong>f. The current on <strong>the</strong><br />

bow would have been sufficient to counteract <strong>the</strong><br />

effects <strong>of</strong> <strong>the</strong> wind and <strong>the</strong> transverse thrust from<br />

<strong>the</strong> propeller as she moved <strong>of</strong>f ahead would help lift<br />

<strong>the</strong> bunker barge’s stern clear <strong>of</strong> <strong>the</strong> deep sea vessel.<br />

Root Cause:<br />

Human error.<br />

Financial Cost:<br />

This owner was fortunate for although <strong>the</strong> damage<br />

to <strong>the</strong> deep sea vessel extended for some distance<br />

down its side <strong>the</strong> indentation was not deep enough<br />

to worry <strong>the</strong> class society and as a result a claim was<br />

not pursued.<br />

Issue Date: 01/01/02<br />

Case No. 22496<br />

72 73


Operations<br />

Luck has Staring Role in Preventing Pollution<br />

The Incident:<br />

A bunker tanker was engaged in delivering bunkers<br />

to an ocean going vessel. The transfer plan was to<br />

discharge numbers 2 and 5 tanks simultaneously<br />

using a separate pump on each tank but discharging<br />

into a common line. As <strong>the</strong> oil transfer commenced<br />

it was noted that <strong>the</strong> discharge pressure gauge<br />

on <strong>the</strong> pump connected to number 5 cargo tank<br />

showed no appreciable <strong>read</strong>ing. As <strong>the</strong>re was no<br />

improvement after a few minutes all pumping was<br />

stopped and <strong>the</strong> matter was investigated.<br />

The pump was found to be full <strong>of</strong> air which was bled<br />

out through <strong>the</strong> air cock valve. As <strong>the</strong> pumps were<br />

restarted number 5 cargo oil tank overflowed on<br />

to <strong>the</strong> deck. Both pumps were stopped, all valves<br />

closed. Fortunately <strong>the</strong> oil spill was contained on <strong>the</strong><br />

deck <strong>of</strong> <strong>the</strong> bunker barge.<br />

Observations:<br />

The problem with <strong>the</strong> cargo pump had allowed<br />

oil pumped from number 2 cargo tank into <strong>the</strong><br />

common discharge line to flow back into number 5<br />

cargo oil tank. This flow would have continued even<br />

after <strong>the</strong> pumps were stopped as gravity would have<br />

caused <strong>the</strong> oil in <strong>the</strong> discharge line to siphon back<br />

into <strong>the</strong> bunker tanker below. Had <strong>the</strong> vessel been<br />

fitted with high-level alarms it is likely that this spill<br />

could have been avoided. Adhering to good tanker<br />

practice by starting <strong>the</strong> discharge from one tank at<br />

a time and positively confirming that oil was flowing<br />

out <strong>of</strong> <strong>the</strong> tank before starting <strong>the</strong> next one would<br />

have done much to avoid <strong>the</strong> problem.<br />

Root Cause:<br />

Ship design failure.<br />

Financial Cost:<br />

In this instance although no oil reached <strong>the</strong> water,<br />

<strong>the</strong> company received a bill from <strong>the</strong> Port Authority<br />

for more than US$600. In addition to this <strong>the</strong> owner<br />

faced additional costs in disposing <strong>of</strong> <strong>the</strong> oil on deck<br />

and cleaning <strong>the</strong> vessel.<br />

Issue Date: 01/01/02<br />

Case No. 22382<br />

74 75


Operations<br />

Hose Bursts Under Pressure<br />

The Incident:<br />

In recent months, <strong>the</strong> Club has been involved in a<br />

large number <strong>of</strong> pollution incidents which have been<br />

caused by transfer hoses bursting during bunkering<br />

operations. The following is a typical example.<br />

The Member’s vessel was employed in <strong>the</strong> process <strong>of</strong><br />

transferring 600mt <strong>of</strong> heavy fuel oil into a receiving<br />

ship. She was tied up starboard side alongside and <strong>the</strong><br />

transfer was being effected by using one cargo pump<br />

and a 30 metre long 6 inch diameter cargo hose.<br />

The Bunker Requisition Form was agreed between<br />

both parties indicating a pumping rate <strong>of</strong> 200 mt/hr<br />

with a maximum manifold pressure <strong>of</strong> 2kg/cm2 . The<br />

transfer began at 0950.<br />

At 1125 a bang was heard and oil was seen leaking<br />

out <strong>of</strong> a section <strong>of</strong> <strong>the</strong> transfer hose lying on <strong>the</strong> deck<br />

<strong>of</strong> <strong>the</strong> Member’s vessel. Pumping operations were<br />

stopped and both crews implemented measures to<br />

reduce <strong>the</strong> spilling <strong>of</strong> oil into <strong>the</strong> harbour. After a<br />

short while <strong>the</strong> harbour authorities’ launch arrived<br />

and undertook clean up operations to minimise <strong>the</strong><br />

effects <strong>of</strong> <strong>the</strong> oil spill.<br />

Observations:<br />

At <strong>the</strong> time <strong>of</strong> <strong>the</strong> incident, <strong>the</strong> receiving vessel had<br />

40 metric tonnes <strong>of</strong> <strong>the</strong> stem left to receive and <strong>the</strong><br />

cause <strong>of</strong> <strong>the</strong> hose bursting was considered to have<br />

been over pressurisation when <strong>the</strong> tank valves were<br />

possibly closed in as <strong>the</strong> receiving vessel’s tanks<br />

were being topped <strong>of</strong>f.<br />

However investigations carried out by <strong>the</strong> Club<br />

surveyor showed <strong>the</strong> condition <strong>of</strong> <strong>the</strong> cargo hoses<br />

to be poor. Several splits were noted in <strong>the</strong> outer<br />

covering. The point at which <strong>the</strong> hose burst was<br />

located within a section <strong>of</strong> hose that had been<br />

parcelled to give protection against chaffing so any<br />

deformations or damage to this section would not<br />

be <strong>read</strong>ily apparent. What <strong>the</strong> condition <strong>of</strong> <strong>the</strong> hose<br />

played in <strong>the</strong> incident is unknown.<br />

Notwithstanding any regulations, if hoses (or any<br />

equipment) exhibit defects <strong>the</strong>y should be tested<br />

immediately and measures taken to replace <strong>the</strong>m.<br />

Satisfactory test results only show <strong>the</strong> hose is in an<br />

acceptable condition at <strong>the</strong> time <strong>of</strong> testing. It does<br />

not provide a guarantee <strong>the</strong> hose’s condition will<br />

remain satisfactory when subjected to fur<strong>the</strong>r wear<br />

and tear. It should also be borne in mind that bunker<br />

vessels, by <strong>the</strong> very nature <strong>of</strong> <strong>the</strong>ir work, place<br />

a greater burden on <strong>the</strong>ir equipment than o<strong>the</strong>r<br />

tanker types and <strong>the</strong>refore <strong>the</strong>ir equipment should<br />

be examined on a more frequent basis.<br />

Root Cause:<br />

Inadequate maintenance programme.<br />

The Member had complied with <strong>the</strong> local authority<br />

requirements for <strong>the</strong> testing <strong>of</strong> <strong>the</strong> hose which<br />

required a pressure test to be carried out twice<br />

every five years with a maximum interval between<br />

tests <strong>of</strong> three years. The regulations do not make<br />

any reference to <strong>the</strong> general condition <strong>of</strong> <strong>the</strong> hose.<br />

Because <strong>of</strong> <strong>the</strong> poor condition, <strong>the</strong> Club only agreed<br />

to provide security when it was proven that <strong>the</strong><br />

local regulations had been complied with.<br />

Financial Cost:<br />

The Club put up security for US$40,000 to cover<br />

<strong>the</strong> port authority costs.<br />

Issue Date: 01/01/02 Case No. 39324<br />

76 77


Pollution<br />

Pollution<br />

Good Record Keeping Wins <strong>the</strong> Day<br />

New Ship, New Crew – Same Old Problems<br />

The Incident:<br />

This incident occurred during bunkering operations in<br />

sheltered waters. The bunker tanker was delivering<br />

gas oil to an ocean going vessel when <strong>the</strong> gaskets on<br />

<strong>the</strong> strainer box on board <strong>the</strong> deep sea vessel burst,<br />

with <strong>the</strong> result that gas oil spilt over <strong>the</strong> deck and into<br />

<strong>the</strong> sea. The deep sea vessel was fined by <strong>the</strong> Port<br />

Authority and sought indemnity for this and <strong>the</strong> cost<br />

<strong>of</strong> cleaning <strong>the</strong>ir vessel. The deep sea vessel alleged<br />

that <strong>the</strong> bunker barge had greatly exceeded <strong>the</strong><br />

agreed loading rate.<br />

Fortunately <strong>the</strong> personnel on board <strong>the</strong> bunker barge<br />

had kept proper records <strong>of</strong> <strong>the</strong> transfer operation<br />

and we were able to show quite conclusively that <strong>the</strong><br />

agreed loading rate had never been exceeded. It is<br />

likely that <strong>the</strong> increase in pressure which caused <strong>the</strong><br />

packing to burst was <strong>the</strong> result <strong>of</strong> valves being closed<br />

on <strong>the</strong> deep sea vessel.<br />

Observations:<br />

This case highlights <strong>the</strong> need to keep proper records<br />

during oil transfer operations. Had <strong>the</strong> barge’s crew<br />

not been diligent in recording events, taking regular<br />

tank soundings and noting pump speeds, we would<br />

have found it much more difficult to avoid liability.<br />

Root Cause:<br />

Inadequate maintenance programme.<br />

Financial Cost:<br />

Nil.<br />

Issue Date: 01/01/02<br />

Case No. 22494<br />

The Incident:<br />

This minor oil spill occurred during a bunkering<br />

operation in sheltered waters. The bunker barge was<br />

supplying fuel to <strong>the</strong> deep sea vessel from tanks 2 and<br />

4. As <strong>the</strong> bunkering operation neared completion<br />

tank 5, containing a different grade <strong>of</strong> oil, overflowed<br />

on to <strong>the</strong> deck. The <strong>of</strong>ficer in charge <strong>of</strong> <strong>the</strong> cargo<br />

operation promptly stopped <strong>the</strong> bunkering operation.<br />

The spill was largely contained within <strong>the</strong> vessel’s oil<br />

spill coaming where plugged scuppers prevented <strong>the</strong><br />

accumulated oil from flowing over <strong>the</strong> ship’s side.<br />

Never<strong>the</strong>less <strong>the</strong> vessel was fined by <strong>the</strong> harbour<br />

authorities.<br />

The cargo <strong>of</strong> 380 CST oil in number 5 tank was<br />

contaminated by approximately 50 tons <strong>of</strong> 180 CST<br />

oil bringing <strong>the</strong> average viscosity down to 300 CST.<br />

No claim was made by <strong>the</strong> charterers who were able<br />

to dispose <strong>of</strong> this oil with no loss <strong>of</strong> value. Surprisingly<br />

no claim for short delivery <strong>of</strong> bunkers was made by<br />

<strong>the</strong> deep sea vessel involved.<br />

Observations:<br />

The spill was caused by a crew member operating<br />

<strong>the</strong> wrong valves. This vessel had only joined <strong>the</strong><br />

fleet a week prior to <strong>the</strong> incident and <strong>the</strong> crew<br />

were unfamiliar with <strong>the</strong> vessel. The valves were not<br />

colour coded nor were <strong>the</strong>y clearly marked. The<br />

instructions given to <strong>the</strong> crewman were generic<br />

and did not specify precisely which valves should<br />

be operated. It is likely that this incident could<br />

have been avoided had <strong>the</strong> crew had more time to<br />

become familiar with <strong>the</strong> vessel, <strong>the</strong> valves been<br />

clearly marked and <strong>the</strong> crewman given precise<br />

instructions.<br />

Root Cause:<br />

Human error.<br />

Financial Cost:<br />

This Member was fortunate as <strong>the</strong> fine and costs<br />

incurred did not exceed US$6,000. It could have<br />

been much greater.<br />

Issue Date:<br />

Case No.<br />

78 79


Pollution<br />

High Loading Rate + Too Few Crew = Pollution<br />

The Incident:<br />

This incident involves an oil spill while loading a small<br />

bunker tanker. The bunker tanker had returned from<br />

supplying fuel to an ocean going vessel. It had oil<br />

remaining in numbers 2, 3 and 4 wing tanks. The plan<br />

was to load number 1 port and starboard first and<br />

<strong>the</strong>reafter top up 2, 3 and 4 wings, finishing in number<br />

4. An 8 inch hose was connected and although <strong>the</strong><br />

vessel was only due to lift 810 metric tons, <strong>the</strong> loading<br />

rate was agreed at 600 tons per hour. As number 2<br />

wings were being topped <strong>of</strong>f, <strong>the</strong> crew failed to shut<br />

<strong>the</strong> tank valves in time and oil overflowed onto <strong>the</strong><br />

deck and into <strong>the</strong> sea.<br />

Observations:<br />

Oil spills are most likely to occur when vessels are<br />

topping <strong>of</strong>f <strong>the</strong>ir tanks. Extreme caution should be<br />

exercised at this stage and adequate personnel need<br />

to be stationed on deck to ensure that <strong>the</strong>re are<br />

sufficient hands available to manipulate <strong>the</strong> valves as<br />

necessary. The loading rate should be reduced while<br />

tanks are being topped <strong>of</strong>f. This procedure should<br />

be agreed with terminal personnel in advance. This<br />

incident occurred while cargo was being loaded at<br />

<strong>the</strong> full 600 tons per hour and only one man was<br />

available to monitor <strong>the</strong> tank level and manipulate<br />

<strong>the</strong> valves. The spill could have been avoided if<br />

<strong>the</strong> loading rate had been reduced and additional<br />

personnel utilised.<br />

Root Cause:<br />

Insufficient operational procedures.<br />

Financial Cost:<br />

The cost <strong>of</strong> clean up operations and <strong>the</strong> fine<br />

imposed by <strong>the</strong> Port Authority brought <strong>the</strong> total<br />

value <strong>of</strong> this claim to almost US$9,000.<br />

Issue Date: 01/01/02<br />

Case No. 19809<br />

80 81


Tankers:<br />

Gas<br />

Miscellaneous<br />

Capsize at Sea<br />

The Incident:<br />

This case concerns <strong>the</strong> capsize and total loss <strong>of</strong><br />

a 690 ton gas tanker. The vessel was steaming<br />

between islands in <strong>the</strong> Philippines fully laden<br />

with LPG when she received a message from her<br />

charterers announcing a change <strong>of</strong> destination. On<br />

receipt <strong>of</strong> <strong>the</strong>se new orders to return to a port that<br />

<strong>the</strong>y had al<strong>read</strong>y passed, <strong>the</strong> helm was put hard to<br />

starboard while <strong>the</strong> vessel was proceeding at full<br />

speed. The vessel listed heavily into <strong>the</strong> turn and<br />

<strong>the</strong> list progressively increased until <strong>the</strong> result that<br />

<strong>the</strong> vessel capsized. Because <strong>of</strong> <strong>the</strong> buoyant nature<br />

<strong>of</strong> her cargo <strong>the</strong> tanker did not sink completely but<br />

came to rest floating vertically in <strong>the</strong> water with her<br />

fo’c’sle structure above <strong>the</strong> water level. Hull and<br />

machinery underwriters immediately declared <strong>the</strong><br />

vessel to be a total loss, leaving <strong>the</strong> owners with <strong>the</strong><br />

problem <strong>of</strong> disposing <strong>of</strong> <strong>the</strong> wreck. After a lengthy<br />

salvage operation <strong>the</strong> vessel was refloated with<br />

her cargo intact. Considerable difficulty was found<br />

in disposing <strong>of</strong> <strong>the</strong> vessel and her cargo because<br />

none <strong>of</strong> <strong>the</strong> major oil companies were prepared to<br />

let a damaged LPG tanker berth in <strong>the</strong>ir terminal.<br />

The vessel and her cargo were ultimately sold to a<br />

salvage buyer for a fraction <strong>of</strong> <strong>the</strong>ir true value.<br />

Observations:<br />

The most likely cause <strong>of</strong> <strong>the</strong> casualty is a reduction<br />

in stability caused by free surface effect <strong>of</strong> liquids on<br />

board <strong>the</strong> vessel. Subsequent investigation revealed<br />

that <strong>the</strong> vessel was having problems with leakage. In<br />

this case <strong>the</strong>re was no formal contract between <strong>the</strong><br />

vessel’s owners and <strong>the</strong> repair yard. The question<br />

<strong>of</strong> responsibility for ensuring that <strong>the</strong> vessel was<br />

fit for hot work to be carried out was not clear.<br />

We would recommend that owners ensure this<br />

subject is addressed in every repair contract and<br />

that where possible <strong>the</strong> shipyard be given this<br />

responsibility.<br />

Root Cause:<br />

Poor maintenance programme.<br />

Financial Cost:<br />

The cost <strong>of</strong> refloating and disposing <strong>of</strong> <strong>the</strong> ship and<br />

cargo exceeded US$820,000.<br />

Issue Date: 01/01/02<br />

Case No. 20524<br />

82 83


Section 3<br />

Fishing Vessels<br />

85


Fishing Vessels<br />

Personal Injury/Illness<br />

Although Out <strong>of</strong> Sight it should be Kept in Mind<br />

The Incident:<br />

This incident took place on a beam trawler and a<br />

resulted in a non-fatal injury to a crew member.<br />

During a late evening in fine wea<strong>the</strong>r conditions <strong>the</strong><br />

fishing gear was being hauled. Four crew members<br />

were positioned on <strong>the</strong> top deck waiting to attend<br />

to <strong>the</strong> beams as <strong>the</strong>y came on board.<br />

As <strong>the</strong>y cleared <strong>the</strong> water, with <strong>the</strong> derrick standing<br />

vertically, <strong>the</strong> starboard topping wire parted. It came<br />

down with some force and struck a deckhand. It was<br />

later found he had sustained a fracture to an ankle<br />

and <strong>the</strong>re is some doubt as to his ability to return to<br />

a life in <strong>the</strong> fishing industry.<br />

Observations:<br />

Unfortunately <strong>the</strong> head block was lost overboard<br />

during <strong>the</strong> incident and it is a matter <strong>of</strong> conjecture<br />

whe<strong>the</strong>r <strong>the</strong> block failed causing <strong>the</strong> wire to part or<br />

whe<strong>the</strong>r <strong>the</strong> wire parted causing <strong>the</strong> block to fail.<br />

The wire was reportedly only seven months old.<br />

The rigging arrangement for <strong>the</strong> derrick was such<br />

that <strong>the</strong> topping wire only moved between 150mm<br />

to 200mm when raising or lowering <strong>the</strong> booms,<br />

thus <strong>the</strong> length which rounded <strong>the</strong> block had been<br />

hidden from view since it was reeved.<br />

Although <strong>the</strong> skipper had in place a thorough greasing<br />

routine for <strong>the</strong> wire and blocks, <strong>the</strong> only way to<br />

examine this small section <strong>of</strong> wire was to land <strong>the</strong><br />

derrick on to a quay, which had never been carried out.<br />

Both ends <strong>of</strong> <strong>the</strong> wire were noted to be frayed<br />

which indicates that it was likely <strong>the</strong> wire had parted,<br />

destroying <strong>the</strong> block.<br />

Root Cause:<br />

Inadequate maintenance programmes.<br />

Financial Cost:<br />

The cost <strong>of</strong> this claim is US$80,000.<br />

Issue Date: 05/07/06<br />

Case No. 38878<br />

It is not uncommon for static sections <strong>of</strong> wire to<br />

corrode significantly in a short period <strong>of</strong> time and<br />

Members and Skippers should ensure that such<br />

sections <strong>of</strong> wire are frequently examined and greased.<br />

86 87


Personal Injury/Illness<br />

The Importance <strong>of</strong> Good Risk Assessment Highlighted<br />

The Incident:<br />

The accident occurred when a<br />

crew member was attending <strong>the</strong><br />

gilsen derrick guys as a catch was<br />

being brought on board. Three<br />

turns had been taken round <strong>the</strong><br />

port warping drum <strong>of</strong> <strong>the</strong> trawl<br />

winch. The drum was rotating at a<br />

steady speed as <strong>the</strong> controls had<br />

been locked in position by <strong>the</strong><br />

use <strong>of</strong> a piece <strong>of</strong> wood wedged<br />

between <strong>the</strong> control lever and<br />

frame. The crew member was<br />

tailing <strong>the</strong> rope behind <strong>the</strong> drum,<br />

surging or heaving as required<br />

when <strong>the</strong> fingers <strong>of</strong> his left hand<br />

became caught between <strong>the</strong> rope<br />

turns and <strong>the</strong> drum. There were<br />

no witnesses to <strong>the</strong> accident but<br />

it seems likely that a riding turn<br />

developed on <strong>the</strong> drum and<br />

instead <strong>of</strong> letting <strong>the</strong> rope go and<br />

stopping <strong>the</strong> winch by pulling on a<br />

small rope attached to <strong>the</strong> piece<br />

<strong>of</strong> wood, <strong>the</strong> crewman tried to<br />

clear <strong>the</strong> guy while <strong>the</strong> machinery<br />

was still rotating. Despite medical<br />

intervention he lost <strong>the</strong> tips to<br />

three fingers.<br />

Observations:<br />

There were two contributing factors to this incident.<br />

Firstly, <strong>the</strong> crew member was very inexperienced<br />

in working on a fishing vessel although <strong>the</strong> task he<br />

was involved in was not an unusual one in terms <strong>of</strong><br />

seamanship. However it appears he tried to clear <strong>the</strong><br />

riding turn whilst <strong>the</strong> winch was rotating. Secondly,<br />

despite two o<strong>the</strong>r crew members being present on<br />

deck, no one was designated to operate <strong>the</strong> winch<br />

which was left in <strong>the</strong> hauling mode by means <strong>of</strong><br />

a makeshift modification. The crew member had<br />

allegedly been told to stop <strong>the</strong> winch in <strong>the</strong> event<br />

<strong>of</strong> any problems, but failed to do so. Had a winch<br />

operator been present, stopping <strong>the</strong> winch would<br />

have been easily achieved and <strong>the</strong> accident avoided.<br />

Indeed he should have been better supervised in<br />

view <strong>of</strong> his relevant inexperience.<br />

Root Cause:<br />

Inadequate operational practices.<br />

Financial Cost:<br />

The claim was settled for US$117,000.<br />

Issue Date:<br />

Case No.<br />

88 89


Personal Injury/Illness<br />

No Excuse for Reduced Maintenance Regimes<br />

The Incident:<br />

A Skipper was killed and two women injured when <strong>the</strong> starboard<br />

derrick, which had been topped up to its fully raised position, suddenly<br />

fell down on <strong>the</strong>m as <strong>the</strong>y stood on <strong>the</strong> quayside next to <strong>the</strong> vessel. It<br />

transpired that <strong>the</strong> eye <strong>of</strong> <strong>the</strong> starboard topping lift block had failed and<br />

subsequent investigation attributed its failure to <strong>the</strong> sudden propagation<br />

<strong>of</strong> a brittle fracture from a pre-existing manufacturing defect.<br />

The claims eventually came to trial and <strong>the</strong> claimants’ primary case<br />

was that <strong>the</strong> Members had failed to put in place an adequate system <strong>of</strong><br />

inspection and maintenance <strong>of</strong> <strong>the</strong> fishing gear. The Members asserted<br />

that <strong>the</strong>ir system <strong>of</strong> inspection and maintenance was in accordance<br />

with all applicable regulations and matched prevailing standards within<br />

<strong>the</strong> industry. They contended that, in any event, any shortcomings in<br />

maintenance were not causative <strong>of</strong> <strong>the</strong> loss since <strong>the</strong> block failed as a<br />

result <strong>of</strong> a latent manufacturing defect which could not have been, and<br />

was not, detected by <strong>the</strong> exercise <strong>of</strong> reasonable diligence.<br />

Observations:<br />

The judge found that <strong>the</strong><br />

Members’ practice <strong>of</strong> leaving<br />

all aspects <strong>of</strong> maintenance and<br />

safety to <strong>the</strong> crew was indeed in<br />

accordance with industry practice<br />

but that it was “simply naive to<br />

assert that good practice cannot<br />

call for more than compliance with<br />

<strong>the</strong> relative statutory regime”. He<br />

said that <strong>the</strong>re should have been<br />

a system <strong>of</strong> planned preventative<br />

inspection and maintenance<br />

<strong>of</strong> all lifting gear blocks every<br />

six months by a person with<br />

sufficient practical experience and<br />

<strong>the</strong>oretical knowledge. He saw<br />

no reason to distinguish between<br />

<strong>the</strong> regime <strong>of</strong> inspection required<br />

<strong>of</strong> cargo ships’ derricks and lifting<br />

gear on a fishing vessel. As to<br />

causation, <strong>the</strong> metallurgist experts<br />

for both parties were agreed that<br />

<strong>the</strong> developing defect in <strong>the</strong> block<br />

would not have been detected<br />

during a routine inspection<br />

and overhaul <strong>of</strong> <strong>the</strong> vessel’s<br />

equipment. However, <strong>the</strong> judge<br />

found that <strong>the</strong> crew were wholly<br />

untrained to recognise degrees <strong>of</strong><br />

wear or corrosion in <strong>the</strong> vessel’s<br />

equipment, that <strong>the</strong>re were o<strong>the</strong>r<br />

defects in <strong>the</strong> block which were<br />

patent and that a proper system<br />

<strong>of</strong> maintenance would have<br />

required <strong>the</strong> block to have been<br />

tested with <strong>the</strong> specific intention<br />

<strong>of</strong> identifying cracks.<br />

Members’ attention is drawn to our<br />

Lookout article 06 <strong>of</strong> 2004 where<br />

a maintenance regime for lifting<br />

tackle on fishing vessels based on<br />

MCA requirements is detailed.<br />

Root Cause:<br />

Inadequate shore maintenance<br />

procedure.<br />

Financial Cost:<br />

The Members paid substantial<br />

compensation to <strong>the</strong> Skipper’s<br />

widow and <strong>the</strong> two injured<br />

women. With <strong>the</strong> associated<br />

costs, <strong>the</strong> total value <strong>of</strong> this claim<br />

was in excess <strong>of</strong> US$2,155,000.<br />

Issue Date: 27/10/05<br />

Case No. 32365<br />

90 91


Personal Injury/Illness<br />

Death from Hydrogen Sulphide Poisoning<br />

The Incident:<br />

The vessel involved in this case<br />

was a 97 foot fishing vessel<br />

which had left her home waters<br />

in Alaska to fish for albacore<br />

tuna in <strong>the</strong> South Pacific. The<br />

vessel experienced problems<br />

with her refrigeration system<br />

which culminated in a full catch<br />

<strong>of</strong> approximately 15 tons <strong>of</strong> tuna<br />

being rejected as being unfit for<br />

human consumption.<br />

The skipper decided to cut his<br />

losses and return to Alaska,<br />

hoping to sell <strong>the</strong> catch as bait. It<br />

appears however that problems<br />

with <strong>the</strong> refrigeration system<br />

worsened and six days into <strong>the</strong><br />

voyage <strong>the</strong> refrigeration system<br />

was shut down altoge<strong>the</strong>r. The<br />

three man crew started to dump<br />

<strong>the</strong> fish over <strong>the</strong> side. Nine tons<br />

were disposed <strong>of</strong> before <strong>the</strong> smell<br />

<strong>of</strong> decomposing fish became<br />

overwhelming. The Captain<br />

decided to partially flood <strong>the</strong><br />

fish hold in <strong>the</strong> hope that <strong>the</strong> fish<br />

would rapidly break down into<br />

a soup which could be pumped<br />

overboard. After leaving <strong>the</strong> fish<br />

to decompose for a few days <strong>the</strong>y<br />

commenced pumping <strong>the</strong><br />

mixture but after a short period<br />

<strong>the</strong> strum box clogged with fish<br />

remains. The skipper descended<br />

<strong>the</strong> ladder into <strong>the</strong> fish hold to<br />

try to clear <strong>the</strong> pump. Within<br />

seconds he was overcome by<br />

hydrogen sulphide gas given <strong>of</strong>f<br />

by <strong>the</strong> rotting fish. The engineer<br />

attempted to rescue him and also<br />

succumbed. The one remaining<br />

crew member was unable to<br />

operate <strong>the</strong> radio to summon<br />

assistance and steamed in <strong>the</strong><br />

general direction <strong>of</strong> Honolulu until<br />

<strong>the</strong> boat’s generator ran out <strong>of</strong><br />

fuel and <strong>the</strong> electrical supplies to<br />

<strong>the</strong> steering gear failed. At that<br />

point he abandoned ship and set<br />

<strong>of</strong>f <strong>the</strong> EPIRB. He was rescued by<br />

<strong>the</strong> US Coastguard.<br />

Observations:<br />

This unusual incident highlights <strong>the</strong> dangers <strong>of</strong><br />

entering enclosed spaces. The atmosphere <strong>of</strong><br />

any enclosed or confined space which is not<br />

continuously and adequately ventilated may be<br />

deficient in oxygen or contain flammable/toxic<br />

fumes, gases or vapours. Crews should be made<br />

aware <strong>of</strong> <strong>the</strong> dangers and instructed not to enter<br />

enclosed spaces if <strong>the</strong>re is any reason to suspect that<br />

<strong>the</strong> atmosphere may be hazardous. On no account<br />

should rescue attempts be made without wearing<br />

breathing apparatus, a rescue harness and lifeline.<br />

In this case <strong>the</strong> crew were aware that <strong>the</strong> fish were<br />

rotting but were ignorant <strong>of</strong> <strong>the</strong> effects <strong>of</strong> <strong>the</strong> gas<br />

being given <strong>of</strong>f. The vessel carried no breathing<br />

apparatus, gas testing equipment or oxygen<br />

analysing equipment. This accident could have been<br />

avoided if <strong>the</strong> crew had been aware <strong>of</strong> <strong>the</strong> risks <strong>of</strong><br />

enclosed spaces and not attempted to deal with <strong>the</strong><br />

problem without proper equipment.<br />

Root Cause:<br />

Inadequate enclosed space entry procedures.<br />

Financial Cost:<br />

The cost <strong>of</strong> this claim exceeded US$650,000.<br />

Issue Date:01/01/02<br />

Case No. 14132<br />

The survivor claimed damages for<br />

post traumatic stress disorder.<br />

Claims were made by <strong>the</strong> families<br />

<strong>of</strong> <strong>the</strong> two dead crew.<br />

92 93


Personal Injury/Illness<br />

Makeshift Platform Results in a Severe Injury<br />

The Incident:<br />

The stern trawler involved in this<br />

incident was lying in a port in<br />

Alaska undergoing repair work.<br />

The vessel’s trawl deck area<br />

was equipped with two cranes,<br />

one located at <strong>the</strong> forward<br />

starboard corner and <strong>the</strong><br />

o<strong>the</strong>r portside aft. Repair work<br />

was being carried out on <strong>the</strong><br />

starboard forward crane by<br />

independent contractors.<br />

The work involved cutting out<br />

and replacing a portion <strong>of</strong> a<br />

starboard forward crane. The<br />

after port crane was used to<br />

assist in <strong>the</strong> repair work.<br />

The contractors could not reach <strong>the</strong> damaged portion <strong>of</strong> <strong>the</strong> crane<br />

from deck level. The contractors brought a large piece <strong>of</strong> plywood<br />

on board, placed it on top <strong>of</strong> <strong>the</strong> starboard trawl winch, which was<br />

conveniently situated just aft <strong>of</strong> and adjacent to <strong>the</strong> crane. At some<br />

point during <strong>the</strong> repair work it became evident to <strong>the</strong> contractors<br />

that as <strong>the</strong>y moved about on <strong>the</strong> plywood sheet it pressed through<br />

<strong>the</strong> control ears activating <strong>the</strong> winch. The contractors approached <strong>the</strong><br />

ship’s crew to ask whe<strong>the</strong>r it would be possible to turn <strong>the</strong> hydraulic<br />

power supply to <strong>the</strong> winch <strong>of</strong>f and <strong>the</strong> ship’s crew advised that it was<br />

possible but as <strong>the</strong> deck cranes and trawl winches were operated from<br />

<strong>the</strong> same hydraulic supply, <strong>the</strong> contractors would lose <strong>the</strong> use <strong>of</strong> <strong>the</strong><br />

aft port crane. The contractors however needed power to <strong>the</strong> crane<br />

and asked that <strong>the</strong> hydraulic power be left on. Not long afterwards <strong>the</strong><br />

trawl winch was accidentally activated, trapping <strong>the</strong> foot <strong>of</strong> one <strong>of</strong> <strong>the</strong><br />

contractors’ workmen. The injuries were so severe that <strong>the</strong> workman<br />

lost <strong>the</strong> big and first toe on his left foot, which disabled him to <strong>the</strong><br />

extent that he was unable to continue with his previous occupation.<br />

Observations:<br />

This incident highlights <strong>the</strong> dangers <strong>of</strong> makeshift<br />

working platforms. This incident could have been<br />

avoided if <strong>the</strong> had erected a proper scaffolding<br />

around <strong>the</strong> crane to provide a safe platform for<br />

his men to work from. In this case despite <strong>the</strong><br />

contractor and his employees being fully aware that<br />

<strong>the</strong> movement <strong>of</strong> <strong>the</strong> plywood sheet was causing<br />

<strong>the</strong> winch to operate unexpectedly, <strong>the</strong>y took<br />

no steps to replace <strong>the</strong> plywood with a proper<br />

structure or take any steps to guard <strong>the</strong> controls.<br />

Fur<strong>the</strong>rmore <strong>the</strong> contractor’s men were still using<br />

<strong>the</strong> winch as a stepping stone to reach parts <strong>of</strong> <strong>the</strong><br />

crane knowing that it was liable to operate without<br />

warning.<br />

Root Cause:<br />

Failure <strong>of</strong> 3rd party working practices.<br />

Issue Date: 01/01/02<br />

Case No. 21949<br />

94 95


Personal Injury/Illness<br />

Importance <strong>of</strong> a Safe Means <strong>of</strong> Access<br />

The Incident:<br />

This incident occurred in harbour at <strong>the</strong> end <strong>of</strong><br />

<strong>the</strong> fishing season. The vessel was being laid up for<br />

some months and <strong>the</strong> crew had been removing<br />

<strong>the</strong>ir belongings from <strong>the</strong> vessel dock. No proper<br />

gangway had been rigged and <strong>the</strong> only access to <strong>the</strong><br />

vessel was by way <strong>of</strong> a jacob’s ladder tied to <strong>the</strong> top<br />

railing on <strong>the</strong> starboard side <strong>of</strong> <strong>the</strong> pilot house deck.<br />

As a crew member was clambering over <strong>the</strong> top <strong>of</strong><br />

<strong>the</strong> railing he lost his balance and fell approximately<br />

12 feet to <strong>the</strong> dock injuring himself.<br />

The crew member suffered a severely broken<br />

wrist which required <strong>the</strong> insertion <strong>of</strong> metal pins.<br />

He was also found to have herniated a disc in<br />

his upper spine which gave rise to neck pain and<br />

dizziness. His doctors advised him that he should<br />

not return to work at sea.<br />

Observations:<br />

This is one <strong>of</strong> <strong>the</strong> many injuries that occur every year<br />

as a result <strong>of</strong> <strong>the</strong> use <strong>of</strong> unsafe means <strong>of</strong> access to<br />

and from vessels. Small vessels <strong>of</strong>ten have greater<br />

problems ensuring safe means <strong>of</strong> access than <strong>the</strong>ir<br />

larger sisters. In this particular case it would have<br />

been difficult if not impossible to rig a conventional<br />

gangway. The accident could however have been<br />

avoided if <strong>the</strong> jacob’s ladder had been rigged<br />

adjacent to an opening in <strong>the</strong> ship’s rail which would<br />

have avoided <strong>the</strong> crew member having to clamber<br />

precariously over <strong>the</strong> ship’s rail. Alternatively a rigid<br />

vertical ladder extending above <strong>the</strong> level <strong>of</strong> <strong>the</strong><br />

vessel’s rails could have been used.<br />

Root Cause:<br />

Inadequate means <strong>of</strong> access.<br />

Financial Cost:<br />

The total cost <strong>of</strong> this claim to <strong>the</strong><br />

Shipowner was $214,114.<br />

Issue Date: 01/01/02<br />

Case No. 21160<br />

96 97


Personal Injury/Illness<br />

It Pays to Plan Ahead<br />

Root Cause:<br />

It Pays to Plan Ahead.<br />

Financial Cost:<br />

The cost <strong>of</strong> this claim was in excess <strong>of</strong> US$117,000.<br />

Issue Date: 10/06/05<br />

Case No. 26039<br />

The Incident:<br />

The Member’s vessel was tied up alongside and a diving company was employed to<br />

undertake underwater cleaning <strong>of</strong> <strong>the</strong> hull. The diver reported to <strong>the</strong> Master and <strong>the</strong>n<br />

proceeded ashore where he changed into his diving gear and entered <strong>the</strong> water.<br />

The Master remained on deck to check work being carried out on a hydraulic winch.<br />

Soon after, <strong>the</strong> Chief Engineer approached <strong>the</strong> Master and requested permission to start<br />

<strong>the</strong> main engine so that electrical power could be provided to test <strong>the</strong> winch. The Master<br />

refused permission on account <strong>of</strong> <strong>the</strong> diver being in <strong>the</strong> water. Because <strong>of</strong> language<br />

difficulties <strong>the</strong> Chief Engineer had not understood what <strong>the</strong> Master had said<br />

and proceeded to <strong>the</strong> engine room to start <strong>the</strong> engine. The diver was working in <strong>the</strong><br />

vicinity <strong>of</strong> <strong>the</strong> propeller and when <strong>the</strong> engine started he was instantly killed.<br />

Observations:<br />

The main cause <strong>of</strong> this fatality was a failure <strong>of</strong> <strong>the</strong><br />

Master to ensure that all crew members were<br />

aware <strong>of</strong> <strong>the</strong> attendance <strong>of</strong> a diver whilst <strong>the</strong> vessel<br />

was alongside. By ensuring <strong>the</strong> facts were known<br />

beforehand, <strong>the</strong> possibility <strong>of</strong> <strong>the</strong> engines being used<br />

would not have arisen. Precautionary measures could<br />

have been taken including notices being placed on <strong>the</strong><br />

starting handles and telegraphs. This case also highlights<br />

<strong>the</strong> need to ensure facts are clearly understood<br />

when language difficulties may arise due to different<br />

nationalities being employed on board. It is important<br />

that all senior crew members have at least a good<br />

working knowledge <strong>of</strong> one common language and can<br />

communicate effectively with <strong>the</strong>ir department staff.<br />

98 99


Personal Injury/Illness<br />

Heat <strong>of</strong> <strong>the</strong> Moment<br />

The Incident:<br />

The skipper <strong>of</strong> a fishing vessel was leaning into an ice<br />

box when <strong>the</strong> lid, weighing half a ton, fell on to him.<br />

He suffered serious chest injuries and has a 10%<br />

body impairment as a result. The normal procedure<br />

for opening <strong>the</strong> lid was to raise it by means <strong>of</strong> a rope<br />

and tackle and <strong>the</strong>n insert a safety prop to hold it<br />

up.<br />

Observations:<br />

Unfortunately, on this occasion <strong>the</strong> skipper relied<br />

on <strong>the</strong> rope to hold <strong>the</strong> lid open and did not use<br />

<strong>the</strong> prop. The lead <strong>of</strong> <strong>the</strong> syn<strong>the</strong>tic rope was such<br />

that it came into contact with <strong>the</strong> funnel and <strong>the</strong><br />

heat had a degrading effect on it which caused <strong>the</strong><br />

rope to eventually part. Had <strong>the</strong> safety prop been<br />

used this accident would have been prevented. In<br />

all likelihood <strong>the</strong> rope would have parted when <strong>the</strong><br />

lid was being ei<strong>the</strong>r opened or closed and <strong>the</strong> crew<br />

standing clear.<br />

This incident highlights<br />

several facts:<br />

• Never rely on a wire or rope<br />

to hold a hatch lid open. A<br />

safety prop or securing pin<br />

should always be used to<br />

secure it in <strong>the</strong> open position.<br />

Such a restraint must enable<br />

clear access to <strong>the</strong> opening.<br />

• Wherever <strong>the</strong>re is a possibility<br />

<strong>of</strong> a syn<strong>the</strong>tic rope coming into<br />

contact with an indirect heat<br />

source, it should be replaced,<br />

preferably by a wire rope or at<br />

least by a natural fibre one.<br />

• Lifting arrangements should<br />

be subjected to a thorough<br />

visual examination at regular<br />

intervals. In this particular<br />

incident, it was reported that<br />

<strong>the</strong> damaged section <strong>of</strong> rope<br />

was not obvious to a casual<br />

observer.<br />

Root Cause:<br />

Human error.<br />

Issue Date: 03/02/06<br />

Case No. 37148<br />

100 101


Personal Injury/Illness<br />

When Applying First Aid – Ensure you Know What you are Doing<br />

The Incident:<br />

This claim involved a Vietnamese<br />

fisherman who, due to <strong>the</strong> medical<br />

treatment he received on board,<br />

had his lower leg amputated.<br />

Whilst fishing, a trawl wire<br />

became entangled around <strong>the</strong><br />

propeller. During efforts to free<br />

<strong>the</strong> wire, <strong>the</strong> crewman became<br />

trapped between <strong>the</strong> wire and<br />

bulwark. As a result he suffered a<br />

fracture to his right tibia, injuries<br />

to his pelvis and serious bruising<br />

and abrasions.<br />

Shortly after <strong>the</strong> accident, <strong>the</strong><br />

victim was transferred to ano<strong>the</strong>r<br />

larger fishing vessel which was<br />

proceeding to <strong>the</strong> nearest port.<br />

Once this vessel was within range,<br />

<strong>the</strong> ship’s helicopter was used<br />

to transfer him to <strong>the</strong> nearest<br />

island with medical facilities. The<br />

medical staff at <strong>the</strong> hospital did<br />

what <strong>the</strong>y could for <strong>the</strong> fisherman<br />

but decided he needed more<br />

specialist care and arrangements<br />

were made to airlift him to <strong>the</strong><br />

main land. Upon examination <strong>the</strong><br />

attending surgeon was left with<br />

no alternative but to amputate<br />

<strong>the</strong> right leg from <strong>the</strong> knee.<br />

Observations:<br />

As a result <strong>of</strong> <strong>the</strong> accident <strong>the</strong><br />

fisherman was bleeding heavily.<br />

The fracture to <strong>the</strong> tibia was open<br />

and a tourniquet was applied to<br />

stem <strong>the</strong> bleeding. This remained<br />

in place until he reached <strong>the</strong> first<br />

hospital 14 hours later.<br />

A tourniquet can be used to<br />

restrict blood flow to limbs, but<br />

<strong>the</strong> use <strong>of</strong> such a device has to<br />

be closely monitored because<br />

by restricting <strong>the</strong> blood flow<br />

<strong>the</strong> affected part <strong>of</strong> <strong>the</strong> body<br />

undergoes metabolic changes<br />

and unless blood flow is restored<br />

it slowly dies. In <strong>the</strong> case <strong>of</strong> <strong>the</strong><br />

fisherman, <strong>the</strong> lower leg muscles<br />

had died by <strong>the</strong> time he received<br />

pr<strong>of</strong>essional medical help and <strong>the</strong><br />

surgeon was left with no alternative<br />

but to remove <strong>the</strong> lower leg.<br />

A tourniquet is no longer<br />

recommended as a means <strong>of</strong><br />

restricting blood flow from a wound.<br />

The preferred option is to apply<br />

pressure to <strong>the</strong> wound by using a<br />

heavy pad held in place by bandages<br />

or even ones hand (preferably whilst<br />

wearing disposable gloves). The<br />

blood will eventually clot and <strong>the</strong><br />

blood flow stemmed.<br />

As a matter <strong>of</strong> last resort and if it<br />

is considered absolutely necessary<br />

to use a tourniquet, <strong>the</strong>n it must<br />

be released every ten or fifteen<br />

minutes for a short time in order<br />

to supply <strong>the</strong> tissue with blood.<br />

However <strong>the</strong> wound must be<br />

covered by a heavy pad and<br />

bandage to stem any blood flow.<br />

In this case <strong>the</strong> injuries sustained,<br />

although serious, were treatable<br />

and a good if not full recovery<br />

would have been made if a<br />

tourniquet had not been used.<br />

The Administration overseeing<br />

a vessel will have requirements<br />

for <strong>the</strong> medical qualifications<br />

required to be held by a vessel’s<br />

crew, and this case highlights <strong>the</strong><br />

importance <strong>of</strong> ensuring regular<br />

training is undertaken.<br />

Root Cause:<br />

Inadequate crew training.<br />

Financial Cost:<br />

The cost <strong>of</strong> this claim was<br />

over US$77,000.<br />

Issue Date: 23/04/04<br />

Case No. 42587<br />

102 103


Personal Injury/Illness<br />

A Real Eye Opener<br />

The Incident:<br />

This claim involved a purse seine fishing vessel engaged in fishing for tuna.<br />

The Chief Engineer was working in <strong>the</strong> vessel’s workshop when a foreign body entered<br />

his eye. The eye proved painful and <strong>the</strong> Master decided to land <strong>the</strong> injured engineer<br />

ashore for medical treatment. The nearest port was three days steaming away.<br />

Doctors removed <strong>the</strong> foreign body and <strong>the</strong> vessel returned to <strong>the</strong> fishing grounds.<br />

Observations:<br />

The medical examination revealed <strong>the</strong> foreign<br />

body (a piece <strong>of</strong> rusted metal) was “lodged<br />

superficially” on <strong>the</strong> eye and was easily removed<br />

by <strong>the</strong> attending doctor.<br />

Two points arise from this incident. Firstly, if <strong>the</strong><br />

Chief Engineer had been wearing safety goggles,<br />

<strong>the</strong> chances <strong>of</strong> <strong>the</strong> metal entering <strong>the</strong> eye would<br />

have been prevented and <strong>the</strong> incident would not<br />

have occurred. Secondly it is a little surprising that<br />

no apparent attempt was made to treat <strong>the</strong> injured<br />

party on board. The foreign body was superficially<br />

lodged and <strong>the</strong> vessel carried a medical outfit<br />

compliance with flag state requirements.<br />

Financial Cost:<br />

The cost to <strong>the</strong> Member in terms <strong>of</strong> <strong>the</strong> deviation<br />

was US$15,500 comprising fuel, port and hospital<br />

costs. The cost to <strong>the</strong> Member in lost fishing time<br />

during <strong>the</strong> 7 day deviation far exceeds this amount.<br />

Issue Date: 13/06/05<br />

Case No. 43868<br />

Root Cause:<br />

Poor Safety Practices.<br />

104 105


Personal Injury/Illness<br />

Carbon Monoxide Poisoning on Fishing Vessels<br />

The Incident:<br />

An experienced crewman <strong>of</strong> a 16 metre potter,<br />

who was both working and living on board <strong>the</strong><br />

vessel, died as he slept due to carbon monoxide<br />

poisoning. This was caused by <strong>the</strong> exhaust fumes<br />

<strong>of</strong> a petrol-driven generator running inside <strong>the</strong> fish<br />

hold. The generator had been brought on board by<br />

<strong>the</strong> crewman himself to power an electric heater,<br />

TV and radio.<br />

Observations:<br />

The bulkhead between <strong>the</strong> fish hold and <strong>the</strong><br />

crewman’s sleeping cabin was nei<strong>the</strong>r watertight<br />

nor gastight.<br />

Putting a petrol generator inside <strong>the</strong> fish hold<br />

introduced a number <strong>of</strong> hazards to <strong>the</strong> vessel:<br />

Carbon Monoxide:<br />

• Has no smell or taste<br />

• Symptoms <strong>of</strong> poisoning are similar to <strong>the</strong> flu<br />

• People may not be aware <strong>the</strong>y are being poisoned<br />

Fire/Explosion:<br />

• Petrol gives <strong>of</strong>f highly flammable fumes<br />

• A petrol engine below decks can potentially cause<br />

explosive fumes<br />

• O<strong>the</strong>r neighbouring boats could also be<br />

destroyed<br />

Electrical Hazard:<br />

• Household appliances are not designed for use in<br />

conditions <strong>of</strong>ten found on board fishing vessels<br />

• Correct wiring essential<br />

When living on board a vessel it is crucial<br />

to conduct a risk assessment so that:<br />

1. Sufficient power is provided for<br />

accommodation and lighting<br />

2. There is adequate ventilation (more needed<br />

for burners and stoves)<br />

3. There are adequate alarms to warn<br />

sleeping crewmen <strong>of</strong> problems<br />

4. Crew can escape from accommodation<br />

in an emergency<br />

5. It is safe for a lone crewman to board or<br />

leave <strong>the</strong> vessel at night<br />

Source - Maritime and Coastguard Agency<br />

Email: fishing@mcga.gov.uk<br />

Issue Date: 08/06/06<br />

Case No. 12346<br />

106 107


Personal Injury/Illness<br />

Careless Action Severely Injures Colleagues<br />

The Incident:<br />

Whilst trawling <strong>the</strong> net became entangled on its<br />

reel. A crew member climbed onto <strong>the</strong> net reel to<br />

clear <strong>the</strong> tangled section. Whilst clearing <strong>the</strong> net, <strong>the</strong><br />

deck boss, who was operating <strong>the</strong> winch, moved <strong>the</strong><br />

net reel without warning and without checking that<br />

<strong>the</strong> crewman was clear. As a result <strong>the</strong> crewman fell<br />

from <strong>the</strong> winch and fractured his leg and severely<br />

damaged his kneecap.<br />

Observations:<br />

The incident was caused by <strong>the</strong><br />

failure <strong>of</strong> <strong>the</strong> winch operator to<br />

ensure all crew were clear before<br />

he operated <strong>the</strong> winch. It is not<br />

uncommon for winch controls to<br />

be positioned such that <strong>the</strong> winch<br />

operator is unsighted and in such<br />

circumstances clear procedures<br />

must be put in place to prevent<br />

<strong>the</strong> winch being turned without<br />

<strong>the</strong> prior knowledge <strong>of</strong> those<br />

working in <strong>the</strong> vicinity. Conversely,<br />

if a crew member has to approach<br />

a winch he should ensure <strong>the</strong><br />

winch operator is made aware <strong>of</strong><br />

his impending actions.<br />

Root Cause:<br />

Dangerous operational practices.<br />

Financial Cost:<br />

US$200,575.<br />

Issue Date: 03/10/07<br />

Case No. 40374<br />

As is <strong>the</strong> case with most <strong>of</strong><br />

<strong>the</strong>se incidents, saving time is<br />

considered to be more important<br />

than safety and shortcuts are<br />

taken. It is only when injuries<br />

are suffered that crew have<br />

more than enough time to<br />

reflect on <strong>the</strong> consequences <strong>of</strong><br />

compromising safety.<br />

108 109


Personal Injury/Illness<br />

Good Intentions Result in a Very Large Claim<br />

The Incident:<br />

This accident occurred to an engineer on board a<br />

fishing vessel.<br />

During fishing operations a hydraulic hose developed<br />

a leak. The vessel’s engineer was called and after<br />

examining <strong>the</strong> hose, <strong>the</strong> engineer placed his thumb over<br />

<strong>the</strong> hole and <strong>the</strong>n instructed ano<strong>the</strong>r crew member to<br />

operate <strong>the</strong> controls. As a result <strong>of</strong> this, hydraulic oil at<br />

1600 psi was injected into his thumb.<br />

The skipper was called to <strong>the</strong> scene. He examined<br />

<strong>the</strong> injury which initially resembled an insect bite.<br />

The skipper suggested that <strong>the</strong> vessel returned<br />

to port. The engineer himself opposed this idea<br />

and dismissed <strong>the</strong> injury as a trivial matter <strong>of</strong> no<br />

consequence. The skipper did not seek fur<strong>the</strong>r<br />

medical advice.<br />

The vessel returned to port three days later. By <strong>the</strong><br />

time <strong>the</strong> engineer reached hospital his thumb had<br />

swollen considerably and he was in severe pain.<br />

Over <strong>the</strong> following two years he underwent a series<br />

<strong>of</strong> operations, but despite this he has been left with<br />

a permanent disability which prevents him from ever<br />

returning to work as an engineer.<br />

Observations:<br />

Although it was clear <strong>the</strong> injury was caused by <strong>the</strong><br />

engineer’s own actions, <strong>the</strong> long term effects <strong>of</strong><br />

<strong>the</strong> injury were due to <strong>the</strong> lack <strong>of</strong> prompt medical<br />

treatment. If <strong>the</strong> injury had been treated within 12<br />

hours <strong>of</strong> <strong>the</strong> incident, it would have been unlikely that<br />

any serious or permanent injuries would have resulted.<br />

Although <strong>the</strong> skipper acted with <strong>the</strong> best intentions<br />

and was guided in his evaluation <strong>of</strong> <strong>the</strong> injury by<br />

<strong>the</strong> engineer himself, <strong>the</strong> fact that he did not obtain<br />

proper medical advice resulted in <strong>the</strong> shipowner<br />

being found liable. If <strong>the</strong>y are in any doubt a Master<br />

should always seek medical advice. Such advice is<br />

<strong>read</strong>ily available by radio and is free <strong>of</strong> charge.<br />

Root Cause:<br />

Human error.<br />

Issue Date: 01/01/02<br />

Case No. 30582<br />

110 111


Navigation<br />

When a Lookout should Lookout<br />

The Incident:<br />

This claim involves a collision<br />

between a fishing vessel and a<br />

17000 gt products tanker.<br />

The Member’s vessel, a stern<br />

trawler was proceeding to<br />

her intended fishing grounds,<br />

which required her to cross a<br />

traffic separation scheme. The<br />

Member’s vessel contravened<br />

Rule 10c <strong>of</strong> <strong>the</strong> Collision<br />

Regulations by not crossing <strong>the</strong><br />

traffic lane at right angles.<br />

The Master had left <strong>the</strong><br />

wheelhouse and an inexperienced<br />

17 year old deckhand was left<br />

alone on watch.<br />

A radar target was noted<br />

approximately 3 miles on <strong>the</strong><br />

starboard bow, and after making<br />

a visual check, <strong>the</strong> watch-keeper<br />

made <strong>the</strong> assumption that<br />

<strong>the</strong> vessel would pass clear to<br />

starboard; having made this<br />

assessment <strong>the</strong> watch-keeper paid<br />

no fur<strong>the</strong>r attention to his lookout<br />

duties. More than one vessel was<br />

in fact within <strong>the</strong> immediate vicinity<br />

and <strong>the</strong> fishing vessel collided with<br />

ano<strong>the</strong>r ship shortly <strong>the</strong>reafter.<br />

The watch-keeper realised<br />

a collision was to take place<br />

seconds before it actually<br />

occurred. He put <strong>the</strong> wheel<br />

over, but as he had not<br />

disconnected <strong>the</strong> auto pilot<br />

<strong>the</strong>re was no response.<br />

Fortunately <strong>the</strong>re was no loss<br />

<strong>of</strong> life, but each vessel sustained<br />

heavy damage.<br />

Observations:<br />

The Member’s vessel failed to maintain a proper<br />

lookout and this was compounded by <strong>the</strong> fact that<br />

an inexperienced crew member was left in charge<br />

<strong>of</strong> <strong>the</strong> watch whilst transiting an area <strong>of</strong> heavy<br />

traffic. Having noted a radar target on <strong>the</strong> starboard<br />

bow and making an initial assessment , no fur<strong>the</strong>r<br />

observations were made until it was too late.<br />

The importance <strong>of</strong> maintaining a proper lookout<br />

cannot be over emphasised nor can <strong>the</strong> need to<br />

monitor all vessels closely when navigating in busy<br />

waterways. Consideration should always be given to<br />

“doubling up” watches in <strong>the</strong>se circumstances.<br />

Root Cause:<br />

Inadequate lookout.<br />

Financial Cost:<br />

The claim is expected to be no less than<br />

US$400,000.<br />

Issue Date: 18/06/03<br />

Case No. 35122<br />

112 113


Navigation<br />

Distracted Skipper Dims Beacon Light<br />

The Incident:<br />

This incident involved an Australian cray fishing vessel. In common with <strong>the</strong> majority <strong>of</strong><br />

this fleet this small vessel is highly powered and navigates at high speed.<br />

The vessel in question had just undergone engine repairs to try to cure an overheating<br />

problem with <strong>the</strong> main engines. The skipper and one deckhand took <strong>the</strong> vessel out<br />

on sea trials. During <strong>the</strong> trials <strong>the</strong> skipper was keeping a careful eye on <strong>the</strong> engine<br />

temperature gauges. As no problems were encountered <strong>the</strong> vessel’s speed was steadily<br />

increased until she was travelling at approximately 18 knots. The skipper’s attention was<br />

so firmly fixed on <strong>the</strong> engine gauges that he failed to notice a navigational marker dead<br />

ahead. Fortunately <strong>the</strong> deckhand who had just come onto <strong>the</strong> bridge spotted <strong>the</strong> beacon<br />

before <strong>the</strong> collision, enabling <strong>the</strong> Master to kill <strong>the</strong> power. Never<strong>the</strong>less <strong>the</strong> resulting<br />

collision severely damaged <strong>the</strong> boat and <strong>the</strong> beacon.<br />

Observations:<br />

This incident emphasises <strong>the</strong> need to maintain<br />

a good lookout at all times as required by <strong>the</strong><br />

International Regulations for <strong>the</strong> Prevention <strong>of</strong><br />

Collision at Sea. Had <strong>the</strong> deckhand not arrived<br />

on <strong>the</strong> bridge at <strong>the</strong> time he did, <strong>the</strong> vessel would<br />

have undoubtedly ploughed into <strong>the</strong> beacon at full<br />

speed with possibly disastrous consequences for<br />

those on board.<br />

Root Cause:<br />

Inadequate lookout.<br />

Financial Cost:<br />

The repairs to <strong>the</strong> beacon cost A$96,500<br />

(US$76,405).<br />

Issue Date: 01/01/02<br />

Case No. 24553<br />

114 115


Navigation<br />

Total Loss<br />

The Incident:<br />

A 360 ton deep sea fishing<br />

vessel had called at Pago Pago in<br />

American Samoa for bunkers en<br />

route to her fishing grounds east<br />

<strong>of</strong> Tahiti. She left Pago Pago in <strong>the</strong><br />

afternoon, steering an easterly<br />

course set to pass nine miles north<br />

<strong>of</strong> Rose Atoll, <strong>the</strong> only US National<br />

Wildlife Reserve in <strong>the</strong> sou<strong>the</strong>rn<br />

hemisphere. At approximately 4<br />

a.m. in clear wea<strong>the</strong>r <strong>the</strong> vessel<br />

ran hard aground on <strong>the</strong> south<br />

western side <strong>of</strong> <strong>the</strong> atoll. The<br />

forward double bottom tank<br />

below <strong>the</strong> fish holds ruptured<br />

immediately and oil started to spill<br />

from <strong>the</strong> vessel. The vessel was<br />

abandoned later in <strong>the</strong> morning<br />

after <strong>the</strong> engine room began to<br />

flood. The crew were picked<br />

up by a passing vessel without<br />

serious injury or loss <strong>of</strong> life.<br />

The nearest suitable salvage<br />

vessel was 2,000 miles from <strong>the</strong><br />

site and by <strong>the</strong> time it arrived<br />

<strong>the</strong> fishing vessel had broken up,<br />

spilling nearly 100,000 gallons<br />

<strong>of</strong> gas oil bunkers. Damage<br />

to <strong>the</strong> reef caused by <strong>the</strong><br />

grounding and <strong>the</strong> toxic effects<br />

<strong>of</strong> <strong>the</strong> oil extended to a radius<br />

<strong>of</strong> approximately 1 km from<br />

<strong>the</strong> wreck. The US authorities<br />

required that a clean-up<br />

operation be mounted and <strong>the</strong><br />

remains <strong>of</strong> <strong>the</strong> vessel removed.<br />

Observations:<br />

There were only two qualified<br />

<strong>of</strong>ficers on <strong>the</strong> fishing vessel, <strong>the</strong><br />

Master and <strong>the</strong> Chief Officer.<br />

The Chief Officer’s responsibility<br />

was apparently confined to <strong>the</strong><br />

operation and maintenance <strong>of</strong><br />

<strong>the</strong> fishing gear. He was not<br />

involved in navigational duties.<br />

After sailing <strong>the</strong> Master remained<br />

on <strong>the</strong> bridge until midnight<br />

when <strong>the</strong> vessel passed south<br />

<strong>of</strong> Manua Island. Before retiring<br />

<strong>the</strong> Master set bridge watches<br />

which consisted <strong>of</strong> one senior<br />

and one junior seaman. The only<br />

instruction given to <strong>the</strong> seamen by<br />

<strong>the</strong> Master were to call him if <strong>the</strong>y<br />

saw any lights. Rose Atoll is not lit.<br />

None <strong>of</strong> <strong>the</strong> seamen given <strong>the</strong> task <strong>of</strong> keeping watch had any<br />

navigational training. They had no knowledge <strong>of</strong> <strong>the</strong> collision<br />

regulations and were not even sure in which direction <strong>the</strong> vessel<br />

was steaming. They had no knowledge <strong>of</strong> navigational hazards in <strong>the</strong><br />

vicinity and <strong>the</strong>re was no chart on <strong>the</strong> bridge. They were untrained<br />

in <strong>the</strong> use <strong>of</strong> radar and <strong>the</strong> set was switched <strong>of</strong>f. The vessel was<br />

equipped with a GPS navigation system however <strong>the</strong> watchkeepers<br />

did not know how to ascertain <strong>the</strong>ir position and were unable<br />

to check whe<strong>the</strong>r <strong>the</strong> vessel was following <strong>the</strong> course set by <strong>the</strong><br />

Master.<br />

Root Cause:<br />

Insufficient manning.<br />

Financial Cost:<br />

In addition to losing a multi million dollar vessel <strong>the</strong> owner faced a<br />

bill <strong>of</strong> over US$1 million for clean-up and was also liable for fines and<br />

penalties under American pollution laws.<br />

Issue Date: 01/01/02<br />

Case No. 21195<br />

116 117


Navigation<br />

Fatigue Causes Grounding and Total Loss<br />

The Incident:<br />

This incident involves <strong>the</strong> grounding and subsequent<br />

total loss <strong>of</strong> a seine fishing vessel. The vessel was<br />

returning to its home port at <strong>the</strong> end <strong>of</strong> <strong>the</strong> salmon<br />

fishing season. She was proceeding in company<br />

with ano<strong>the</strong>r fishing vessel owned and operated by<br />

<strong>the</strong> captain’s bro<strong>the</strong>r. The maximum speed <strong>of</strong> this<br />

vessel was approximately 4 knots less than our ship.<br />

The two bro<strong>the</strong>rs believed that travelling rafted<br />

toge<strong>the</strong>r in sheltered water would reduce <strong>the</strong>ir<br />

overall passage time. Thus when <strong>the</strong> vessels entered<br />

<strong>the</strong> Greenville Channel which forms part <strong>of</strong> <strong>the</strong><br />

Inner Passage between <strong>the</strong> <strong>of</strong>f lying islands and <strong>the</strong><br />

coast <strong>of</strong> British Columbia <strong>the</strong> vessels were lashed<br />

alongside one ano<strong>the</strong>r and proceeded as a rafted<br />

unit. In <strong>the</strong> early hours <strong>of</strong> <strong>the</strong> morning both vessels<br />

ran hard aground on a small promontory on <strong>the</strong><br />

port side <strong>of</strong> <strong>the</strong> channel at a point where <strong>the</strong>re was<br />

a slight bend to starboard. An order to remove <strong>the</strong><br />

vessels was issued by <strong>the</strong> Department <strong>of</strong> Fisheries.<br />

Observations:<br />

No agreement had been reached for controlling<br />

<strong>the</strong> navigation <strong>of</strong> <strong>the</strong> combined unit. Nei<strong>the</strong>r vessel<br />

could control <strong>the</strong> course or engines <strong>of</strong> <strong>the</strong> o<strong>the</strong>r.<br />

Both vessels were on autopilot. The wheelhouse <strong>of</strong><br />

each vessel was manned by a single watchkeeper<br />

whose only method <strong>of</strong> communication with his<br />

counterpart was by VHF radio. At <strong>the</strong> time <strong>of</strong> <strong>the</strong><br />

grounding <strong>the</strong> watchkeeper on <strong>the</strong> o<strong>the</strong>r fishing<br />

vessel had reportedly left <strong>the</strong> wheelhouse to relieve<br />

himself and <strong>the</strong> watchkeeper on our vessel had fallen<br />

asleep.<br />

At some point shortly before <strong>the</strong> grounding <strong>the</strong><br />

vessels had run into a bank <strong>of</strong> fog however this was<br />

probably not causative <strong>of</strong> <strong>the</strong> loss. The most likely<br />

explanation is that with one bridge unmanned and <strong>the</strong><br />

o<strong>the</strong>r watchkeeper asleep <strong>the</strong> vessels failed to make<br />

<strong>the</strong> slight alteration <strong>of</strong> course necessary to follow <strong>the</strong><br />

channel. The problem was probably compounded<br />

by <strong>the</strong> fact that <strong>the</strong> more powerful vessel lay on <strong>the</strong><br />

starboard side <strong>of</strong> <strong>the</strong> o<strong>the</strong>r, making <strong>the</strong> combined unit<br />

more likely to veer to port.<br />

Root Cause:<br />

Poor navigational practices.<br />

Financial Cost:<br />

The smaller vessel was a<br />

constructive total loss and<br />

<strong>the</strong> larger vessel was severely<br />

damaged. Both vessels were<br />

refloated by <strong>the</strong>ir respective<br />

owners’ efforts. Never<strong>the</strong>less<br />

<strong>the</strong> costs incurred exceeded<br />

US$20,000.<br />

Issue Date: 01/01/02<br />

Case No. 24451<br />

It is unlikely that both vessels would have grounded<br />

had <strong>the</strong>y been navigating independently. With <strong>the</strong><br />

vessels rafted side by side both on autopilot and<br />

with no system for controlling <strong>the</strong> course or <strong>the</strong><br />

engines <strong>of</strong> <strong>the</strong> o<strong>the</strong>r, <strong>the</strong> slightest error by ei<strong>the</strong>r<br />

watchkeeper would almost inevitably end in disaster.<br />

118 119


Navigation<br />

If Only he could Swim<br />

The Incident:<br />

This incident involved a boom trawler stranding<br />

whilst fishing for prawns and is one <strong>of</strong> a number<br />

<strong>of</strong> similar incidents <strong>the</strong> Club has been involved<br />

with recently.<br />

The vessel was fishing approximately 0.5 miles<br />

from <strong>the</strong> shore with <strong>the</strong> Skipper on watch, alone.<br />

At approximately 23:00 on <strong>the</strong> evening in question,<br />

<strong>the</strong> engineer advised <strong>the</strong> Skipper that a problem had<br />

developed with <strong>the</strong> hydraulic pump for <strong>the</strong> trawl<br />

winch, rendering it inoperative. The Skipper left<br />

<strong>the</strong> wheelhouse to assess <strong>the</strong> situation for himself<br />

and returned shortly afterwards to telephone<br />

his managers. Whilst on <strong>the</strong> phone, <strong>the</strong> vessel<br />

grounded. After a list <strong>of</strong> some 35º developed,<br />

<strong>the</strong> crew donned <strong>the</strong>ir lifejackets, two liferafts<br />

were launched and <strong>the</strong> vessel was abandoned.<br />

Unfortunately <strong>the</strong> cook could not swim and,<br />

on entering <strong>the</strong> water, he panicked and<br />

subsequently drowned.<br />

Observations:<br />

The prime cause <strong>of</strong> <strong>the</strong> incident<br />

was <strong>the</strong> fact that <strong>the</strong> wheelhouse<br />

was undermanned. The vessel<br />

grounded only 100 metres from<br />

<strong>the</strong> shoreline which shows that<br />

during <strong>the</strong> time <strong>the</strong> Skipper’s<br />

attention had been diverted,<br />

<strong>the</strong> wind and current had set<br />

<strong>the</strong> vessel in towards <strong>the</strong> shore.<br />

Being alone on watch <strong>the</strong> Skipper<br />

had many tasks to attend to<br />

not least <strong>the</strong> navigation <strong>of</strong> <strong>the</strong><br />

vessel, keeping a lookout and<br />

steering, all whilst operating<br />

close inshore. The failure <strong>of</strong> <strong>the</strong><br />

hydraulic pump increased <strong>the</strong><br />

demands placed on <strong>the</strong> Skipper<br />

which led to <strong>the</strong> wheelhouse<br />

being left unmanned for a period<br />

<strong>of</strong> time and navigation continuing<br />

unmonitored whilst <strong>the</strong> telephone<br />

call to <strong>the</strong> managers took place.<br />

The incident was caused by a<br />

failure on <strong>the</strong> Skipper’s part to<br />

call for suitable assistance in<br />

<strong>the</strong> wheelhouse. There were<br />

no moves to supplement <strong>the</strong><br />

wheelhouse watch whilst <strong>the</strong><br />

Skipper’s attention was diverted<br />

to <strong>the</strong> problems with <strong>the</strong><br />

hydraulic pump which is difficult<br />

to understand considering <strong>the</strong><br />

proximity <strong>of</strong> <strong>the</strong> vessel to <strong>the</strong><br />

shore. Manning levels on fishing<br />

boats, whilst in accordance with<br />

Flag State requirements do not<br />

always provide for <strong>the</strong> luxury <strong>of</strong><br />

spare qualified crew members,<br />

but when circumstances dictate,<br />

as in this case, adjustments to<br />

work routines should be made<br />

to ensure <strong>the</strong> safety <strong>of</strong> <strong>the</strong> crew<br />

and vessel.<br />

In all likelihood, had <strong>the</strong> cook<br />

been able to swim, he would not<br />

have panicked to <strong>the</strong> extent he<br />

did and would probably still be<br />

alive today. He was found wearing<br />

his lifejacket. The Flag States<br />

Code <strong>of</strong> Safe Working Practices<br />

for Fishing Vessels recommends<br />

that all fishermen should be able<br />

to swim. So do we.<br />

Root Cause:<br />

Inadequate navigational practices.<br />

Financial Cost:<br />

The cost to <strong>the</strong> Club was only<br />

US$2,776. Fortunately <strong>the</strong> vessel’s<br />

diesel oil was blown out to sea<br />

with no beach pollution taking<br />

place. The crew were covered<br />

under <strong>the</strong> Flag States Workman’s<br />

Compensation Act and <strong>the</strong><br />

Club was not required by <strong>the</strong><br />

authorities to remove <strong>the</strong> wreck<br />

even though it had grounded in a<br />

scientifically sensitive area.<br />

The cost to <strong>the</strong> cook and his<br />

family was beyond calculation.<br />

Issue Date: 01/01/02<br />

Case No. 30438<br />

120 121


Navigation<br />

Unmanned Wheelhouses Cause Collision<br />

The Incident:<br />

The vessel involved in this collision was a<br />

19 metre steel trawler which worked <strong>the</strong><br />

scallop and prawn fishery <strong>of</strong>f <strong>the</strong> coast <strong>of</strong><br />

Queensland, Australia. The vessel fished by<br />

night and anchored during <strong>the</strong> day. She was<br />

manned by a crew <strong>of</strong> two. On <strong>the</strong> morning<br />

<strong>of</strong> <strong>the</strong> collision <strong>the</strong>y finished fishing at 7<br />

a.m. The skipper set course for her home<br />

port, handing over <strong>the</strong> watch to <strong>the</strong> deck<br />

hand in late morning. In <strong>the</strong> early afternoon<br />

<strong>the</strong> vessel collided with ano<strong>the</strong>r fishing<br />

vessel which was lying at anchor.<br />

Observations:<br />

At <strong>the</strong> time <strong>of</strong> <strong>the</strong> collision nei<strong>the</strong>r vessel<br />

was keeping a proper lookout as required<br />

by <strong>the</strong> International Regulations for<br />

<strong>the</strong> Prevention <strong>of</strong> <strong>the</strong> Collisions at sea.<br />

No anchor watch had been set on <strong>the</strong><br />

anchored vessel and all her crew were<br />

turned in. The crew member that was<br />

supposed to be keeping a navigational<br />

watch on our Member’s vessel was in<br />

fact on <strong>the</strong> afterdeck cleaning when <strong>the</strong><br />

collision occurred. The vessel was not<br />

fitted with a watch alarm, nor did it have a<br />

guardring facility on <strong>the</strong> radar.<br />

Root Cause:<br />

Inadequate navigational lookout.<br />

Financial Cost:<br />

Repairs to <strong>the</strong> anchored vessel cost over<br />

A$100,000. It was out <strong>of</strong> action at <strong>the</strong> height <strong>of</strong><br />

<strong>the</strong> scallop season for over two months, giving rise<br />

to a substantial claim for loss <strong>of</strong> pr<strong>of</strong>its, which was<br />

eventually settled for A$45,000. In addition to this<br />

<strong>the</strong>re was substantial damage to our Member’s<br />

vessel and it too was out <strong>of</strong> action for a substantial<br />

period at <strong>the</strong> height <strong>of</strong> <strong>the</strong> season.<br />

Issue Date: 01/01/02<br />

Case No. 23183<br />

122 123


Navigation<br />

A fatal nap<br />

The Incident:<br />

The crew <strong>of</strong> a longline fishing vessel had to abandon<br />

ship in violent seas at night after she grounded<br />

on rocks. The skipper drowned and one crew<br />

member’s body was never recovered. Two o<strong>the</strong>r<br />

crew members were tossed against rocks in stormy<br />

seas for hours. Before <strong>the</strong> grounding, no one had<br />

been keeping an anchor watch.<br />

The 18 metre steel-hulled commercial longliner set<br />

<strong>of</strong>f on a three day voyage at a time when heavy storm<br />

warnings were issued for all <strong>of</strong> <strong>the</strong> country, and most<br />

vessels in <strong>the</strong> area were heading for safe anchorage.<br />

In <strong>the</strong> late afternoon <strong>of</strong> <strong>the</strong> second day, <strong>the</strong> skipper<br />

anchored in a large bay. To get <strong>the</strong>re, <strong>the</strong> vessel<br />

steamed about 20 nautical miles past a safe and open<br />

port and instead anchored approximately 300 metres<br />

from a rocky coastline in about two metre seas.<br />

The nearby port’s Harbour Master saw <strong>the</strong> vessel<br />

‘punching’ through <strong>the</strong> seas and thought it peculiar<br />

for <strong>the</strong> vessel to stay at sea in such conditions.<br />

About an hour before <strong>the</strong> vessel weighed anchor,<br />

a nearby wave buoy recorded wave heights <strong>of</strong> 3.2<br />

metres, reaching 6.2 metres and increasing. Soon<br />

after midnight, <strong>the</strong> crew all turned in for <strong>the</strong> night.<br />

No anchor watch was kept. The vessel was fitted<br />

with radar and a GPS, depth sounder and course<br />

plotter, but none <strong>of</strong> <strong>the</strong>se were set to supplement<br />

an anchor watch or provide an alert.<br />

At about 3 am, <strong>the</strong> crew were woken by heavy<br />

waves battering <strong>the</strong> vessel. They soon discovered<br />

<strong>the</strong> vessel had dragged her anchor and was almost<br />

aground against <strong>the</strong> rocky coastline. Wave buoy<br />

recordings show that by this time <strong>the</strong> swells had<br />

increased to 5.2 metres, reaching a maximum <strong>of</strong> 9.1<br />

metres. At <strong>the</strong> vessel’s position, <strong>the</strong> waves would have<br />

been significantly higher in <strong>the</strong> shallow water.<br />

Waves had damaged <strong>the</strong> vessel, and she was set in to<br />

<strong>the</strong> shore with big seas breaking over her. The crew<br />

attempted to recover <strong>the</strong> anchor, but <strong>the</strong> winch would<br />

not operate. Attempts to cut <strong>the</strong> anchor wire with<br />

bolt cutters failed. When <strong>the</strong> vessel hit <strong>the</strong> rocks, <strong>the</strong><br />

skipper gave <strong>the</strong> order to abandon ship and set <strong>of</strong>f a<br />

distress beacon. All four on board dived into <strong>the</strong> sea.<br />

The skipper and one crew member drowned.<br />

The two remaining crew members spent hours in<br />

<strong>the</strong> water, being smashed by waves. One suffered<br />

a collapsed lung and extensive cuts and bruising.<br />

The o<strong>the</strong>r managed to crawl onto a small beach<br />

and suffered hypo<strong>the</strong>rmia. They were eventually<br />

rescued by helicopter and flown to hospital.<br />

Observations:<br />

1. Given <strong>the</strong> wea<strong>the</strong>r conditions from <strong>the</strong> outset<br />

<strong>of</strong> <strong>the</strong> voyage and <strong>the</strong> forecast, <strong>the</strong> vessel should<br />

not have set sail. Once en route, <strong>the</strong>re were two<br />

ports within timely reach <strong>of</strong> <strong>the</strong> vessel where she<br />

could have ber<strong>the</strong>d safely.<br />

2. The position <strong>the</strong> skipper chose to anchor in was<br />

unsuitable for <strong>the</strong> conditions, but <strong>the</strong> skipper did<br />

not seek local knowledge about a better location<br />

from Marine Radio or <strong>the</strong> Harbour Master.<br />

3. No anchor watch was kept by <strong>the</strong> crew. Maritime<br />

rules require that a proper lookout is maintained<br />

at all times and, given <strong>the</strong> conditions, was essential<br />

for <strong>the</strong> safety <strong>of</strong> <strong>the</strong> vessel.<br />

4. In addition to its four crew members, <strong>the</strong> vessel<br />

was fitted with radar and a GPS, depth sounder<br />

and chart plotter, which could have been set<br />

to assist <strong>the</strong> designated watchkeepers. Failing<br />

to maintain an anchor watch appeared to be<br />

standard practice on this vessel.<br />

5. The company that had contracted <strong>the</strong> vessel had<br />

adopted a ‘hands-<strong>of</strong>f’ approach to monitoring<br />

<strong>the</strong> safety performance <strong>of</strong> vessels it contracted.<br />

The operations manager knew this vessel was<br />

departing into <strong>the</strong> storm and, despite discussing<br />

<strong>the</strong> potential catch with <strong>the</strong> crew, made no<br />

mention <strong>of</strong> <strong>the</strong> wea<strong>the</strong>r. It was company policy<br />

to nei<strong>the</strong>r require nor dissuade a crew from<br />

undertaking a particular voyage.<br />

6. The need for keeping an anchor watch,<br />

particularly in adverse wea<strong>the</strong>r or when<br />

anchored on an open coastline, should have<br />

been reinforced by <strong>the</strong> contracting company.<br />

Both factors applied in this case and <strong>the</strong> failure<br />

directly contributed to <strong>the</strong> loss <strong>of</strong> <strong>the</strong> vessel<br />

and two lives. This dangerous failing could have<br />

been identified and corrected.<br />

7. As a result <strong>of</strong> this tragedy, <strong>the</strong> contracting<br />

company was fined and required to pay<br />

reparations to <strong>the</strong> victims’ families. The court<br />

found that <strong>the</strong> company failed to implement<br />

adequate policies or processes to ensure <strong>the</strong><br />

vessel’s crew properly followed maritime rules<br />

by ensuring a proper anchor watch was kept..<br />

Trading Area:<br />

Australasia & Pacific<br />

Issue Date: 23/08/10<br />

Case No. 230810<br />

This case study has been taken from:<br />

Maritime New Zealand’s ‘lookout’ issue 17.<br />

124 125


Pollution<br />

Short Cuts can take Longer<br />

The Incident:<br />

This incident involved <strong>the</strong> inadvertent spill overboard<br />

<strong>of</strong> oil during an internal transfer <strong>of</strong> bunkers.<br />

The day prior to <strong>the</strong> oil spill, <strong>the</strong> engineers had<br />

been pumping waste oil to a shore reception facility.<br />

Because it was felt <strong>the</strong> operation would take too<br />

long utilising <strong>the</strong> standard connection as required by<br />

<strong>the</strong> MARPOL regulations, a cross connection had<br />

been fabricated to fit between <strong>the</strong> bilge and bunker<br />

systems. The waste oil was <strong>the</strong>n pumped ashore<br />

via <strong>the</strong> bunker manifold without incident. When an<br />

internal transfer <strong>of</strong> oil was commenced <strong>the</strong> following<br />

day, heavy fuel oil spilled onto deck through an open<br />

manifold connection and <strong>the</strong>n spilt overboard.<br />

Observations:<br />

The vessel was detained by <strong>the</strong><br />

harbour authorities on a number<br />

<strong>of</strong> deficiencies which came to<br />

light during investigations into<br />

<strong>the</strong> incident. These included:-<br />

1. Oil Record Book not being<br />

correctly maintained<br />

2. SOPEP not updated<br />

3. Crew not familiar with<br />

<strong>the</strong> procedures required<br />

by <strong>the</strong> SOPEP<br />

4. Unauthorised cross<br />

connection between <strong>the</strong><br />

bilge and bunker systems.<br />

Notwithstanding <strong>the</strong> illegal cross<br />

connection, <strong>the</strong> primary cause <strong>of</strong><br />

this oil spill was <strong>the</strong> fact that valves<br />

utilised during <strong>the</strong> previous day’s<br />

operation had not been closed<br />

upon completion nor had <strong>the</strong><br />

manifold connection been blanked.<br />

It is imperative that pipeline<br />

systems are fully closed down<br />

after use and when utilised again,<br />

<strong>the</strong> pipelines and valves are<br />

checked during <strong>the</strong> early stages<br />

to ensure <strong>the</strong> oil is only flowing<br />

to <strong>the</strong> required destination and<br />

nowhere else.<br />

The ironic aspect <strong>of</strong> this incident<br />

was that <strong>the</strong> time saved in<br />

pumping <strong>the</strong> waste oil ashore via<br />

<strong>the</strong> bunker system was lost in<br />

<strong>the</strong> detention <strong>of</strong> <strong>the</strong> vessel which<br />

lasted four days.<br />

Root Cause:<br />

Inadequate SOPEP procedures.<br />

Financial Cost:<br />

The cost <strong>of</strong> this incident including<br />

fines and clean up charges is<br />

estimated to be US$90,000.<br />

Issue Date: 27/10/05<br />

Case No.42370<br />

126 127


Pollution<br />

Environmentally Unfriendly Bunkering<br />

The Incident:<br />

The Club is concerned at <strong>the</strong> number <strong>of</strong> oil pollution claims arising<br />

from oil transfer operations carried out by large fishing vessels,<br />

particularly in European ports.<br />

Typical examples are:<br />

1. A 7300 GT fishing vessel was to pump <strong>the</strong> contents <strong>of</strong> her sludge<br />

tank ashore to a road tanker hired for <strong>the</strong> purpose. The hose was<br />

connected and, immediately upon commencement <strong>of</strong> pumping,<br />

oil escaped on to <strong>the</strong> deck and into <strong>the</strong> dock from <strong>the</strong> outboard<br />

connection. Investigation showed that this unused connection had<br />

been left with its valve open and blank flange missing.<br />

2. A vessel <strong>of</strong> 2417 GT commenced bunkering heavy fuel oil.<br />

Approximately 30 minutes later, personnel observed oil spilling on<br />

to <strong>the</strong> deck and into <strong>the</strong> harbour waters. The leak was traced to a<br />

loose flange on an elbow piece at <strong>the</strong> manifold connection.<br />

3. In ano<strong>the</strong>r case oil was observed spilling out <strong>of</strong> an air vent and<br />

subsequently over <strong>the</strong> vessel’s side. Investigations showed that <strong>the</strong><br />

labels on <strong>the</strong> filling connections had been incorrectly placed and<br />

<strong>the</strong> wrong tank was being filled. (It should be pointed out that this<br />

bunkering operation was usually carried out on <strong>the</strong> o<strong>the</strong>r side <strong>of</strong> <strong>the</strong><br />

vessel without incident, but due to operational reasons this was not<br />

possible on this occasion).<br />

4. During <strong>the</strong> final stages <strong>of</strong> a bunkering operation, heavy fuel<br />

oil spilled out <strong>of</strong> <strong>the</strong> receiving tanks air pipe. Operations were<br />

immediately stopped but not before a quantity <strong>of</strong> oil had run<br />

out through <strong>the</strong> scupper pipes. It is thought <strong>the</strong> cause was an air<br />

bubble in <strong>the</strong> bunker tank which probably arose because <strong>of</strong> <strong>the</strong><br />

vessel’s three degree list and large stern trim at <strong>the</strong> time. The o<strong>the</strong>r<br />

possibility was an incorrect assessment <strong>of</strong> <strong>the</strong> capacity available.<br />

Observations:<br />

To some extent, <strong>the</strong>se incidents are all attributable<br />

to lax bunkering procedures. In one case, none <strong>of</strong><br />

<strong>the</strong> vessel’s staff were on board overseeing <strong>the</strong><br />

operation. All could have been prevented with a<br />

little more conscientious monitoring <strong>of</strong> operations.<br />

Loose flanges and open ended pipes appear to be a<br />

common feature.<br />

All <strong>the</strong> vessels in question have a gross tonnage<br />

in excess <strong>of</strong> 400 tonnes, so are governed by <strong>the</strong><br />

MARPOL regulations, in particular <strong>the</strong> Shipboard<br />

Oil Pollution Emergency Plan (SOPEP) which is in<br />

place to prevent instances described above.<br />

The non-mandatory section <strong>of</strong> a vessel’s SOPEP<br />

Manual should contain <strong>the</strong> operating company’s<br />

bunkering procedures. Equally, vessels to which <strong>the</strong><br />

regulations do not apply would be well advised to<br />

have in place similar procedures.<br />

Such procedures we believe should include <strong>the</strong><br />

following requirements:<br />

1. All valves in a pipeline system not required to be<br />

opened should be confirmed as being closed.<br />

2. All flanges not in use should be blanked <strong>of</strong>f.<br />

3. A crew member should be detailed to remain on<br />

deck at or near <strong>the</strong> manifold connection during<br />

<strong>the</strong> entire operation.<br />

4. Bunkering operations should be started and<br />

completed at a slow rate until a) it is confirmed<br />

that <strong>the</strong> oil is going into <strong>the</strong> correct tank and<br />

<strong>the</strong>re are no leaks and b) <strong>the</strong> tanks are “topped<br />

<strong>of</strong>f” in a controlled manner.<br />

5. Scupper plugs should be fitted and if this is<br />

not feasible, savealls fitted around <strong>the</strong> bunker<br />

connections and air vents should be <strong>of</strong> a practical<br />

size.<br />

6. Oil spill clean up equipment and absorbents<br />

should be placed on deck.<br />

Root Cause:<br />

Inadequate bunkering procedures.<br />

Issue Date:01/01/02<br />

Case No. 35341<br />

128 129


Section 4<br />

Passenger Vessels<br />

131


Passenger Vessels<br />

Personal Injury/Illness<br />

To be Forewarned should mean you are Forearmed<br />

The Incident:<br />

Shortly after boarding <strong>the</strong> vessel, a small passenger<br />

ferry, a young girl aged 10 fell down a storeroom<br />

access. She apparently climbed out <strong>of</strong> <strong>the</strong> 2 metre<br />

deep opening via a fixed ladder <strong>of</strong> her own accord.<br />

Her parents notified <strong>the</strong> crew and alerted <strong>the</strong><br />

shore based emergency services. She was taken<br />

to hospital and spent twelve days in <strong>the</strong> Intensive<br />

Care Unit as she was diagnosed as having a<br />

ruptured spleen. Subsequently <strong>the</strong> young girl<br />

made a full recovery.<br />

Apart from <strong>the</strong> girl’s parents, <strong>the</strong>re were no<br />

witnesses to <strong>the</strong> incident.<br />

Observations:<br />

Doubt exists as to whe<strong>the</strong>r or not <strong>the</strong> hatch cover<br />

used to secure <strong>the</strong> opening was in fact closed and<br />

<strong>the</strong> view taken is that a 10 year old girl, whilst not<br />

incapable <strong>of</strong> opening such a device would be unlikely<br />

to. However, <strong>the</strong> facts are that no warning or “No<br />

Admittance” notices were posted on or in <strong>the</strong> vicinity<br />

<strong>of</strong> <strong>the</strong> hatch cover and apart from a hook, <strong>the</strong> cover<br />

was not locked to prevent unauthorised opening.<br />

During investigations into <strong>the</strong> incident, <strong>the</strong> Chief<br />

Engineer admitted that he had observed on more<br />

than one occasion young passengers opening <strong>the</strong><br />

hatch cover out <strong>of</strong> curiosity, but unfortunately he<br />

had nei<strong>the</strong>r taken any action to secure <strong>the</strong> opening<br />

or advise anyone else <strong>of</strong> what he had observed.<br />

There are no safety reasons for <strong>the</strong> hatch cover not<br />

to have been padlocked closed when not in use as it<br />

only served a storeroom. Had it been secured in this<br />

manner, this incident would not have happened.<br />

The posting <strong>of</strong> warning or prohibitive signs would<br />

have made passengers aware <strong>of</strong> <strong>the</strong> dangers and<br />

would have helped <strong>the</strong> Member’s defence.<br />

Root Cause:<br />

Insufficient safety signs.<br />

Financial Cost:<br />

The lawyers were <strong>of</strong> <strong>the</strong> opinion that <strong>the</strong> Member<br />

would be held liable for <strong>the</strong> incident as it would<br />

be very difficult and expensive to prove any<br />

contributory negligence on behalf <strong>of</strong> a minor, thus<br />

<strong>the</strong> case was settled out <strong>of</strong> court.<br />

Total cost US$34,000.<br />

Issue Date: 01/01/02 Case No. 34113<br />

132 133


Personal Injury/Illness<br />

Difficult Step Causes Passenger Injury<br />

The Incident:<br />

This incident involves an injury to an elderly<br />

lady passenger disembarking from a tourist craft<br />

operating in north eastern Australia. The craft<br />

itself was <strong>of</strong> unusual construction, being a semisubmersible<br />

vessel which was designed to allow<br />

passengers to view coral reefs through windows in<br />

<strong>the</strong> lower deck below water level.<br />

The incident occurred after <strong>the</strong> vessel had returned<br />

to <strong>the</strong> dock. The passenger and her husband had<br />

not disembarked with <strong>the</strong> main body <strong>of</strong> passengers<br />

as <strong>the</strong>y had remained on board to search for a<br />

lost piece <strong>of</strong> camera equipment. Having found <strong>the</strong><br />

missing item <strong>the</strong>y ascended to <strong>the</strong> main deck and<br />

moved towards <strong>the</strong> gangway. To do so <strong>the</strong>y had<br />

to negotiate a change in level on <strong>the</strong> upper deck<br />

where <strong>the</strong>re was a 27 cm. step. In doing so <strong>the</strong> lady<br />

stumbled and fell, severely breaking her ankle.<br />

Observations:<br />

The raised section <strong>of</strong> <strong>the</strong> upper deck was covered<br />

to within 6 cms. <strong>of</strong> <strong>the</strong> step by a black plastic mat.<br />

The lower level and <strong>the</strong> 6 cm. strip along <strong>the</strong> edge<br />

<strong>of</strong> <strong>the</strong> higher level was painted with white non-skid<br />

paint. The result was that <strong>the</strong> edge <strong>of</strong> <strong>the</strong> step was<br />

difficult to detect visually. There were no handrails<br />

and <strong>the</strong>re were no warning notices or o<strong>the</strong>r visual<br />

warnings. Although crew members had been<br />

assigned to assist passengers at <strong>the</strong> gangway close<br />

by, none were assigned to assist passengers who<br />

negotiated <strong>the</strong> step.<br />

This accident should never have been allowed to<br />

happen. Our investigations revealed that crew<br />

members assigned to <strong>the</strong> gangway had observed<br />

passengers stumbling on <strong>the</strong> step on numerous<br />

occasions. If <strong>the</strong> company had implemented a safety<br />

management system <strong>the</strong> crew members would<br />

have a means <strong>of</strong> reporting <strong>the</strong>ir observations and<br />

appropriate measures could <strong>the</strong>n have been taken<br />

to minimise <strong>the</strong> risk to passengers. Those measures<br />

could have included painting <strong>the</strong> edge <strong>of</strong> <strong>the</strong> step<br />

in high visibility paint, <strong>of</strong> contrasting colour placing<br />

appropriate warning notices in <strong>the</strong> vicinity, fitting<br />

a handrail and stationing crew members to assist<br />

frail passengers in negotiating <strong>the</strong> change in level.<br />

Alternatively it might have been possible to replace<br />

<strong>the</strong> step with a ramp.<br />

Root Cause:<br />

Inadequate access.<br />

Financial Cost:<br />

The cost <strong>of</strong> this incident exceeded US$46,000.<br />

Issue Date: 01/01/02<br />

Case No. 21142<br />

134 135


Personal Injury/Illness<br />

One for <strong>the</strong> Water<br />

The Incident:<br />

The Members’ vessel was engaged on a wine and<br />

sightseeing tour. As <strong>the</strong> boat was leaving a jetty after<br />

a stop for refreshments and sightseeing, to return<br />

down river to her home berth, a passenger appeared<br />

to stand on <strong>the</strong> bow, step over <strong>the</strong> railings and jump<br />

or dive into <strong>the</strong> water. The skipper was alerted and<br />

he immediately put <strong>the</strong> engines into neutral. Efforts<br />

were <strong>the</strong>n made to manoeuvre <strong>the</strong> vessel to pick up<br />

<strong>the</strong> passenger. However, because <strong>of</strong> <strong>the</strong> configuration<br />

<strong>of</strong> <strong>the</strong> twin hulls <strong>the</strong> passenger went under <strong>the</strong><br />

bow and between <strong>the</strong> hulls where she caught her<br />

legs in <strong>the</strong> propeller housing causing <strong>the</strong> eventual<br />

amputation <strong>of</strong> both her feet.<br />

Observations:<br />

Lawyers acting for <strong>the</strong> passenger<br />

commenced proceedings alleging<br />

that she had fallen into <strong>the</strong> water<br />

as a result <strong>of</strong> insufficient guard<br />

railings and that her retrieval<br />

from <strong>the</strong> water was delayed<br />

for some 20 minutes while <strong>the</strong><br />

Master negligently manoeuvred<br />

<strong>the</strong> vessel causing her injury. (It is<br />

important to note that <strong>the</strong> <strong>of</strong>ficial<br />

investigation by <strong>the</strong> authorities<br />

exonerated <strong>the</strong> Master from any<br />

pr<strong>of</strong>essional blame).<br />

The Members asserted in defence<br />

that <strong>the</strong> passenger deliberately<br />

jumped into <strong>the</strong> water and was<br />

entirely responsible for her own<br />

injury. Witness evidence appeared<br />

to support <strong>the</strong> Members’ position<br />

that <strong>the</strong> passenger jumped <strong>of</strong>f<br />

<strong>the</strong> boat but also confirms that<br />

she was apparently intoxicated at<br />

<strong>the</strong> time. Despite this evidence<br />

<strong>the</strong> Members bore <strong>the</strong> brunt <strong>of</strong><br />

<strong>the</strong> responsibility <strong>of</strong> this incident<br />

despite <strong>the</strong> fact that it would<br />

appear <strong>the</strong> passenger acted <strong>of</strong><br />

her own volition. This case proves<br />

that <strong>the</strong> courts hold <strong>the</strong> carrier<br />

liable in such circumstances.<br />

Members are responsible for<br />

ensuring that passengers are<br />

not permitted to board <strong>the</strong>ir<br />

vessel whilst under <strong>the</strong> apparent<br />

influence <strong>of</strong> alcohol or drugs, or<br />

to drink excessively whilst on<br />

board. If it is considered that <strong>the</strong><br />

actions <strong>of</strong> passengers may put<br />

ei<strong>the</strong>r <strong>the</strong>mselves or o<strong>the</strong>rs in<br />

danger, efforts must be made by<br />

<strong>the</strong> ship’s crew to prevent such<br />

conduct getting out <strong>of</strong> hand.<br />

Prevention is better than cure!<br />

Root Cause:<br />

Lack <strong>of</strong> passenger supervision.<br />

Financial Cost:<br />

This claim was finally settled at<br />

US$608,500.<br />

Issue Date: 05/10/05<br />

Case No. 25685<br />

136 137


Personal Injury/Illness<br />

Reminder to Carry Out Frequent Risk Assessments,<br />

Especially on Routine Matters<br />

The Incident:<br />

This case involved an embarking passenger who<br />

slipped into a gap between <strong>the</strong> vessel’s starboard<br />

gangway and <strong>the</strong> ship.<br />

The passenger, who has difficulty walking/climbing<br />

steps due to his weight, started to board <strong>the</strong> vessel<br />

assisted by two crew members. At <strong>the</strong> top <strong>of</strong> <strong>the</strong><br />

steps <strong>the</strong> passenger paused for a few moments. As<br />

he continued he lost his balance whilst lifting his<br />

foot and he fell backwards into <strong>the</strong> gap between<br />

<strong>the</strong> steps and <strong>the</strong> vessel. The passenger’s leg was<br />

crushed. Due to <strong>the</strong> passenger’s weight <strong>the</strong> two<br />

crew members that were holding <strong>the</strong> passenger’s<br />

hands fell with him, one was injured. First aid was<br />

administered to <strong>the</strong> passenger and an ambulance<br />

was called. It was later learnt <strong>the</strong> passenger had a<br />

history <strong>of</strong> health, heart and leg problems.<br />

During <strong>the</strong> incident two ABs and <strong>the</strong> Chief Officer<br />

were present, advising and monitoring passenger<br />

embarkation. The sea was calm.<br />

The passenger had two operations to rectify <strong>the</strong><br />

crushed skin on <strong>the</strong> damaged leg.<br />

Observations:<br />

Plaintiff’s lawyers alleged <strong>the</strong> vessel’s employees<br />

were negligent in that <strong>the</strong>y failed to provide and<br />

ensure suitable and safe embarkation devices or aids<br />

and/or failed to control and secure <strong>the</strong> vessel during<br />

embarkation.<br />

As stated above three <strong>of</strong> <strong>the</strong> ship’s crew were<br />

present during <strong>the</strong> embarkation operation, ample<br />

safety notices were posted and company safety<br />

procedures were in place and being followed.<br />

This event highlights <strong>the</strong> importance <strong>of</strong> carrying<br />

out risk assessments in operational matters even if<br />

ample procedures are in place.<br />

Root Cause:<br />

Lack <strong>of</strong> passenger supervision.<br />

Financial Cost:<br />

The claim was settled at S$12,500.<br />

Issue Date: 01/06/06<br />

Case No. 47804<br />

138 139


Personal Injury/Illness<br />

Expect <strong>the</strong> Unexpected<br />

The Incident:<br />

This incident involved a 21 metre<br />

twin hulled passenger vessel<br />

engaged on a sightseeing voyage.<br />

The vessel was certified to carry<br />

240 passengers and at <strong>the</strong> time<br />

<strong>of</strong> <strong>the</strong> incident she had on board<br />

121 passengers.<br />

As <strong>the</strong> voyage progressed, <strong>the</strong><br />

wea<strong>the</strong>r conditions were fair to<br />

good with a moderate easterly<br />

wind with 0.5 metre waves on a<br />

1 to 2 metre swell.<br />

Approximately 15 passengers<br />

were standing on <strong>the</strong> foredeck.<br />

As <strong>the</strong> vessel turned into<br />

a bay, <strong>the</strong> Master made an<br />

announcement over <strong>the</strong><br />

public address system advising<br />

passengers that <strong>the</strong> seas may<br />

become “more choppy” and<br />

that <strong>the</strong>y should take care when<br />

moving about <strong>the</strong> ship. Shortly<br />

afterwards, a higher than normal<br />

wave was experienced and <strong>the</strong><br />

vessel rose and fell; this wave was<br />

followed by an even larger wave<br />

which caused <strong>the</strong> vessel’s bow<br />

to rise even higher than with <strong>the</strong><br />

previous wave and <strong>the</strong>n fall into<br />

<strong>the</strong> steep trough that followed.<br />

The effect <strong>of</strong> <strong>the</strong> vessel falling<br />

into <strong>the</strong> trough was to bodily lift a<br />

number <strong>of</strong> <strong>the</strong> passengers located<br />

on <strong>the</strong> fore deck and as <strong>the</strong> bow<br />

rose quickly on <strong>the</strong> next wave,<br />

<strong>the</strong> deck came up to meet <strong>the</strong> still<br />

falling passengers. As a result four<br />

passengers were seriously injured.<br />

Observations:<br />

The wave experienced could have been described as a rogue or freak wave, but <strong>the</strong><br />

following investigation concluded that <strong>the</strong> possibility <strong>of</strong> experiencing such a wave could<br />

have been expected in <strong>the</strong> area that was being navigated. (The generation <strong>of</strong> such waves<br />

is very complex and is caused by two or more wave trains, being deflected by islands in<br />

<strong>the</strong> vicinity, meeting which can cause a resultant wave with irregular heights).<br />

None <strong>of</strong> <strong>the</strong> passengers sitting within <strong>the</strong> accommodation were hurt and careful<br />

consideration must be given as to when to allow passengers out on to <strong>the</strong> foredeck. If<br />

such practice is restricted to periods <strong>of</strong> smooth waters or when <strong>the</strong> swells are low and<br />

even, <strong>the</strong> repetition <strong>of</strong> such an incident is unlikely.<br />

The authorities found that <strong>the</strong> Master and crew handled <strong>the</strong> post incident situation in a<br />

competent manner.<br />

The above case study is based on an investigation carried out by <strong>the</strong> Transport Accident<br />

Investigation Commission <strong>of</strong> New Zealand.<br />

Issue Date: 28/07/05<br />

Case No. 11234<br />

140 141


Personal Injury/Illness<br />

Good Record Keeping would have Reduced Claim<br />

The Incident:<br />

This accident happened to an elderly female passenger whilst<br />

disembarking from a tourist vessel operating <strong>of</strong>f <strong>the</strong> west coast <strong>of</strong><br />

Australia. As she was disembarking <strong>the</strong> passenger tripped, with <strong>the</strong><br />

result that she lost her balance and fell injuring her right knee on <strong>the</strong><br />

jetty. The passenger claimed that <strong>the</strong> principal cause <strong>of</strong> <strong>the</strong> accident was<br />

inadequate lighting.<br />

The first notice <strong>of</strong> a claim came in <strong>the</strong> form <strong>of</strong> a letter from a lawyer<br />

many months after <strong>the</strong> event. On investigation we found that no<br />

contemporary records <strong>of</strong> <strong>the</strong> incident existed. The deck log could not<br />

be found, <strong>the</strong>re was no accident report, nor was <strong>the</strong>re an entry in <strong>the</strong><br />

accident <strong>book</strong>. In addition during <strong>the</strong> intervening period <strong>the</strong>re had been<br />

staff changes, with <strong>the</strong> result that only one <strong>of</strong> <strong>the</strong> deck crew could be<br />

traced. From <strong>the</strong> evidence <strong>of</strong> this one witness we learnt that it was<br />

possible that <strong>the</strong> gangway was not in use at <strong>the</strong> time <strong>of</strong> this particular<br />

incident. Apparently it had been <strong>the</strong> practice <strong>of</strong> crew not to use <strong>the</strong><br />

gangway if <strong>the</strong> state <strong>of</strong> <strong>the</strong> tide brought <strong>the</strong> deck <strong>of</strong> <strong>the</strong> vessel level with<br />

<strong>the</strong> jetty. In those circumstances <strong>the</strong> passengers were simply assisted<br />

across <strong>the</strong> narrow gap.<br />

Observations:<br />

The biggest problem <strong>the</strong> Club encountered in dealing with this case<br />

was simply lack <strong>of</strong> information. In <strong>the</strong> words <strong>of</strong> <strong>the</strong> lawyers advising <strong>the</strong><br />

Club “in <strong>the</strong> light <strong>of</strong> .... your Member’s inability to refute <strong>the</strong> plaintiff’s<br />

version <strong>of</strong> <strong>the</strong> events, we are <strong>of</strong> <strong>the</strong> opinion that you would probably<br />

be found liable”.<br />

Root Cause:<br />

Inadequate access.<br />

Financial Cost:<br />

The claim was finally settled for US$13,000. However Members should<br />

note that <strong>the</strong> costs incurred simply trying to piece toge<strong>the</strong>r what had<br />

happened exceeded $5,000.<br />

Issue Date: 01/01/02<br />

Case No. 15003<br />

142 143


Personal Injury/Illness<br />

Good Record Keeping Prevents Claim<br />

The Incident:<br />

The owners <strong>of</strong> this vessel received a letter<br />

from lawyers representing an elderly lady who<br />

alleged that she had been injured when boarding<br />

<strong>the</strong> Member’s vessel 18 months previously. No<br />

incident had been recorded in <strong>the</strong> accident<br />

<strong>book</strong> on <strong>the</strong> day in question. The Master was<br />

interviewed and was quite emphatic that if an<br />

accident had occurred and <strong>the</strong> crew been aware<br />

<strong>of</strong> it, it would have been recorded. The o<strong>the</strong>r crew<br />

no longer worked for <strong>the</strong> company and two were<br />

known to have gone abroad. The remainder were<br />

traced but had no recollection <strong>of</strong> any accidents<br />

around <strong>the</strong> date in question.<br />

To board <strong>the</strong> vessel passengers simply stepped on<br />

to <strong>the</strong> deck. The gap between <strong>the</strong> vessel and <strong>the</strong><br />

dock varied between 2 and 10 cms. The claimant<br />

alleged that as she stepped across <strong>the</strong> boat moved<br />

away from <strong>the</strong> dock and her leg slipped between<br />

<strong>the</strong> vessel and <strong>the</strong> dock whereupon <strong>the</strong> boat moved<br />

back towards <strong>the</strong> dock, crushing her leg.<br />

An investigation <strong>of</strong> her medical history revealed that<br />

<strong>the</strong> lady had suffered from osteoarthritis for some<br />

time and had been treated for <strong>the</strong> problem by her<br />

general practitioner prior to <strong>the</strong> alleged incident.<br />

There was no mention <strong>of</strong> an accident in her medical<br />

records. Some seven months after <strong>the</strong> incident<br />

was alleged to have occurred she had arthroscopic<br />

surgery on her knee joint and later underwent<br />

fur<strong>the</strong>r surgery for a total knee replacement.<br />

Surgery however was not successful and she was left<br />

with a permanent disability. It was only <strong>the</strong>n that a<br />

claim was made against <strong>the</strong> vessel owner.<br />

Observations:<br />

This case is typical <strong>of</strong> many instances where<br />

claimants suffering from degenerative conditions<br />

try to link that condition to some ‘accident’ aboard<br />

a Member’s vessel in <strong>the</strong> hope <strong>of</strong> extorting large<br />

sums <strong>of</strong> money in ‘compensation’. These cases<br />

are <strong>of</strong>ten difficult to defend as first notice <strong>of</strong> <strong>the</strong><br />

problem <strong>of</strong>ten comes many months after <strong>the</strong><br />

alleged incident when it is difficult to identify <strong>the</strong><br />

crew on board at <strong>the</strong> time and when recollections<br />

are no longer fresh in <strong>the</strong> mind. It emphasises <strong>the</strong><br />

need to keep detailed records <strong>of</strong> crew and <strong>the</strong><br />

need to document every accident, however minor,<br />

to provide a body <strong>of</strong> evidence to demonstrate to<br />

a court that utmost care was taken and even <strong>the</strong><br />

most minor incidents were recorded. It is <strong>the</strong>n<br />

easier to convince a court that an unrecorded<br />

incident is unlikely to have taken place.<br />

Root Cause:<br />

Inadequate access arrangements.<br />

Financial Cost:<br />

This claim was settled at nuisance value however <strong>the</strong><br />

cost <strong>of</strong> lawyers, medical experts and investigation<br />

brought <strong>the</strong> total bill to over US$21,000.<br />

Issue Date: 01/01/02<br />

Case No. 15595<br />

144 145


Personal Injury/Illness<br />

Uncovered Hawse Pipe Leads to Expensive Passenger Trip<br />

The Incident:<br />

The vessel in question is a<br />

Mississippi type showboat<br />

steamer that carried out harbour<br />

cruises during which time<br />

passengers could enjoy meals<br />

and cabaret type entertainment.<br />

Passengers were actively<br />

encouraged to walk freely around<br />

<strong>the</strong> open decks, including <strong>the</strong><br />

fore and after decks, to enjoy <strong>the</strong><br />

views as <strong>the</strong> cruise proceeded.<br />

At approximately 21.15 on <strong>the</strong><br />

day in question, <strong>the</strong> attention<br />

<strong>of</strong> ship’s staff was drawn to <strong>the</strong><br />

fact one 57 year old female<br />

passenger had sustained injuries<br />

to her leg after falling in <strong>the</strong> bow<br />

region <strong>of</strong> <strong>the</strong> vessel. Initially <strong>the</strong><br />

injuries, although painful, were not<br />

considered severe enough to land<br />

<strong>the</strong> passenger immediately; in fact<br />

she expressed a wish to watch<br />

<strong>the</strong> evening’s entertainment. She<br />

was sent to hospital by taxi once<br />

<strong>the</strong> vessel returned to her berth<br />

later that evening.<br />

Initial medical opinion did not<br />

believe <strong>the</strong>re to be any fractures<br />

to her leg, but specialists later<br />

discovered she had in fact suffered<br />

a fracture behind her knee.<br />

Observations:<br />

Situated in <strong>the</strong> bow area <strong>of</strong> <strong>the</strong> vessel was <strong>the</strong><br />

windlass/winch arrangement and an associated<br />

hawse pipe which had not been provided with<br />

a cover (an oversight since building), leaving<br />

it exposed to all who passed by. It is not clear<br />

whe<strong>the</strong>r <strong>the</strong> fall was caused by <strong>the</strong> plaintiff stepping<br />

into <strong>the</strong> open pipe or catching her walking stick<br />

on it as she passed by. However <strong>the</strong> contributing<br />

factor to this incident is <strong>the</strong> fact <strong>the</strong> opening was<br />

not covered or fenced <strong>of</strong>f. Ano<strong>the</strong>r factor was<br />

considered to be <strong>the</strong> subdued lighting in <strong>the</strong> area<br />

with shadows masking <strong>the</strong> hazards.<br />

People who are unused to a marine environment<br />

may not appreciate dangers that are <strong>read</strong>ily<br />

apparent to a vessel’s crew. With this in mind, all<br />

areas to which passengers are permitted access<br />

must be regularly assessed for potential hazards<br />

and suitable precautions taken to prevent accidents,<br />

even if this means limiting access to non ship’s staff.<br />

Root Cause:<br />

Insufficient safety signs.<br />

Financial Cost:<br />

The case was settled at US$330,365.<br />

Issue Date: 01/01/02<br />

Case No. 23550<br />

146 147


Personal Injury/Illness<br />

Passenger Injury on Access Ramp<br />

The Incident:<br />

This incident arose on board a harbour ferry operating in smooth<br />

water. The harbour ferry was fitted with hydraulic ramps designed<br />

for <strong>the</strong> embarkation or disembarkation <strong>of</strong> passengers. The ramps had<br />

been lowered to enable passengers to board <strong>the</strong> vessel and having<br />

been positioned hydraulics were ‘locked’. Shortly after passengers<br />

started to board ano<strong>the</strong>r vessel backed into an adjacent wharf<br />

creating some wash. The combination <strong>of</strong> that wash and wave actions<br />

in <strong>the</strong> harbour caused <strong>the</strong> ferry to surge and roll. The movement<br />

resulted in <strong>the</strong> hydraulic ramp fitted to <strong>the</strong> ferry rising a few inches<br />

up <strong>of</strong>f <strong>the</strong> connecting hydraulic ramp fitted to <strong>the</strong> jetty. When <strong>the</strong><br />

vessel rolled back a passenger’s foot was trapped between <strong>the</strong><br />

ramps.<br />

Observations:<br />

Surprisingly <strong>the</strong> claimant’s lawyers did not argue<br />

that <strong>the</strong> ramp was unsafe because it did not hinge.<br />

Instead <strong>the</strong>y concentrated on <strong>the</strong> fact that <strong>the</strong><br />

wharfhand on duty had been preoccupied with tying<br />

up ano<strong>the</strong>r vessel when <strong>the</strong> accident occurred and<br />

that <strong>the</strong> ramp was unattended. Plaintiff’s lawyers<br />

alleged that had <strong>the</strong> crewman been at his place <strong>of</strong><br />

duty he could have warned passengers <strong>of</strong> <strong>the</strong> danger<br />

and prevented <strong>the</strong>m from boarding until it was safe<br />

to do so.<br />

While <strong>the</strong>re were considerable doubts about<br />

whe<strong>the</strong>r <strong>the</strong> presence <strong>of</strong> a company employee<br />

would have had any material effect on <strong>the</strong> incident,<br />

our lawyers advised that <strong>the</strong> simple fact that <strong>the</strong><br />

Member did not have an employee on <strong>the</strong> spot<br />

overseeing <strong>the</strong> boarding process would almost<br />

certainly have led <strong>the</strong> courts to <strong>the</strong> conclusion that<br />

our Member had not discharged <strong>the</strong>ir duty <strong>of</strong> care<br />

to <strong>the</strong> passenger. This illustrates <strong>the</strong> high standards<br />

that are expected from <strong>the</strong> operators <strong>of</strong> passenger<br />

vessels carrying <strong>the</strong> general public and <strong>the</strong> levels <strong>of</strong><br />

care which <strong>the</strong>y are expected to maintain.<br />

Root Cause:<br />

Inadequate access.<br />

Financial Cost:<br />

This claim was settled within <strong>the</strong> Member’s<br />

deductible.<br />

Issue Date: 01/01/02<br />

Case No. 23590<br />

148 149


Personal Injury/Illness<br />

Passenger Dies <strong>of</strong> Heat Attack Despite<br />

Determined Effort by Crew to Save Him.<br />

The Incident:<br />

The incident occurred on board a tourist vessel<br />

ferrying passengers out to a resort pontoon<br />

on <strong>the</strong> Great Barrier Reef. Although wea<strong>the</strong>r<br />

conditions were moderate a passenger succumbed<br />

to seasickness during <strong>the</strong> voyage. On arrival at <strong>the</strong><br />

pontoon most passengers <strong>the</strong>n boarded a glass<br />

bottom boat to view <strong>the</strong> flora and fauna on <strong>the</strong><br />

reef but <strong>the</strong> sick passenger and his wife remained<br />

on <strong>the</strong> pontoon. The crew provided a cabin for <strong>the</strong><br />

gentleman so that he could lie down. Some minutes<br />

later his wife called for assistance as her husband was<br />

having chest pains. The passenger had a history <strong>of</strong><br />

heart problems and it was clear that he was having<br />

a heart attack. The passenger carried medication<br />

for his condition which <strong>the</strong> crew supplemented with<br />

oxygen. The passenger was placed in a semi-sitting<br />

position with his legs elevated to reduce <strong>the</strong> strain<br />

on his heart. The Captain contacted his head <strong>of</strong>fice<br />

to arrange to evacuate <strong>the</strong> passenger. The head<br />

<strong>of</strong>fice were unable to locate a seaplane but were<br />

able to find a helicopter although that could not get<br />

to <strong>the</strong> ship for over two hours. The <strong>of</strong>fice called a<br />

doctor to <strong>the</strong> radio so that <strong>the</strong> Captain could obtain<br />

medical advice.<br />

Initially <strong>the</strong> passenger responded well to treatment<br />

but shortly after 1 p.m. <strong>the</strong> passenger stopped<br />

breathing. The ship’s crew was swiftly to organise<br />

resuscitation. Their efforts were supplemented by a<br />

registered nurse and an anaes<strong>the</strong>tist from amongst<br />

<strong>the</strong> passengers. The crew’s efforts to revive <strong>the</strong><br />

passenger continued until <strong>the</strong> helicopter containing<br />

a doctor and paramedic arrived and took over.<br />

Although <strong>the</strong> attempts to resuscitate <strong>the</strong> passenger<br />

continued for a fur<strong>the</strong>r hour <strong>the</strong>y were not successful.<br />

Observations:<br />

Although on this occasion <strong>the</strong> crew’s efforts did not save <strong>the</strong> passenger’s life, <strong>the</strong>y did<br />

everything possible for him. In addition in <strong>the</strong> heat <strong>of</strong> <strong>the</strong> crisis <strong>the</strong>y still found time to<br />

look after his wife and attend to her needs, comfort her during <strong>the</strong> ordeal and keep her<br />

fully informed <strong>of</strong> what was happening and <strong>the</strong> efforts being made to save her husband.<br />

The passenger’s wife later wrote to <strong>the</strong> company praising <strong>the</strong> efforts <strong>of</strong> all on board and<br />

commending <strong>the</strong>m for <strong>the</strong>ir efforts and support.<br />

This incident illustrates <strong>the</strong> benefits <strong>of</strong> maintaining good communication between <strong>the</strong><br />

crew and <strong>the</strong> friends and relatives <strong>of</strong> a sick or injured passenger. It is essential to keep<br />

friends and relatives fully advised <strong>of</strong> all developments and <strong>the</strong> action being taken to help<br />

<strong>the</strong> passenger. Bad communication can increase<br />

anxiety and create distrust, leaving friends and<br />

relatives feeling that <strong>the</strong> ship’s staff could or should<br />

be doing more, which could in <strong>the</strong> future lead to<br />

acrimony and litigation.<br />

Issue Date: 01/01/02<br />

Case No. 25478<br />

150 151


Personal Injury/Illness<br />

Explosion in Battery Locker<br />

The Incident:<br />

The vessel involved in this<br />

incident was a purpose-designed<br />

sail training vessel built in 1991.<br />

The vessel carried a substantial<br />

bank <strong>of</strong> lead acid batteries to<br />

power emergency systems, radios<br />

and fire detection systems. The<br />

batteries were housed in a locker<br />

on <strong>the</strong> port side <strong>of</strong> <strong>the</strong> main deck<br />

below <strong>the</strong> wheelhouse.<br />

In addition to a permanent crew<br />

<strong>the</strong> vessel carried 31 students<br />

who, in addition to pursuing<br />

academic studies, assisted in <strong>the</strong><br />

sailing and maintenance <strong>of</strong> <strong>the</strong><br />

vessel. On <strong>the</strong> morning <strong>of</strong> <strong>the</strong><br />

incident a party <strong>of</strong> students had<br />

been assigned <strong>the</strong> task <strong>of</strong> scaling<br />

and painting <strong>the</strong> port side <strong>of</strong> <strong>the</strong><br />

deck house. During <strong>the</strong> work<br />

an explosion occurred in <strong>the</strong><br />

battery locker. The blast threw<br />

one student overboard. Despite<br />

an extensive air and sea search he<br />

was never recovered.<br />

Observations:<br />

The student who died had been removing rust accumulations from<br />

around <strong>the</strong> battery locker door with a rotary grinding machine. The<br />

battery locker door was secured by four lugs and wing nuts. In order<br />

to grind <strong>of</strong>f rust around <strong>the</strong> lugs <strong>the</strong> student loosened <strong>the</strong> wing nuts<br />

and lifted <strong>the</strong>m clear <strong>of</strong> <strong>the</strong> lugs. Sparks from <strong>the</strong> grinding machine<br />

entered <strong>the</strong> locker and ignited an accumulation <strong>of</strong> hydrogen gas causing<br />

<strong>the</strong> explosion.<br />

The battery locker door was marked with <strong>the</strong> word ‘batteries’ in large<br />

red letters. Signs were fitted inside <strong>the</strong> locker to alert personnel to<br />

<strong>the</strong> presence <strong>of</strong> corrosive acid and <strong>the</strong> dangers <strong>of</strong> corrosive acid burns.<br />

There were no external warning signs prohibiting naked lights and<br />

smoking, nor was <strong>the</strong>re any warning <strong>of</strong> <strong>the</strong> explosive risk.<br />

Subsequent investigations revealed that <strong>the</strong> locker’s ventilation<br />

arrangements consisted <strong>of</strong> a single 20 mm diameter vent pipe which<br />

made no provisions for through ventilation. This was inadequate to<br />

dissipate <strong>the</strong> quantity <strong>of</strong> hydrogen gas given <strong>of</strong>f at high charge rates.<br />

Root Cause:<br />

Unsafe wing practices.<br />

Issue Date: 01/01/02<br />

Case No. 26355<br />

152 153


Personal Injury/Illness<br />

Hasty Exit Brings Slide <strong>of</strong> Despair<br />

The Incident:<br />

In this case a passenger fell <strong>of</strong>f his motorbike whilst<br />

disembarking from a ferry via <strong>the</strong> vessel’s ramp.<br />

The accident occurred as <strong>the</strong> front tyre made<br />

contact with <strong>the</strong> ramp. This resulted in <strong>the</strong> bike<br />

sliding from under <strong>the</strong> claimant.<br />

The passenger sustained an injury to his right hand<br />

and <strong>the</strong> motorbike sustained damage to <strong>the</strong> body<br />

work on <strong>the</strong> upper and lower right hand side. The<br />

rear bike pedal was also snapped <strong>of</strong>f.<br />

Observations:<br />

It is alleged that <strong>the</strong> accident occurred due to<br />

<strong>the</strong> combination <strong>of</strong> <strong>the</strong> highly polished surface <strong>of</strong><br />

<strong>the</strong> aluminium ramp, which was wet due to <strong>the</strong><br />

prevailing wea<strong>the</strong>r, and <strong>the</strong> motorbike’s speed.<br />

It is recommended that an anti-slip paint or o<strong>the</strong>r<br />

means, e.g. raised t<strong>read</strong>s, be applied to ramps and<br />

o<strong>the</strong>r passenger access areas as a preventative<br />

measure.<br />

Speed restriction signs should be displayed in<br />

prominent positions.<br />

Root Cause:<br />

Inadequate speed restrictions.<br />

Financial Cost:<br />

US$2,333.39<br />

Issue Date: 01/01/02<br />

Case No. 49748<br />

154 155


Personal Injury/Illness<br />

Passenger Impatience Leads to Injury<br />

The Incident:<br />

This incident concerns a serious injury suffered by<br />

a middle aged male passenger while disembarking<br />

from a harbour ferry. The passenger was a<br />

construction worker who had used <strong>the</strong> ferry service<br />

for several weeks before <strong>the</strong> incident to travel to<br />

and from work.<br />

During <strong>the</strong> crossing he occupied a seat near <strong>the</strong><br />

bows <strong>of</strong> <strong>the</strong> ferry on <strong>the</strong> lower deck. As <strong>the</strong> vessel<br />

approached its berth an announcement was made<br />

to passengers asking <strong>the</strong>m to remain seated until<br />

<strong>the</strong> ferry had ber<strong>the</strong>d and <strong>the</strong> gangway had been<br />

lowered. Despite this <strong>the</strong> passenger, along with<br />

many o<strong>the</strong>rs, left his seat to join a mass <strong>of</strong> people<br />

eager to disembark at <strong>the</strong> earliest moment. As <strong>the</strong><br />

vessel came alongside <strong>the</strong> man somehow came to<br />

fall between <strong>the</strong> vessel and <strong>the</strong> dock suffering severe<br />

crush injuries to his pelvis. The exact cause <strong>of</strong> his fall<br />

has never been adequately explained however <strong>the</strong>re<br />

has been speculation that <strong>the</strong> passenger had ei<strong>the</strong>r<br />

tried to disembark by an unorthodox manner or<br />

had somehow been pushed over <strong>the</strong> bulwark by <strong>the</strong><br />

pressure <strong>of</strong> <strong>the</strong> crowd.<br />

Observations:<br />

The ferry ber<strong>the</strong>d at a purposedesigned<br />

terminal. It was<br />

equipped with permanent<br />

gangways, which are hinged<br />

at deck level and lowered<br />

like a drawbridge onto <strong>the</strong><br />

dock, which was level with <strong>the</strong><br />

deck. There is solid bulwark<br />

extending to deckhead level<br />

for over two meters ei<strong>the</strong>r side<br />

<strong>of</strong> <strong>the</strong> gangway. Beyond that<br />

<strong>the</strong>re is a conventional solid<br />

bulwark to waist height which is<br />

supplemented by an additional rail<br />

approximately 30cm above <strong>the</strong><br />

bulwark cap in all areas except<br />

adjacent to mooring bits.<br />

Prior to docking <strong>the</strong> crew<br />

routinely make an announcement<br />

warning passengers to remain<br />

seated and <strong>the</strong> passenger decks<br />

are liberally supplied with<br />

multilingual notices to that effect.<br />

The passenger sued claiming<br />

substantial damages alleging that<br />

<strong>the</strong> owners failed to erect railings<br />

in <strong>the</strong> region <strong>of</strong> <strong>the</strong> mooring<br />

bulwarks to prevent passengers<br />

falling <strong>of</strong>f <strong>the</strong> ferry and that <strong>the</strong><br />

owner failed to take appropriate<br />

steps to ensure that passengers<br />

remain seated while <strong>the</strong> ferry<br />

was in motion. The court in Hong<br />

Kong gave judgement on case in<br />

November 2000. Judge Seagroaat<br />

found that <strong>the</strong> bulwarks near<br />

<strong>the</strong> mooring bits where <strong>the</strong>re<br />

are no additional railings was<br />

high enough to protect <strong>the</strong><br />

passengers disembarking properly<br />

at <strong>the</strong> appropriate time. More<br />

importantly however, <strong>the</strong><br />

Judge carefully considered <strong>the</strong><br />

duties and obligations on vessel<br />

owners on crowd control. In<br />

his judgement, Judge Seagroaat<br />

commented that passengers who<br />

leave <strong>the</strong>ir seats despite oral and<br />

written warnings to <strong>the</strong> contrary<br />

know, as any reasonable person<br />

knows, that <strong>the</strong> reason for such<br />

warnings or advice is that <strong>the</strong>re is<br />

always a risk <strong>of</strong> sudden movement<br />

<strong>of</strong> <strong>the</strong> ferry or <strong>of</strong> it hitting <strong>the</strong><br />

pontoon with some force <strong>the</strong>reby<br />

causing passengers to loose <strong>the</strong>ir<br />

balance and fall. Anyone who<br />

ignores such warnings does so at<br />

his or her own risk.<br />

The Judge went on to say that<br />

he did not think <strong>the</strong> defendants<br />

could do anything to deter such<br />

action o<strong>the</strong>r than by announced<br />

and visible warnings. He did<br />

not consider it practicable or<br />

reasonable to require <strong>the</strong> size<br />

<strong>of</strong> <strong>the</strong> crew to be increased to<br />

such proportions as to be able to<br />

physically restrain adult persons<br />

hellbent on early disembarkation.<br />

Consequently he found <strong>the</strong> ferry<br />

operators were not liable for <strong>the</strong><br />

passenger’s injuries.<br />

Root Cause:<br />

Inadequate access.<br />

Issue Date: 01/01/02 Case No.<br />

28627<br />

156 157


Personal Injury/Illness<br />

Certainly not a toast to good health<br />

The Incident:<br />

A steward onboard <strong>the</strong> vessel, washing <strong>the</strong> dishes as usual, poured<br />

some concentrated industrial detergent into an empty green mineral<br />

water bottle, to assist in measuring <strong>the</strong> correct quantity to be put into<br />

<strong>the</strong> dishwashing machine. The partly filled drinking water bottle was<br />

<strong>the</strong>n placed without any label indicating <strong>the</strong> contents with cleaning<br />

chemicals, near <strong>the</strong> galley sink.<br />

The next day, <strong>the</strong> unlabelled mineral water bottle, partly filled with<br />

detergent was put in <strong>the</strong> refrigerator, obviously being mistaken<br />

for drinking water. Subsequently it was placed on <strong>the</strong> lunch table.<br />

Unfortunately <strong>the</strong> liquid was odourless and <strong>the</strong> unsuspecting seaman<br />

poured it into a glass and took a few quick sips. He immediately<br />

became aware <strong>of</strong> an acute burning sensation in his mouth and<br />

throat. Fortunately, <strong>the</strong> yacht was in port and he was sent ashore<br />

to <strong>the</strong> local clinic, however it was not equipped to handle such<br />

serious cases and <strong>the</strong> seaman had to be transported to a hospital<br />

in a nearby larger town. By <strong>the</strong>n, he was suffering from breathing<br />

problems, had a swollen tongue and a purple face. The hospital<br />

managed to administer suitable treatment and confirmed that <strong>the</strong><br />

seaman had suffered internal burns. His permanent disability was<br />

assessed at 7% and as a result <strong>of</strong> his injuries, he will suffer from a<br />

bitonal voice and slow digestion.<br />

Observations:<br />

The use <strong>of</strong> a drinking water bottle for handling<br />

chemicals and also its careless stowage without any<br />

warning labels was <strong>the</strong> root cause <strong>of</strong> <strong>the</strong> incident.<br />

Fur<strong>the</strong>rmore, its storage within an area (<strong>the</strong> galley)<br />

where it was easily mistaken for drinking water was<br />

ano<strong>the</strong>r major contributing factor. Chemicals should<br />

only be stored in containers specifically designated<br />

and adequately marked for <strong>the</strong> purpose. They should<br />

not be handled in any containers that can be easily<br />

mistaken for anything else. Only <strong>the</strong> required quantity<br />

should be used and <strong>the</strong> remaining quantity, if possible,<br />

must be returned to its storage container. The mixing<br />

containers should be cleaned appropriately and<br />

stowed back in <strong>the</strong>ir designated place..<br />

Financial Cost:<br />

The total cost <strong>of</strong> this claim was USD 69,000<br />

Trading Area:<br />

Europe<br />

Issue Date: 16/03/10<br />

Case No. 56506<br />

158 159


Navigation<br />

Familiarity Breeding Contempt<br />

The Incident:<br />

This case involved two high speed passenger ferries<br />

owned and operated by <strong>the</strong> same company, which<br />

collided in reduced visibility.<br />

During <strong>the</strong> course <strong>of</strong> <strong>the</strong> early morning, both vessels<br />

had successfully carried out a number <strong>of</strong> runs<br />

between <strong>the</strong>ir designated ports. One vessel <strong>the</strong>n<br />

commenced a scheduled new run that involved a<br />

reciprocal course to <strong>the</strong> o<strong>the</strong>r vessel in a relatively<br />

narrow channel. Both Masters were aware that <strong>the</strong><br />

prevailing fog patches were reducing <strong>the</strong> visibility to<br />

50 metres or less.<br />

At <strong>the</strong> time <strong>of</strong> entering <strong>the</strong> same fog patch, <strong>the</strong><br />

Masters each detected <strong>the</strong> o<strong>the</strong>r vessel on radar. Over<br />

<strong>the</strong> VHF, one Master requested a “green to green”<br />

passing but <strong>the</strong> o<strong>the</strong>r Master declined requesting “red<br />

to red” and at <strong>the</strong> same time put his helm to hard a<br />

starboard and reduced engine revolutions.<br />

Shortly <strong>the</strong>reafter <strong>the</strong> vessels collided. Fortunately,<br />

<strong>of</strong> <strong>the</strong> combined total <strong>of</strong> 127 passengers and 7 crew<br />

<strong>the</strong>re were no injuries.<br />

Observations:<br />

The principal factors causing <strong>the</strong> collision were <strong>the</strong><br />

excessive speeds <strong>of</strong> both vessels and <strong>the</strong> short radar<br />

ranges utilised by <strong>the</strong> Masters immediately prior to<br />

<strong>the</strong> collision. Investigations showed that <strong>the</strong> vessels<br />

had a combined closing speed <strong>of</strong> 36 knots yet both<br />

radars were set on <strong>the</strong> 0.75n.m. range. This resulted<br />

in <strong>the</strong> maximum duration <strong>of</strong> 75 seconds from <strong>the</strong><br />

time <strong>the</strong> echo appeared at <strong>the</strong> edge <strong>of</strong> <strong>the</strong> screen<br />

to <strong>the</strong> time <strong>of</strong> impact. There were a number <strong>of</strong><br />

additional contributory factors including a failure<br />

to comply with <strong>the</strong> Rules for <strong>the</strong> Prevention <strong>of</strong><br />

Collisions at Sea, a failure to follow <strong>the</strong> company’s<br />

own procedures and <strong>the</strong> lack <strong>of</strong> a suitably qualified<br />

lookout on ei<strong>the</strong>r vessel.<br />

The speed <strong>of</strong> both vessels was excessive for <strong>the</strong><br />

conditions and <strong>the</strong> basic principle <strong>of</strong> frequently<br />

scanning greater radar ranges in order to permit <strong>the</strong><br />

early detection <strong>of</strong> o<strong>the</strong>r vessels in restricted visibility<br />

was not followed. The manning scales on board<br />

both vessels meant that <strong>the</strong> Masters were <strong>the</strong> only<br />

suitably qualified mariners on board, thus placing<br />

a great burden on both men at times <strong>of</strong> reduced<br />

visibility. The company had in place procedures<br />

and recommendations for courses to be followed,<br />

specifically designed to prevent end on situations<br />

and <strong>the</strong>se were not adhered to.<br />

Root Cause:<br />

Failure to comply with collision regulations.<br />

Issue Date: 01/01/02<br />

Case No. 39495<br />

160 161


Navigation<br />

If Only <strong>the</strong>y had Tried Something Different<br />

The Incident:<br />

A passenger vessel with 26 passengers and 12 crew<br />

on board ran aground in unsurveyed waters. At<br />

<strong>the</strong> time <strong>of</strong> <strong>the</strong> grounding <strong>the</strong> Master was alone<br />

on <strong>the</strong> bridge and <strong>the</strong> vessel was in automatic<br />

navigation mode. In this mode, course adjustments<br />

were initiated by a GPS linked to an electronic<br />

chart system which transmitted course alteration<br />

information to <strong>the</strong> auto pilot.<br />

A number <strong>of</strong> passengers received minor injuries as<br />

a result <strong>of</strong> <strong>the</strong> initial impact.<br />

Observations:<br />

The investigation deemed that <strong>the</strong> most likely<br />

cause <strong>of</strong> this incident was a discrepancy between<br />

<strong>the</strong> vessel’s true position and that determined by<br />

<strong>the</strong> GPS. Because total reliance was placed on<br />

<strong>the</strong> GPS with no o<strong>the</strong>r means used to verify <strong>the</strong><br />

vessel’s position, <strong>the</strong> discrepancy went unnoticed.<br />

In addition, it was clear that with <strong>the</strong> Master being<br />

alone on <strong>the</strong> bridge, a proper lookout could not<br />

be kept and this is all <strong>the</strong> more pertinent as <strong>the</strong><br />

vessel was navigating in uncharted waters. The<br />

investigation also raised concerns over <strong>the</strong> fatigue<br />

<strong>the</strong> Master may have been suffering, brought on by<br />

his intensive work routine.<br />

O<strong>the</strong>r navigational irregularities were highlighted<br />

including <strong>the</strong> fact <strong>the</strong> electronic chart system in use<br />

was not approved, in that <strong>the</strong> computer was not<br />

dedicated to <strong>the</strong> vessel’s navigation system but was<br />

also used for <strong>the</strong> ship’s administration.<br />

This case study is based on <strong>the</strong> investigation report<br />

prepared by <strong>the</strong> Australian Transport Safety Bureau.<br />

Root Cause:<br />

Incorrect navigational procedures.<br />

Issue Date: 31/08/05<br />

Case No. 12345<br />

This incident shows that no matter how<br />

technologically advanced a vessel’s navigation<br />

system is, <strong>the</strong>re is no substitute for good old<br />

fashioned seamanship!<br />

162 163


Navigation<br />

Paperwork Leads to Grounding<br />

The Incident:<br />

This incident occurred on <strong>the</strong> inland waterways <strong>of</strong> sou<strong>the</strong>rn Australia. A passenger<br />

excursion vessel on a river passage collided with <strong>the</strong> river bank in good conditions and<br />

broad daylight. Fortunately little damage was done and passenger injuries were limited to<br />

a few cuts and bruises.<br />

Subsequent investigation revealed that <strong>the</strong> Mate was not paying attention to his duties.<br />

He was trying to catch up with his paperwork and was not looking where he was going.<br />

Observations:<br />

In recent years ever-increasing amounts <strong>of</strong> legislation<br />

have increased <strong>the</strong> administrative workload on<br />

board ship. Ships’ <strong>of</strong>ficers are spending increasing<br />

amounts <strong>of</strong> time on paperwork. Owners must<br />

however ensure that <strong>the</strong>ir <strong>of</strong>ficers’ attention is not<br />

distracted from <strong>the</strong>ir principal responsibilities in<br />

relation to <strong>the</strong> safe navigation <strong>of</strong> <strong>the</strong> ship and safety<br />

<strong>of</strong> life on board. Duties should be arranged so that<br />

adequate time is allowed for <strong>the</strong> completion <strong>of</strong><br />

paperwork in a manner that will not interfere with<br />

an <strong>of</strong>ficer’s primary responsibilities.<br />

Root Cause:<br />

Failure to perform correct lookout.<br />

Financial Cost:<br />

Although no claims arose from this occurrence<br />

<strong>the</strong> costs for a precautionary investigation to<br />

protect <strong>the</strong> owners from potential injury claims<br />

from passengers and any possible inquiry by <strong>the</strong><br />

regulatory authorities exceeded US$5,000.<br />

Issue Date: 01/01/02<br />

Case No. 24492<br />

164 165


Navigation<br />

Collision Alongside<br />

The Incident:<br />

The claim involved three passenger<br />

vessels, two <strong>of</strong> which collided,<br />

whilst performing unberthing/<br />

berthing operations in a river.<br />

Two <strong>of</strong> <strong>the</strong> vessels were ber<strong>the</strong>d<br />

alongside a quay. To allow <strong>the</strong><br />

inner vessel, with passengers on<br />

board, to sail <strong>the</strong> outer vessel<br />

manoeuvred “crabways” to<br />

starboard. When <strong>the</strong> route was<br />

clear <strong>the</strong> inner vessel sailed.<br />

During this time <strong>the</strong> third vessel<br />

was approaching <strong>the</strong> same quay<br />

from astern <strong>of</strong> <strong>the</strong> o<strong>the</strong>r two<br />

vessels. The outer vessel began<br />

to return to <strong>the</strong> berth by moving<br />

“crabways” to port and did not<br />

observe <strong>the</strong> closing third vessel.<br />

A collision occurred between<br />

<strong>the</strong> second vessel on its port aft<br />

corner and <strong>the</strong> third vessel on its<br />

starboard fore corner.<br />

Minor bruises were noted on<br />

some <strong>of</strong> <strong>the</strong> passengers on <strong>the</strong><br />

third vessel and damage occurred<br />

to <strong>the</strong> second vessel.<br />

Observations:<br />

• The approaching vessel assumed both vessels ahead were<br />

clearing <strong>the</strong> berth but never made contact to confirm<br />

• Nei<strong>the</strong>r vessel made any effort to ascertain <strong>the</strong><br />

actions <strong>of</strong> <strong>the</strong> o<strong>the</strong>r vessels in <strong>the</strong> vicinity<br />

• Complacency on <strong>the</strong> part <strong>of</strong> <strong>the</strong> vessel returning to <strong>the</strong> berth<br />

• No effective port control<br />

This claim reiterates <strong>the</strong> importance <strong>of</strong> keeping an efficient look out at all times, especially<br />

whilst performing manoeuvres in close proximity to fixed and floating objects. If in doubt<br />

contact should be made with <strong>the</strong> o<strong>the</strong>r vessels to confirm <strong>the</strong>ir intentions.<br />

Root Cause:<br />

Insufficient communication.<br />

Financial Cost:<br />

Approximately €35,000.<br />

Issue Date: 11/04/07<br />

Case No. 46260<br />

166 167


Navigation<br />

Intermittent Main Engine Fault Leads to Dock Damage<br />

The Incident:<br />

This incident occurred when a harbour ferry failed to respond to <strong>the</strong><br />

main engine controls with <strong>the</strong> result that she collided with <strong>the</strong> dock.<br />

The ferry had been approaching <strong>the</strong> berth at slow speed when <strong>the</strong><br />

Master tried to engage astern power. At this point he lost bridge<br />

control <strong>of</strong> <strong>the</strong> main engines with <strong>the</strong> result that <strong>the</strong> vessel continued<br />

forward, colliding with <strong>the</strong> piles at <strong>the</strong> end <strong>of</strong> <strong>the</strong> jetty.<br />

Observations:<br />

Investigation into <strong>the</strong> accident revealed that a similar problem had<br />

been encountered by <strong>the</strong> Master <strong>of</strong> <strong>the</strong> vessel during <strong>the</strong> previous<br />

shift. On that occasion power had been restored by jiggling <strong>the</strong> key<br />

in <strong>the</strong> engine control selector switch panel. Apart from completing a<br />

defects report no fur<strong>the</strong>r investigation or repair work was undertaken.<br />

The vessel remained in passenger service and no special precautions<br />

were taken during <strong>the</strong> berthing operation to minimise <strong>the</strong> risk from<br />

sudden control failure. After <strong>the</strong> accident <strong>the</strong> control switches were<br />

replaced. Had <strong>the</strong> problem been properly investigated immediately<br />

and appropriate corrective action taken, this accident need not have<br />

occurred. In this case <strong>the</strong> two Captains would have benefited from<br />

clear guidelines on removing <strong>the</strong> vessel from service.<br />

Root Cause:<br />

Insufficient maintenance system.<br />

Financial Cost:<br />

The cost <strong>of</strong> repairs to <strong>the</strong> dock exceeded US$15,000.<br />

Issue Date: 01/01/02<br />

Case No. 22685<br />

168 169


Section 5<br />

Offshore Vessels<br />

171


Offshore Vessels<br />

Personal Injury/Illness<br />

A Scenic View but a Dangerous Place to Stand<br />

The Incident:<br />

The Member’s tug was standing by an anchored<br />

dumb barge which was being loaded with sawn<br />

timber. The tug Master noted that in <strong>the</strong> rough sea<br />

conditions, <strong>the</strong> barge was dragging her anchor and<br />

starting to drift towards shallow water. The decision<br />

was made to tow <strong>the</strong> barge back out to clear water.<br />

The Chief Officer and Chief Engineer were<br />

instructed to pass <strong>the</strong> tow line to <strong>the</strong> barge, but in<br />

<strong>the</strong> wea<strong>the</strong>r conditions <strong>the</strong>y experienced difficulty.<br />

The cook was observing <strong>the</strong> operation and,<br />

characteristically, <strong>of</strong>fered his assistance. With <strong>the</strong><br />

cook’s help <strong>the</strong> line was successfully made fast. The<br />

Master <strong>the</strong>n took <strong>the</strong> strain on <strong>the</strong> tow line. The<br />

configuration <strong>of</strong> <strong>the</strong> tug, tow line and barge was such<br />

that <strong>the</strong> line was in contact with <strong>the</strong> tug’s towing<br />

pins. As <strong>the</strong> strain on <strong>the</strong> tow line was increased, <strong>the</strong><br />

towing pin failed and <strong>the</strong> tow line struck <strong>the</strong> cook<br />

who was standing in close proximity. The force <strong>of</strong><br />

<strong>the</strong> blow threw him overboard and his body was<br />

never recovered.<br />

Observations:<br />

This fatality arose because <strong>the</strong><br />

cook was standing in entirely <strong>the</strong><br />

wrong place when <strong>the</strong> strain was<br />

being taken up on <strong>the</strong> tow line.<br />

From <strong>the</strong> diagram it can be seen<br />

that <strong>the</strong> o<strong>the</strong>r two crew members<br />

were safely standing clear and<br />

were never in any danger.<br />

The investigation into this incident<br />

did not determine <strong>the</strong> events or<br />

signals that were made between<br />

<strong>the</strong> Chief Officer and <strong>the</strong><br />

Master once <strong>the</strong> tow had been<br />

successfully made fast, however it<br />

is abundantly clear that <strong>the</strong> cook<br />

was allowed to place himself in<br />

danger. The Chief Officer should<br />

not have given <strong>the</strong> all fast signal<br />

to <strong>the</strong> Master until all crew had<br />

cleared <strong>the</strong> danger area.<br />

Whilst <strong>the</strong> cook’s voluntary<br />

efforts in his willingness to<br />

assist his fellow crew mates are<br />

commendable, this incident<br />

shows how naivety can have<br />

disastrous consequences.<br />

Catering and engineering staff are<br />

not necessarily natural seamen<br />

and do not always appreciate<br />

<strong>the</strong> dangers that tow lines pose,<br />

nor <strong>the</strong> destruction that can take<br />

place when a line under strain<br />

fails through whatever cause. It<br />

would appear that in this case no<br />

guidance at all was given to <strong>the</strong><br />

cook – if it was and ignored <strong>the</strong>n<br />

a formal order should have been<br />

given and towing not commenced<br />

until everyone was standing clear<br />

and <strong>the</strong>reafter kept clear until<br />

operations were over.<br />

Root Cause:<br />

Poor operational practice.<br />

Issue Date: 31/10/05<br />

Case No. 47261<br />

172 173


Personal Injury/Illness<br />

Short Cuts do not Always Result in a Quick Job<br />

The Incident:<br />

This incident resulted in <strong>the</strong><br />

death <strong>of</strong> a seaman whilst securing<br />

a container on deck.<br />

A single 20 foot container<br />

weighing about 10 tonnes had<br />

been loaded onto <strong>the</strong> deck <strong>of</strong><br />

an Anchor Handling Tug.<br />

The crew were engaged in<br />

securing <strong>the</strong> container by means<br />

<strong>of</strong> a 3 inch polypropylene<br />

mooring rope which was secured<br />

at one end and <strong>the</strong>n led around<br />

<strong>the</strong> container. The loose end was<br />

placed on <strong>the</strong> drum end <strong>of</strong> an<br />

anchor handling winch and <strong>the</strong><br />

slack was being taken up.<br />

The rope parted and struck<br />

<strong>the</strong> victim in <strong>the</strong> face. He<br />

was immediately evacuated<br />

to hospital. Never regaining<br />

consciousness he died fifteen<br />

days later.<br />

Observations:<br />

Investigations showed <strong>the</strong> rope to be old and in a<br />

poor condition brought about by its age, heat and<br />

exposure to sunlight. The conclusion drawn was that<br />

<strong>the</strong> rope was severed as it passed over <strong>the</strong> sharp<br />

edge <strong>of</strong> <strong>the</strong> container. The victim was positioned<br />

by <strong>the</strong> warping drum obscured from <strong>the</strong> winch<br />

operator’s view.<br />

The method used to secure <strong>the</strong> container was<br />

inefficient and inherently dangerous. The vessel<br />

was fitted with more than an adequate number <strong>of</strong><br />

dedicated securing rings and fixing points which<br />

would have enabled a correct method <strong>of</strong> securing to<br />

have been used.<br />

This incident highlights <strong>the</strong> dangers <strong>of</strong> taking shortcuts,<br />

poor work practices and <strong>the</strong> use <strong>of</strong> old rope.<br />

Root Cause:<br />

Poor working practices.<br />

Financial Cost:<br />

The cost <strong>of</strong> <strong>the</strong> claim was US$33,000.<br />

Issue Date: 25/08/03<br />

Case No. 36103<br />

174 175


Personal Injury/Illness<br />

Prevention is Necessary as <strong>the</strong>re is No Cure<br />

The Incident:<br />

A tug belonging to one <strong>of</strong> <strong>the</strong><br />

Club’s Members was stationed<br />

<strong>of</strong>f Point Noire Congo when<br />

one <strong>of</strong> <strong>the</strong> crew took seriously ill<br />

one evening. He was transferred<br />

to a nearby rig and, after<br />

assessment by a doctor, was<br />

transferred ashore to hospital<br />

where he later died. The<br />

diagnosis was a severe strain <strong>of</strong><br />

cerebral malaria.<br />

On passage to <strong>the</strong> next port,<br />

ano<strong>the</strong>r crew member was taken<br />

ill with a mild strain <strong>of</strong> malaria and<br />

was repatriated.<br />

A few days later, <strong>the</strong> Master took<br />

ill and <strong>the</strong> vessel was diverted to<br />

<strong>the</strong> nearest port but unfortunately<br />

he died before medical assistance<br />

could be arranged. His death was<br />

caused by malaria.<br />

The families <strong>of</strong> <strong>the</strong> deceased took<br />

legal action against <strong>the</strong> Members<br />

for failing to provide adequate antimalarial<br />

protection for <strong>the</strong> crew.<br />

Observations:<br />

An expert in tropical medications examined this case and confirmed that<br />

<strong>the</strong> Members had not taken appropriate measures to ensure <strong>the</strong> health<br />

and safety <strong>of</strong> <strong>the</strong> crew. The anti-malarial medicine made available was<br />

<strong>of</strong> <strong>the</strong> wrong type for <strong>the</strong> area <strong>the</strong> vessel was operating in, and it was<br />

concluded that if <strong>the</strong> correct medication had been made available <strong>the</strong><br />

fatalities would have been avoided.<br />

In <strong>the</strong> malarial regions <strong>of</strong> <strong>the</strong> world, different strains <strong>of</strong> <strong>the</strong> infection build<br />

up resistance to <strong>the</strong> various medications available and it is important that<br />

medical advice is obtained for <strong>the</strong> area in question prior to <strong>the</strong> vessel<br />

arriving.<br />

The Ship Captain’s Medical<br />

Guide and Marine Guidance<br />

Note 257 (M) (published by <strong>the</strong><br />

UK’s Maritime and Coastguard<br />

Agency) contain advice on <strong>the</strong><br />

precautions to be taken and <strong>the</strong><br />

medicines available. The Health<br />

Authorities <strong>of</strong> <strong>the</strong> Members’<br />

country <strong>of</strong> domicile will be able<br />

to give advice on <strong>the</strong> type <strong>of</strong><br />

preventative medicines to be<br />

administered whilst <strong>the</strong> vessel is in<br />

a malarial region.<br />

Root Cause:<br />

Inadequate medical procedures.<br />

Issue Date: 06/02/06<br />

Case No.35489<br />

176 177


Personal Injury/Illness<br />

Safety Goggles - Not Just for Hindsight<br />

The Incident:<br />

This incident occurred on board an anchor handling<br />

supply vessel operating <strong>of</strong>f <strong>the</strong> west coast <strong>of</strong> Africa.<br />

The second engineer was supervising <strong>the</strong> cleaning<br />

<strong>of</strong> <strong>the</strong> mechanism <strong>of</strong> <strong>the</strong> vessel’s towing pins as part<br />

<strong>of</strong> <strong>the</strong> vessel’s routine maintenance programme.<br />

The cleaning was being carried out using a<br />

high-pressure water jet. The operator <strong>of</strong> <strong>the</strong> highpressure<br />

jet was wearing protective clothing in<br />

accordance with <strong>the</strong> manufacturer’s instructions.<br />

During <strong>the</strong> cleaning operation <strong>the</strong> second engineer<br />

who was wearing no protective clothing was hit in<br />

<strong>the</strong> left eye at a distance <strong>of</strong> about one metre by <strong>the</strong><br />

jet <strong>of</strong> water from <strong>the</strong> high-pressure washer.<br />

His vision was affected and a few days later was<br />

examined by an ophthalmologist in Point Noire<br />

in <strong>the</strong> Congo. The ophthalmologist diagnosed a<br />

simple eye irritation. The ophthalmologist treated<br />

<strong>the</strong> engineer for approximately two months with<br />

antiseptic eye lotions without improvement.<br />

During this period <strong>the</strong>re was no discernible<br />

improvement in his condition. The engineer<br />

completed his normal tour <strong>of</strong> duty. On his return<br />

home <strong>the</strong> second engineer consulted his own<br />

doctors who immediately diagnosed a detached<br />

retina. The <strong>of</strong>ficer underwent immediate eye<br />

surgery but because <strong>of</strong> <strong>the</strong> delay <strong>the</strong> doctors were<br />

unable to restore his vision.<br />

Observations:<br />

This accident would have been avoided if <strong>the</strong> second<br />

engineer had set a good example to <strong>the</strong> crew by<br />

wearing goggles while in <strong>the</strong> vicinity <strong>of</strong> <strong>the</strong> work.<br />

Masters should be given clear guidelines about<br />

reporting on-going medical problems to head<br />

<strong>of</strong>fice. The fact that <strong>the</strong> second engineer’s condition<br />

did not improve quickly should have been cause<br />

for concern. If <strong>the</strong> second engineer had been<br />

repatriated earlier he may not have lost <strong>the</strong> sight <strong>of</strong><br />

his eye.<br />

Root Cause:<br />

Human Error.<br />

Financial Cost:<br />

Although <strong>the</strong> engineer received benefits from<br />

his State’s welfare system <strong>the</strong> cost to <strong>the</strong> owners<br />

exceeded US$25,000.<br />

Issue Date:01/01/02<br />

Case No.21940<br />

178 179


Navigation<br />

Close Quarters Manoeuvring Results in Sinking<br />

The Incident:<br />

This anchor handling supply vessel had been<br />

chartered to deploy anchors for a pipelaying barge<br />

operating in shallow water. In addition to <strong>the</strong> new<br />

pipeline <strong>the</strong>re was an old pipeline and an unmarked<br />

subsea wellhead in <strong>the</strong> vicinity. While retrieving one<br />

<strong>of</strong> <strong>the</strong> barge’s anchors <strong>the</strong> anchor handler hit <strong>the</strong><br />

wellhead, breaching <strong>the</strong> engine room. The vessel’s<br />

pumps could not keep up with <strong>the</strong> ingress <strong>of</strong> water<br />

and it sank to <strong>the</strong> seabed impaled on <strong>the</strong> wellhead.<br />

Observations:<br />

A few days before <strong>the</strong> incident occurred <strong>the</strong> barge<br />

Master had given <strong>the</strong> Master a new chart <strong>of</strong> <strong>the</strong><br />

working area. Although <strong>the</strong> well’s position was<br />

accurately shown to within a metre <strong>the</strong> depth<br />

information was incorrect, leading <strong>the</strong> Master to<br />

believe that he would have an underkeel clearance<br />

<strong>of</strong> approximately two metres when in fact he had<br />

none. The barge was equipped with a sophisticated<br />

positioning system utilising differential GPS which<br />

was accurate to +/- 3 metres. Additional equipment<br />

on board <strong>the</strong> anchor handler allowed <strong>the</strong> surveyors<br />

on <strong>the</strong> barge to monitor <strong>the</strong> position <strong>of</strong> <strong>the</strong> anchor<br />

handler’s stern roller, enabling <strong>the</strong>m to position <strong>the</strong><br />

anchors with great accuracy. The anchor handler<br />

however was not given a monitor and had no way<br />

<strong>of</strong> accessing this information. The wellhead was<br />

not buoyed and <strong>the</strong> Master had no visual reference<br />

o<strong>the</strong>r than <strong>the</strong> barge. As a result he had been<br />

manoeuvring solely on <strong>the</strong> orders <strong>of</strong> <strong>the</strong> barge.<br />

Modern position fixing systems permit many<br />

operations to take place in closer proximity to<br />

navigational hazards than was possible in <strong>the</strong> past.<br />

Offshore personnel must however remain aware <strong>of</strong><br />

<strong>the</strong> practical problems in accurately manoeuvring<br />

a large anchor handler without visual reference. In<br />

this case <strong>the</strong> anchor had been positioned only 30<br />

metres from <strong>the</strong> wellhead, with <strong>the</strong> result that <strong>the</strong><br />

Master was required to manoeuvre his vessel within<br />

less than half a ship’s length <strong>of</strong> <strong>the</strong> hazard without<br />

<strong>the</strong> benefit <strong>of</strong> a visual reference or a GPS monitor.<br />

This incident could have been avoided if divers<br />

had checked <strong>the</strong> depth over <strong>the</strong> wellhead and its<br />

position had been marked with a buoy.<br />

Root Cause:<br />

Inadequate third party procedures.<br />

Financial Cost:<br />

The anchor handler valued at approximately US$3<br />

million was a total loss. In addition to this <strong>the</strong> costs<br />

<strong>of</strong> removing <strong>the</strong> wreck from <strong>the</strong> wellhead and<br />

disposing <strong>of</strong> it exceeded US$2.25 million.<br />

Issue Date:01/01/02<br />

Case No.21777<br />

180 181


Navigation<br />

A Good Case for Adequate Bridge Manning<br />

The Incident:<br />

This claim involved a small dredger operating a<br />

three times a week service between two local<br />

ports. She was manned by a senior and junior<br />

Master, two engineers and two ABs who were split<br />

into two teams <strong>of</strong> three, operating a six on, six <strong>of</strong>f<br />

watchkeeping rota.<br />

At <strong>the</strong> time in question <strong>the</strong> junior Master, at <strong>the</strong><br />

request <strong>of</strong> <strong>the</strong> senior Master, had taken <strong>the</strong> bridge<br />

watch early upon <strong>the</strong> vessel’s departure from <strong>the</strong><br />

berth at 1745.<br />

As <strong>the</strong> vessel proceeded down a buoyed channel<br />

<strong>the</strong> VTS observed that <strong>the</strong> vessel was straying to<br />

port <strong>of</strong> her advised track and unsuccessful efforts<br />

were made to alert <strong>the</strong> vessel. Shortly <strong>the</strong>reafter<br />

<strong>the</strong> vessel should have made a substantial alteration<br />

<strong>of</strong> course to port, but did not make <strong>the</strong> turn,<br />

instead headed across <strong>the</strong> main shipping channel<br />

and towards a pier and shallow waters. The VTS<br />

again tried to make contact with <strong>the</strong> vessel to<br />

advise <strong>of</strong> <strong>the</strong> impending danger but no response<br />

was received. After narrowly missing a marina <strong>the</strong><br />

vessel collided with a pier, causing severe structural<br />

damage. Fortunately no injuries were sustained.<br />

Observations:<br />

The <strong>of</strong>ficial investigation into <strong>the</strong> cause <strong>of</strong> this<br />

incident found that <strong>the</strong> junior Master had very little<br />

recollection <strong>of</strong> events. It was concluded that his<br />

performance was greatly reduced through a possible<br />

combination <strong>of</strong> tiredness, alcohol consumption<br />

prior to taking over <strong>the</strong> watch and <strong>the</strong> taking <strong>of</strong><br />

prescribed medication. In addition, at <strong>the</strong> time <strong>of</strong> <strong>the</strong><br />

incident he was <strong>the</strong> sole watchkeeper on <strong>the</strong> bridge<br />

after <strong>the</strong> AB had left following an altercation.<br />

The vessel complied with <strong>the</strong> minimum manning<br />

requirements <strong>of</strong> <strong>the</strong> governing authority however<br />

<strong>the</strong> rest periods as required by <strong>the</strong> Hours <strong>of</strong><br />

Work regulations were not being fully met for<br />

a number <strong>of</strong> reasons. The junior Master had<br />

been ashore immediately prior to <strong>the</strong> vessel’s<br />

departure consuming alcohol and he was also<br />

taking anti-depressants.<br />

As is <strong>the</strong> case with <strong>the</strong>se incidents, <strong>the</strong> causation<br />

was a collection <strong>of</strong> factors, not least <strong>of</strong> all bridge<br />

manning that did not comply with <strong>the</strong> regulations,<br />

<strong>the</strong> sole bridge watchkeeper having consumed<br />

sufficient alcohol to exceed <strong>the</strong> legal road driving<br />

limits and an element <strong>of</strong> tiredness due to poor use<br />

<strong>of</strong> <strong>of</strong>f-duty periods.<br />

Members are advised to ensure that <strong>the</strong>ir vessels<br />

are manned so that all regulatory requirements can<br />

be met and Masters instructed accordingly. This case<br />

has shown that familiarity with a navigating area is<br />

not an excuse for allowing standards to slip.<br />

Root Cause:<br />

Inadequate Navigation Lookout.<br />

Financial Cost:<br />

US$795,000<br />

Issue Date: 27/10/05<br />

Case No. 41728<br />

182 183


Navigation<br />

Keeping a Proper Lookout at ALL Times<br />

The Incident:<br />

This incident involved a harbour tug which collided with a moored tanker.<br />

The tug had completed one assignment and was crossing <strong>the</strong> port to its next job. The<br />

skipper was assisted on <strong>the</strong> bridge by a deck hand, who prior to <strong>the</strong> incident had a<br />

prolonged toilet break. The skipper made a final alteration <strong>of</strong> course towards <strong>the</strong> vessel<br />

she was to assist. Shortly afterwards <strong>the</strong> tug collided head on with a vessel moored at<br />

<strong>the</strong> terminal. This caused damage to some sections <strong>of</strong> <strong>the</strong> tanker’s shell plating and <strong>the</strong><br />

vessel had to be taken out <strong>of</strong> service for repairs. Fortunately no-one was hurt.<br />

Observations:<br />

The Master and crew man stated that <strong>the</strong>y had<br />

fallen asleep in <strong>the</strong> period between <strong>the</strong> alteration <strong>of</strong><br />

course and <strong>the</strong> collision, although this was at most<br />

six minutes. Notwithstanding <strong>the</strong> reason, <strong>the</strong> fact<br />

is that an effective lookout was not kept on <strong>the</strong> tug<br />

and it is very fortunate that <strong>the</strong> result <strong>of</strong> <strong>the</strong> collision<br />

was not a lot worse than it was.<br />

The importance <strong>of</strong> keeping a good lookout at all<br />

times on all types <strong>of</strong> vessels when underway cannot<br />

be over emphasised. It also raises <strong>the</strong> ever present<br />

question <strong>of</strong> fatigue which must not be ignored.<br />

Root Cause:<br />

Inadequate navigational lookout.<br />

Financial Cost:<br />

The claim was settled for US$200,000<br />

Issue Date: 30/08/05<br />

Case No. 46140<br />

184 185


Navigation<br />

A Moment’s Lapse <strong>of</strong> Concentration Causes Collision<br />

The Incident:<br />

The supply vessel in question<br />

had been chartered by a drilling<br />

contractor to service a semisubmersible<br />

rig. The barge Master<br />

<strong>of</strong> <strong>the</strong> rig had instructed <strong>the</strong><br />

supply vessel to act as safety boat<br />

on <strong>the</strong> starboard side <strong>of</strong> <strong>the</strong> rig<br />

while service personnel worked<br />

on a flare boom. The supply<br />

vessel was being manoeuvred in<br />

close proximity to <strong>the</strong> rig by an<br />

experienced Master.<br />

Some <strong>of</strong> <strong>the</strong> supply vessel’s crew<br />

were using a hose to wash down<br />

<strong>the</strong> bridge and accommodation<br />

block. Water from <strong>the</strong>ir hose<br />

came into <strong>the</strong> bridge through an<br />

open bridge wing door, splashing<br />

<strong>the</strong> radar and o<strong>the</strong>r electrical<br />

equipment. The Master left <strong>the</strong><br />

aft controls to close <strong>the</strong> door but<br />

in that short period <strong>the</strong> vessel<br />

moved astern and <strong>the</strong> port<br />

quarter came into contact with<br />

<strong>the</strong> centre starboard column <strong>of</strong><br />

<strong>the</strong> semi-submersible.<br />

Observations:<br />

This incident highlights <strong>the</strong> risks <strong>of</strong> a momentary<br />

lapse <strong>of</strong> attention on <strong>the</strong> part <strong>of</strong> <strong>the</strong> <strong>of</strong>ficer in charge<br />

when manoeuvring in very close proximity to o<strong>the</strong>r<br />

vessels or structures. The incident would not have<br />

occurred if <strong>the</strong> Master had ignored <strong>the</strong> distraction<br />

and not left <strong>the</strong> controls. The Master should have<br />

used <strong>the</strong> deck loudhailer system to draw <strong>the</strong><br />

attention <strong>of</strong> <strong>the</strong> crew to <strong>the</strong> problem.<br />

Root Cause:<br />

Human error.<br />

Financial Cost:<br />

Repairs to <strong>the</strong> rig alone cost US$55,000 and by <strong>the</strong><br />

time surveyors’ fees and o<strong>the</strong>r costs had been taken<br />

into account <strong>the</strong> total cost to <strong>the</strong> owner was over<br />

US$60,000.<br />

Issue Date:01/01/02<br />

Case No.23178<br />

186 187


Navigation<br />

Thruster Failure Causes Rig Damage<br />

The Incident:<br />

This vessel was one <strong>of</strong> two anchor handlers shifting a semisubmersible<br />

rig. Conditions were not ideal. A strong wind was<br />

blowing on <strong>the</strong> port bow <strong>of</strong> <strong>the</strong> rig and a current <strong>of</strong> over 1 knot<br />

setting onto that side. The anchor handler was ordered to retrieve<br />

<strong>the</strong> no. 2 anchor on <strong>the</strong> port side which was run out at an angle <strong>of</strong><br />

about 60° from <strong>the</strong> rig’s centre line. The anchor was lifted clear <strong>of</strong> <strong>the</strong><br />

bottom and hauled up to <strong>the</strong> stern roller. The tug <strong>the</strong>n manoeuvred<br />

slowly astern towards <strong>the</strong> rig while <strong>the</strong> anchor chain was being<br />

recovered by <strong>the</strong> windlass on <strong>the</strong> rig. As <strong>the</strong> tug approached <strong>the</strong> rig<br />

<strong>the</strong> barge Master asked that it swing aft to a position on <strong>the</strong> beam<br />

<strong>of</strong> <strong>the</strong> rig in order to give a better clearance to <strong>the</strong> no. 1 port side<br />

anchor wire. This brought <strong>the</strong> wind onto <strong>the</strong> beam <strong>of</strong> <strong>the</strong> anchor<br />

handler. To hold this position required full power from <strong>the</strong> bow<br />

thruster which started to overheat and eventually tripped out,<br />

with <strong>the</strong> result that <strong>the</strong> bow fell <strong>of</strong>f <strong>the</strong> wind. The loss <strong>of</strong> <strong>the</strong> bow<br />

thruster made <strong>the</strong> supply vessel difficult to manoeuvre. Attempts<br />

were made to pass <strong>the</strong> anchor pennant wire to <strong>the</strong> barge crane,<br />

however <strong>the</strong> shark’s jaws malfunctioned and <strong>the</strong> pennant wire could<br />

not be released. The tug, pinned by <strong>the</strong> anchor wire at <strong>the</strong> stern,<br />

was swept down onto <strong>the</strong> rig by wind and tide. She landed heavily on<br />

<strong>the</strong> port side ranging up and down causing severe damage.<br />

Observations:<br />

This incident shows how a number <strong>of</strong> factors can<br />

<strong>of</strong>ten combine to create a serious incident. It also<br />

emphasises <strong>the</strong> need to ensure that equipment<br />

is properly maintained in full working order,<br />

particularly when close quarters manoeuvring is<br />

envisaged. Although this was <strong>the</strong> first time <strong>the</strong><br />

shark’s jaws had failed, overheating was a recurrent<br />

problem with <strong>the</strong> bow thruster which had never<br />

been properly repaired. In this case failure <strong>of</strong> ei<strong>the</strong>r<br />

<strong>the</strong> bow thruster or <strong>the</strong> shark’s jaws alone would<br />

not have resulted in a collision, but when <strong>the</strong> effects<br />

<strong>of</strong> <strong>the</strong> two were combined when <strong>the</strong> vessel was in<br />

close proximity to <strong>the</strong> rig it became inevitable.<br />

Root Cause:<br />

Insufficient maintenance<br />

programme.<br />

Financial Cost:<br />

The rig was out <strong>of</strong> action for<br />

10½ days. The claim for damage<br />

and loss <strong>of</strong> use exceeded <strong>the</strong><br />

tug’s limitation fund under <strong>the</strong><br />

1976 Convention. The claim was<br />

settled for <strong>the</strong> limitation fund<br />

but never<strong>the</strong>less <strong>the</strong> total cost<br />

exceeded US$450,000. The tug<br />

itself suffered heavy damage as a<br />

result <strong>of</strong> <strong>the</strong> collision.<br />

Issue Date:01/01/02<br />

Case No.23047<br />

188 189


Navigation<br />

Tidal Calculation Error Results in Bridge Damage<br />

The Incident:<br />

A coastal tug towing a barge<br />

carrying 6,000 tons <strong>of</strong> cargo<br />

encountered difficulties<br />

manoeuvring on <strong>the</strong> way up<br />

river at her destination. The tug<br />

lost control <strong>of</strong> <strong>the</strong> barge which<br />

collided with a swing railway<br />

bride causing damage valued at<br />

US$180,000.<br />

The tug had brought <strong>the</strong> barge<br />

up <strong>the</strong> coast, arriving <strong>of</strong>f <strong>the</strong> river<br />

mouth at midday. Before starting<br />

up <strong>the</strong> river <strong>the</strong> tug Master<br />

shortened up <strong>the</strong> tow, bringing<br />

<strong>the</strong> tow line right in until only <strong>the</strong><br />

bridle remained out board - this<br />

brought <strong>the</strong> swim bow <strong>of</strong> <strong>the</strong><br />

barge close up to <strong>the</strong> stern <strong>of</strong><br />

<strong>the</strong> tug. The tug and barge <strong>the</strong>n<br />

proceeded at slow speed up <strong>the</strong><br />

north arm <strong>of</strong> <strong>the</strong> Fraser river,<br />

aiming to arrive below <strong>the</strong> Arthur<br />

Laing Bridge after <strong>the</strong> ebb had<br />

started to flow. Arrangements<br />

had been made for a harbour tug<br />

to rendezvous with <strong>the</strong> flotilla<br />

at this point to assist <strong>the</strong>m in<br />

rounding <strong>the</strong> bend and passing<br />

through <strong>the</strong> Marpole swing<br />

railway bridge. Despite <strong>the</strong> lead<br />

tug plying full helm and maximum<br />

power <strong>the</strong> flotilla failed to<br />

complete <strong>the</strong> turn and <strong>the</strong> barge<br />

struck <strong>the</strong> swing span protection<br />

pier, causing serious damage.<br />

Observations:<br />

The reasons why <strong>the</strong> barge<br />

did not negotiate <strong>the</strong> turn<br />

successfully have never been fully<br />

explained. There were however<br />

a number <strong>of</strong> factors which<br />

contributed to <strong>the</strong> accident.<br />

Both tug skippers had carried out<br />

this operation many times before.<br />

Perhaps because <strong>of</strong> this <strong>the</strong>re<br />

was no communication between<br />

<strong>the</strong> skippers when <strong>the</strong>y met and<br />

no instructions were given by <strong>the</strong><br />

lead tug.<br />

This unsatisfactory situation was<br />

compounded by <strong>the</strong> fact that <strong>the</strong><br />

barge completely blocked <strong>the</strong><br />

coastal tug’s view astern, with <strong>the</strong><br />

result that its skipper was unable<br />

to see where <strong>the</strong> assist tug was<br />

pushing. The primary function <strong>of</strong><br />

<strong>the</strong> assist tug is to help hold <strong>the</strong><br />

barge close to <strong>the</strong> north side <strong>of</strong><br />

<strong>the</strong> channel. If <strong>the</strong> assist tug pushes<br />

too far aft on <strong>the</strong> barge’s side it<br />

counteracts <strong>the</strong> lead tug’s efforts<br />

to pull <strong>the</strong> barge’s head round.<br />

Tidal streams upriver are less<br />

predictable than at <strong>the</strong> river<br />

mouth. The flotilla may have<br />

arrived at <strong>the</strong> turn too early,<br />

before <strong>the</strong> flood had ceased.<br />

The last <strong>of</strong> <strong>the</strong> flood tends to flow<br />

from north to south across <strong>the</strong><br />

basin between <strong>the</strong> bridges, which<br />

would have set <strong>the</strong> flotilla sideways<br />

down on to <strong>the</strong> railway bridge.<br />

The incident could have been<br />

avoided by delaying <strong>the</strong> flotilla’s<br />

arrival until <strong>the</strong> ebb was flowing<br />

strongly and by proper planning<br />

and better communication<br />

between <strong>the</strong> tug skippers.<br />

Root Cause:<br />

Inadequate operational planning.<br />

Issue Date: 01/01/02<br />

Case No.16344<br />

190 191


Navigation<br />

Master’s Failure to take Control Causes Dock Damage<br />

The Incident:<br />

A large cargo handling crane constructed in China was being transported to a new berth<br />

in South East Asia on <strong>the</strong> deck <strong>of</strong> a large ocean-going barge. Pilotage was compulsory at<br />

<strong>the</strong> port <strong>of</strong> destination and as <strong>the</strong> tug and barge combination approached its berth <strong>the</strong><br />

vessel was effectively being controlled by <strong>the</strong> pilot. To assist <strong>the</strong> tug Master a company<br />

superintendent had been stationed on <strong>the</strong> barge itself and was in radio contact with <strong>the</strong><br />

tug. In <strong>the</strong> final stages <strong>of</strong> <strong>the</strong> approach it became apparent to <strong>the</strong> superintendent that<br />

<strong>the</strong> angle <strong>of</strong> approach was too steep and <strong>the</strong> speed was too great. This information was<br />

passed to <strong>the</strong> Captain <strong>of</strong> <strong>the</strong> tug who requested <strong>the</strong> pilot abort <strong>the</strong> berthing manoeuvre.<br />

The pilot refused to do so. The Master did not take control <strong>of</strong> <strong>the</strong> situation and allowed<br />

<strong>the</strong> manoeuvre to continue. The barge made heavy contact with <strong>the</strong> dock, causing<br />

damage to <strong>the</strong> fendering system.<br />

Observations:<br />

National laws and Port bye-laws normally hold<br />

vessels strictly liable for damage done to harbour<br />

works. The relevant law in this case provided “any<br />

damage done to wharves ..... by a vessel whe<strong>the</strong>r<br />

due to <strong>the</strong> incompetence or carelessness <strong>of</strong> <strong>the</strong><br />

authority pilot .... shall be made good by <strong>the</strong> owner,<br />

Master or agent <strong>of</strong> <strong>the</strong> vessel”.<br />

In any event pilots invariably contract on terms<br />

which severely limit <strong>the</strong>ir liability or absolve <strong>the</strong>m<br />

entirely <strong>of</strong> responsibility for <strong>the</strong>ir actions. A pilot’s<br />

function is to advise and assist <strong>the</strong> vessel’s Master,<br />

who remains ultimately responsible for <strong>the</strong> handling<br />

<strong>of</strong> his vessel. The Master should have taken control<br />

and aborted <strong>the</strong> manoeuvre.<br />

Root Cause:<br />

Human error.<br />

Financial Cost:<br />

The Port Authority’s claim exceeded US$50,000.<br />

On this occasion however <strong>the</strong>y did accept that <strong>the</strong><br />

pilot was largely to blame and <strong>the</strong> agreed to settle<br />

for two thirds <strong>of</strong> <strong>the</strong> actual repair costs. The pilot<br />

concerned was subsequently sacked.<br />

Issue Date:01/01/02<br />

Case No.23774<br />

192 193


Navigation<br />

Grounding/Pollution because <strong>of</strong> Bad Lookout<br />

The Incident:<br />

This incident involves <strong>the</strong><br />

accidental grounding <strong>of</strong><br />

a rig standby vessel in an<br />

environmentally sensitive<br />

area. The vessel which was<br />

carrying 160 tons <strong>of</strong> oil at<br />

<strong>the</strong> time suffered extensive<br />

bottom damage and her engine<br />

room was flooded. Pollution<br />

prevention measures were<br />

immediately put in place and <strong>the</strong><br />

vessel was finally salvaged.<br />

Observations:<br />

The vessel had been returning to her home port<br />

with <strong>the</strong> Master as sole watchkeeper. As he<br />

approached land <strong>the</strong> Master moved to <strong>the</strong> after<br />

end <strong>of</strong> <strong>the</strong> wheelhouse to make a radio telephone<br />

call. What <strong>the</strong> Master believed would be a short call<br />

proved more complex than expected. The Master<br />

lost track <strong>of</strong> time and <strong>the</strong> vessel continued under<br />

autopilot, eventually driving itself hard aground<br />

at full speed at <strong>the</strong> base <strong>of</strong> cliffs adjacent to <strong>the</strong><br />

port. This incident occurred as a direct result <strong>of</strong><br />

<strong>the</strong> Master’s failure to keep a proper lookout and<br />

maintain a safe navigational watch. The accident<br />

could have been avoided by augmenting <strong>the</strong> bridge<br />

watch to cope safely with <strong>the</strong> additional workload as<br />

<strong>the</strong> vessel closed <strong>the</strong> land.<br />

Root Cause:<br />

Failure to maintain proper lookout.<br />

Financial Cost:<br />

The cost <strong>of</strong> salving and repairing <strong>the</strong> vessel<br />

exceeded US$2.3 million. Anti-pollution measures<br />

added a fur<strong>the</strong>r US$50,000 to <strong>the</strong> bill.<br />

Issue Date:01/01/02<br />

Case No.12868<br />

194 195


Navigation<br />

Knock for Knock Clause Fails to Protect Owner from Rig Damage Claim<br />

The Incident:<br />

The incident occurred as a supply vessel was<br />

backloading drill casing from a semi-submersible<br />

rig. The vessel was backed up to <strong>the</strong> rig with her<br />

stern into <strong>the</strong> prevailing current and <strong>the</strong> wind on<br />

her port quarter. The vessel was being held in<br />

position by her engines and bow thruster.<br />

During cargo transfer operations <strong>the</strong> port engine<br />

pitch control failed and although its control was<br />

set to give forward thrust, <strong>the</strong> pitch moved to<br />

full astern. Despite <strong>the</strong> Master’s prompt actions<br />

in declutching <strong>the</strong> engine and applying full ahead<br />

power on <strong>the</strong> starboard engine, <strong>the</strong> vessel collided<br />

with and seriously damaged <strong>the</strong> rig leg.<br />

Observations:<br />

This incident highlights <strong>the</strong><br />

risks inherent in close quarters<br />

manoeuvring. In this particular<br />

situation <strong>the</strong>re was little more<br />

that <strong>the</strong> Master could have done<br />

to avoid <strong>the</strong> collision. The vessel’s<br />

pitch control was arranged in <strong>the</strong><br />

‘conventional’ manner with <strong>the</strong><br />

fail-safe position being full astern.<br />

For rig supply vessels however<br />

<strong>the</strong> greatest danger arises when<br />

<strong>the</strong> vessel is backed up to a rig<br />

and for this reason it is generally<br />

considered good practice for <strong>the</strong>se<br />

vessels’ pitch controls to fail-safe to<br />

<strong>the</strong> full ahead position. Although<br />

<strong>the</strong>re was a knock-for-knock clause<br />

in <strong>the</strong> charterparty its effect was<br />

restricted to claims between <strong>the</strong><br />

owners <strong>of</strong> <strong>the</strong> supply vessel and<br />

<strong>the</strong> charterers in relation to <strong>the</strong>ir<br />

respective personnel and property.<br />

In this case <strong>the</strong> rig was not <strong>the</strong><br />

charterer’s property and <strong>the</strong> rig’s<br />

owners were not bound by those<br />

contractual terms. If <strong>the</strong> knockfor-knock<br />

clause had been worded<br />

in such a way as to include <strong>the</strong><br />

contractors and sub-contractors <strong>of</strong><br />

each party, <strong>the</strong>n <strong>the</strong> owners <strong>of</strong> <strong>the</strong><br />

supply boat would not have had to<br />

pay for <strong>the</strong> damage to <strong>the</strong> rig.<br />

Financial Cost:<br />

Repairs to <strong>the</strong> rig were carried<br />

out concurrently with a routine<br />

refit. Never<strong>the</strong>less by <strong>the</strong> time<br />

surveyors’ fees and classification<br />

survey costs had been taken into<br />

account <strong>the</strong> total cost rose to<br />

almost US$160,000.<br />

Issue Date:01/01/02<br />

Case No.25250<br />

196 197


Miscellaneous<br />

When is a Master Off Duty<br />

The Incident:<br />

Whilst alongside a lay-by berth<br />

on <strong>the</strong> UK east coast, <strong>the</strong> Master<br />

<strong>of</strong> an oil rig supply vessel was<br />

informed by charterers that<br />

<strong>the</strong> vessel was not required<br />

for working until <strong>the</strong> following<br />

morning. As usual on this vessel<br />

under such circumstances <strong>the</strong><br />

Chief Officer went on duty for<br />

<strong>the</strong> night and deck and engine<br />

port watches were set.<br />

The Master went ashore and<br />

returned some time later in <strong>the</strong><br />

evening having consumed three<br />

or four pints <strong>of</strong> beer. Some<br />

hours after his return an incident<br />

occurred that necessitated police<br />

attendance. However, despite <strong>the</strong><br />

incident not involving <strong>the</strong> Master<br />

he was breathalysed by <strong>the</strong> police<br />

and arrested and charged on<br />

suspicion <strong>of</strong> being a pr<strong>of</strong>essional<br />

Master <strong>of</strong> a ship while on duty<br />

with a proportion <strong>of</strong> alcohol in his<br />

breath which exceeded <strong>the</strong><br />

prescribed limits <strong>of</strong> 35 micrograms<br />

<strong>of</strong> alcohol in 100 millilitres <strong>of</strong><br />

blood, contrary to Section 78.1(a)<br />

<strong>of</strong> <strong>the</strong> United Kingdom’s “Railways<br />

and Transport Safety Act 2003”.<br />

A fur<strong>the</strong>r test at <strong>the</strong> police station<br />

confirmed that he was over <strong>the</strong><br />

prescribed limit.<br />

A forensic toxicology report<br />

indicated that <strong>the</strong> Master would<br />

have been below <strong>the</strong> prescribed<br />

limit at 08:00 <strong>the</strong> following day<br />

when he was due to come back<br />

on duty. Fur<strong>the</strong>rmore, <strong>the</strong> amount<br />

<strong>of</strong> alcohol consumed did not put<br />

him in breach <strong>of</strong> his Company’s<br />

Drug and Alcohol Regulations.<br />

The case was tried in <strong>the</strong> local<br />

Magistrates Court before a<br />

District Judge.<br />

The case turned on whe<strong>the</strong>r <strong>the</strong><br />

Master was ‘always on duty’ and<br />

particularly whe<strong>the</strong>r he was always<br />

on duty for <strong>the</strong> purposes <strong>of</strong> <strong>the</strong> Act.<br />

The Act did not define ‘duty’ and<br />

fur<strong>the</strong>rmore ‘duty’ is not defined<br />

elsewhere. It is <strong>of</strong>ten thought that a<br />

Master is always on duty from <strong>the</strong><br />

moment he/she signs on a vessel to<br />

<strong>the</strong> moment he/she signs <strong>of</strong>f. It was<br />

argued that a Master’s duty was not<br />

unlimited in its b<strong>read</strong>th or scope;<br />

to find o<strong>the</strong>rwise would confuse<br />

performance and discharge <strong>of</strong> duty<br />

with <strong>the</strong> existence <strong>of</strong> a status or<br />

responsibility. Fur<strong>the</strong>rmore, to do<br />

so would fail to distinguish between<br />

<strong>the</strong> different facets <strong>of</strong> a Master’s<br />

duties, which include duties by<br />

common law, statute, regulation,<br />

custom and by contract.<br />

It was argued on behalf <strong>of</strong> <strong>the</strong><br />

Master that <strong>the</strong> correct definition<br />

<strong>of</strong> ‘duty’ for <strong>the</strong> purposes <strong>of</strong> <strong>the</strong><br />

Act is:-<br />

“Whilst on duty means, in <strong>the</strong><br />

course <strong>of</strong> his employment as a<br />

pr<strong>of</strong>essional Master <strong>of</strong> a ship,<br />

performing or being liable to be<br />

called onto perform a safety critical<br />

function, in <strong>the</strong> operation <strong>of</strong> <strong>the</strong><br />

ship, which it is his duty to perform.”<br />

The Judge accepted this definition,<br />

accepted that <strong>the</strong> Master had<br />

not performed any ‘safety critical<br />

functions’ at <strong>the</strong> time he was ‘over<br />

<strong>the</strong> prescribed limit’ and acquitted<br />

<strong>the</strong> Master accordingly.<br />

Whilst <strong>the</strong> definition <strong>of</strong> ‘duty’ put<br />

forward on behalf <strong>of</strong> <strong>the</strong> Master<br />

was accepted by <strong>the</strong> Court,<br />

<strong>the</strong> facts <strong>of</strong> <strong>the</strong> case assisted<br />

<strong>the</strong> Master’s defence, and in<br />

particular:-<br />

The vessel was laid up with<br />

no orders to sail until <strong>the</strong><br />

following morning.<br />

1. The Chief Officer was certified<br />

to act as Master on this<br />

particular vessel.<br />

2. The level <strong>of</strong> alcohol consumed,<br />

whilst over <strong>the</strong> prescribed limit,<br />

was relatively low.<br />

3. The Master complied with<br />

all company regulations and<br />

procedures as regards alcohol.<br />

4. The vessel complied with all<br />

<strong>the</strong> local harbour regulations<br />

and bye-laws.<br />

5. Toxicology tests showed that<br />

<strong>the</strong> Master would have been<br />

sober upon taking up his duties<br />

<strong>the</strong> following morning.<br />

The outcome could have been<br />

different had any <strong>of</strong> <strong>the</strong>se facts<br />

been different, for example, had<br />

<strong>the</strong> Master been breathalysed and<br />

found to be over <strong>the</strong> limit one<br />

hour before sailing.<br />

Therefore whilst it is up to individual<br />

companies to decide whe<strong>the</strong>r <strong>the</strong>y<br />

run dry ships, those that do not still<br />

need to ensure <strong>the</strong>ir staff are fully<br />

aware <strong>of</strong> <strong>the</strong>ir obligations under<br />

<strong>the</strong> Act in addition to any company<br />

procedures that may be in place,<br />

because <strong>the</strong> Master being removed<br />

from his vessel by <strong>the</strong> authorities<br />

can have serious commercial<br />

implications beyond those personal<br />

consequences suffered by <strong>the</strong><br />

Master himself.<br />

Although this case has arisen<br />

under <strong>the</strong> law in <strong>the</strong> UK, similar<br />

legislation exists in many countries<br />

around <strong>the</strong> world and it is<br />

appropriate to circulate it widely.<br />

Issue Date: 15/05/07<br />

Case No. 50052<br />

198 199


Miscellaneous<br />

Early Request for Club Assistance could have Buoyed up Members Defence<br />

The Incident:<br />

During a transit <strong>of</strong> <strong>the</strong> Suez<br />

Canal our Member’s vessels were<br />

alleged to have hit and severely<br />

damaged a navigation buoy.<br />

The first notice that <strong>the</strong> owners had<br />

was a letter from <strong>the</strong> Suez Canal<br />

Authority alleging that <strong>the</strong>ir vessel<br />

had damaged a navigational mark<br />

and inviting <strong>the</strong>m to attend a joint<br />

survey. Our Member contacted<br />

<strong>the</strong> tug Master and <strong>the</strong> pilot, both<br />

<strong>of</strong> whom denied that <strong>the</strong>re had<br />

been any contact. In view <strong>of</strong> this<br />

our Member wrote back to <strong>the</strong><br />

Authority denying liability. A few<br />

weeks later <strong>the</strong>y were shocked to<br />

find that <strong>the</strong> Suez Canal Authority<br />

had unilaterally deducted Egyptian<br />

£89,000 from <strong>the</strong>ir deposit.<br />

At that point <strong>the</strong> Member contacted <strong>the</strong> Club who instructed its<br />

correspondent lawyers in Egypt to defend <strong>the</strong> Member’s interests.<br />

Our lawyers advised that <strong>the</strong>ir past experience was that once <strong>the</strong><br />

deduction had been made and it had been recorded in <strong>the</strong> accounts<br />

<strong>of</strong> <strong>the</strong> Canal Authority, it was almost impossible to persuade<br />

<strong>the</strong>m to re-open <strong>the</strong> case. We were able to demonstrate that our<br />

Member’s vessel’s passed <strong>the</strong> buoy in <strong>the</strong> early hours <strong>of</strong> <strong>the</strong> morning<br />

and that <strong>the</strong> damage was not reported until mid-afternoon. In <strong>the</strong><br />

intervening period <strong>the</strong> entire southbound convoy passed <strong>the</strong> location<br />

<strong>of</strong> <strong>the</strong> buoy and also some <strong>of</strong> <strong>the</strong> northbound ships, any <strong>of</strong> which<br />

could have done <strong>the</strong> damage. The Canal Authority prevented our<br />

correspondents from taking statements from <strong>the</strong> pilot or any o<strong>the</strong>r<br />

canal personnel. They refused to provide any documents, reports<br />

or o<strong>the</strong>r evidence to substantiate <strong>the</strong>ir claim that our Member was<br />

responsible for <strong>the</strong> loss.<br />

The Canal Authorities remained intransigent and faced with an<br />

expensive legal battle which might not be resolved for ten years or<br />

more, <strong>the</strong> Members decided not to pursue <strong>the</strong> matter.<br />

Observations:<br />

Members should be aware that in many parts <strong>of</strong><br />

<strong>the</strong> world Canal Authorities, Harbour Authorities<br />

and o<strong>the</strong>r quasi-governmental bodies enjoy special<br />

status where <strong>the</strong> normal rules <strong>of</strong> business dealing<br />

may not apply. Members encountering problems<br />

with such bodies are advised to obtain assistance<br />

from <strong>the</strong> Club at an early stage while <strong>the</strong> matter is<br />

still open to discussion.<br />

Financial Cost:<br />

The costs to our Member exceeded US$26,000.<br />

Issue Date: 01/01/02<br />

Case No. 21744<br />

200 201


Miscellaneous<br />

A Good Case for Tracking<br />

The Incident:<br />

A Member’s tug was towing a barge laden with coal between ports in South East Asia.<br />

Late one evening whilst on passage she was boarded by a gang <strong>of</strong> ten men, two <strong>of</strong><br />

whom were armed. The crew were tied up and <strong>the</strong> towline to <strong>the</strong> barge cut. The crew<br />

were <strong>the</strong>n taken near to <strong>the</strong> shore in <strong>the</strong> pirates’ speed boat and left to swim ashore,<br />

unharmed. The speed boat returned to <strong>the</strong> barge. The pirates <strong>the</strong>n turned <strong>the</strong> tug<br />

through 180 degrees, presumably heading for a port at which <strong>the</strong>y could disguise <strong>the</strong> tug.<br />

Unknown to <strong>the</strong> pirates, <strong>the</strong> Member had installed a tracking device on <strong>the</strong> tug. Upon her<br />

failure to arrive at <strong>the</strong> discharge port as expected, an investigation was carried out and<br />

it soon became clear to <strong>the</strong> Member what had occurred. The authorities were advised<br />

and within 36 hours both <strong>the</strong> tug and barge (which had been drifting at <strong>the</strong> mercy <strong>of</strong> <strong>the</strong><br />

elements) were located and arrangements made to recover <strong>the</strong>m.<br />

Observations:<br />

The Member’s foresight in equipping <strong>the</strong> tug with<br />

a satellite tracking system prevented a major claim.<br />

The cost <strong>of</strong> installation was recovered from this one<br />

unsuccessful attempt at hijacking <strong>the</strong> tug.<br />

The speed in which recovery was possible clearly<br />

demonstrates <strong>the</strong> value <strong>of</strong> <strong>the</strong> tracking equipment.<br />

The Club would encourage all Members who<br />

operate such vulnerable craft, to consider seriously<br />

installing a satellite tracking system.<br />

Financial Cost:<br />

No claim arose out <strong>of</strong> this incident and<br />

fortuitously all <strong>the</strong> crew were unharmed.<br />

Issue Date: 14/06/0<br />

Case No. 12345<br />

202 203


Miscellaneous<br />

Corrosion Causes Sinking <strong>of</strong> Laid-Up Vessel<br />

The Incident:<br />

This 14 year old vessel had been inactive for three years. She was laid<br />

up unmanned at a shipyard belonging to an associated company. One<br />

morning <strong>the</strong> vessel’s agent noticed that she was listing 15° to port and<br />

reported this to <strong>the</strong> yard. Yard personnel were mobilised to investigate<br />

<strong>the</strong> listing <strong>of</strong> <strong>the</strong> vessel however prior to any remedial action being<br />

possible <strong>the</strong> vessel capsized, landing on her port side on a s<strong>of</strong>t mud<br />

bottom. As <strong>the</strong>re was no-one on board at <strong>the</strong> time she capsized <strong>the</strong>re<br />

were no injuries. Shortly after <strong>the</strong> capsize an oil sheen started to<br />

appear on <strong>the</strong> surface. The Port Authority and <strong>the</strong> shipyard mobilised<br />

<strong>the</strong>ir pollution clean-up team. An oil boom was placed around <strong>the</strong><br />

vicinity <strong>of</strong> <strong>the</strong> capsized vessel and dispersant was sprayed on <strong>the</strong><br />

escaping oil. The Port Authority issued a wreck removal order. The<br />

vessel was salvaged ten days later.<br />

Observations:<br />

An investigation into <strong>the</strong> cause <strong>of</strong> <strong>the</strong> sinking traced <strong>the</strong><br />

source <strong>of</strong> sea water ingress to a small sea water pipe<br />

between <strong>the</strong> sea suction strainer and <strong>the</strong> refrigeration<br />

cooling water pump. During <strong>the</strong> period <strong>the</strong> vessel was<br />

laid up an elbow progressively corroded away at <strong>the</strong><br />

welded seams on ei<strong>the</strong>r side until it was so weakened<br />

that it fell <strong>of</strong>f. The subsequent ingress <strong>of</strong> sea water<br />

slowly flooded <strong>the</strong> engine room space, initially causing<br />

<strong>the</strong> vessel to sink deeper into <strong>the</strong> water and <strong>the</strong>n, as<br />

<strong>the</strong> starboard bilge grounded on <strong>the</strong> uneven bottom,<br />

to list and ultimately capsize.<br />

The loss would have been avoided if good practice<br />

had been followed and all sea valves had been closed<br />

when <strong>the</strong> vessel was laid up. The leak would also have<br />

been detected if <strong>the</strong> owners had made arrangements<br />

with <strong>the</strong> shipyard for regular housekeeping<br />

inspections to be carried out by yard personnel.<br />

Root Cause:<br />

Inadequate Procedure.<br />

Financial Cost:<br />

The owners were fortunate that heavy lifting<br />

equipment was al<strong>read</strong>y available in <strong>the</strong> port, <strong>the</strong>reby<br />

avoiding heavy mobilisation costs. Never<strong>the</strong>less<br />

raising <strong>the</strong> vessel still cost over US$125,000 and <strong>the</strong><br />

cost <strong>of</strong> anti-pollution measures reached US$20,000.<br />

Sea water had destroyed all <strong>the</strong> electrical equipment<br />

and installations and much <strong>of</strong> <strong>the</strong> machinery,<br />

with <strong>the</strong> result that <strong>the</strong> vessel required complete<br />

refurbishment.<br />

Issue Date: 01/01/02<br />

Case No.27691<br />

204 205


Section 6<br />

Harbour Craft<br />

207


Harbour Craft<br />

Personal Injury/Illness<br />

Face <strong>the</strong> Danger<br />

The Incident:<br />

The following accident report issued by <strong>the</strong> MAIB<br />

concerns an incident where a deckhand suffered<br />

multiple fractures to his arm whilst connecting a<br />

tug’s towing wire:<br />

“The tug’s tow rope messenger was led through a<br />

Panama lead, around <strong>the</strong> bits at a 100˚ angle and<br />

on to <strong>the</strong> winch end whipping drum. The drum<br />

end seaman was standing with his back to <strong>the</strong><br />

working part <strong>of</strong> <strong>the</strong> rope and <strong>the</strong> supervisor,<br />

as he hauled on <strong>the</strong> rope.<br />

Unfortunately <strong>the</strong> tug was not paying out slack at<br />

a controlled speed and, feeling <strong>the</strong> strain <strong>of</strong> <strong>the</strong><br />

jerking motion, <strong>the</strong> drum end seaman attempted to<br />

apply more turns to <strong>the</strong> whipping drum. During this<br />

process, <strong>the</strong> messenger rope snapped back, and <strong>the</strong><br />

whiplash <strong>of</strong> <strong>the</strong> working part connected with, and<br />

broke, <strong>the</strong> drum end seaman’s arm.<br />

The supervisor, who was standing in <strong>the</strong> precarious<br />

position <strong>of</strong> <strong>the</strong> bight <strong>of</strong> <strong>the</strong> rope, escaped injury.<br />

Had <strong>the</strong> rope come clear <strong>of</strong> <strong>the</strong> bits, <strong>the</strong> outcome<br />

for him could have been extremely serious.”<br />

Conclusion:<br />

Messenger rope arrangement<br />

1. Stand facing <strong>the</strong> danger: always put <strong>the</strong> winch<br />

between <strong>the</strong> operative and <strong>the</strong> potential danger<br />

zone. This, in itself, creates a safety barrier, allows<br />

full visual contact with <strong>the</strong> mooring team and<br />

surroundings, allows controlled surging on <strong>the</strong><br />

drum end and keeps <strong>the</strong> operative clear <strong>of</strong> <strong>the</strong><br />

working part.<br />

2. Be aware <strong>of</strong> <strong>the</strong> dangers <strong>of</strong> sharp nips – <strong>the</strong>se<br />

cause excess strain on machinery, fittings and<br />

ropes – and use fairleads wherever possible.<br />

3. During our first day at sea, most <strong>of</strong> us were made<br />

aware <strong>of</strong> <strong>the</strong> dangers <strong>of</strong> standing in bights <strong>of</strong> rope;<br />

a brief lapse <strong>of</strong> attention to this ordinary practice<br />

can so easily cause grief.<br />

4. Watch out for shipmates and <strong>the</strong>ir work<br />

practices. Ships operate on efficient teamworking,<br />

part <strong>of</strong> which involves looking out for<br />

our shipmates and recognising potential dangers<br />

to <strong>the</strong>m. It is so much easier to stop bad habits<br />

than to patch up broken bodies.<br />

Issue Date: 24/10/07<br />

Case No. 12349<br />

208 209


Personal Injury/Illness<br />

Girting Capsizes Small Tug<br />

The Incident:<br />

This incident occurred as a small passenger vessel<br />

was being towed from a river into a harbour basin.<br />

This dead tow was being performed by a harbour<br />

tug acting as lead tug and a tug/workboat which<br />

was made fast aft. The Masters <strong>of</strong> <strong>the</strong> two tugs had<br />

agreed that <strong>the</strong> towlines would be shortened <strong>of</strong>f <strong>the</strong><br />

basin entrance and that <strong>the</strong> lead tug would <strong>the</strong>n tow<br />

<strong>the</strong> vessel into <strong>the</strong> basin with <strong>the</strong> workboat holding<br />

<strong>the</strong> stern <strong>of</strong> <strong>the</strong> passenger vessel up into <strong>the</strong> ebb<br />

tide, which was running downriver at approximately<br />

3 knots. As <strong>the</strong>y commenced <strong>the</strong> final stage <strong>of</strong> <strong>the</strong><br />

tow <strong>the</strong> tug/workboat was girted and capsized,<br />

drowning its skipper.<br />

Observations:<br />

Once <strong>the</strong> towline had been shortened and <strong>the</strong><br />

slack had been picked up <strong>the</strong> lead tug called <strong>the</strong><br />

workboat to confirm that <strong>the</strong>y were <strong>read</strong>y to<br />

proceed. On receiving <strong>the</strong> all-clear <strong>the</strong> lead tug<br />

progressively applied power, turning <strong>the</strong> tow into line<br />

with <strong>the</strong> approach. Power had been brought up to<br />

approximately half ahead when <strong>the</strong> tug received a<br />

VHF message asking it to stop. Almost simultaneously<br />

crew members on board <strong>the</strong> tow shouted to <strong>the</strong> lead<br />

tug that <strong>the</strong> workboat had capsized.<br />

Based on information from <strong>the</strong> survivor and<br />

witnesses on <strong>the</strong> tow, it appears that <strong>the</strong> workboat<br />

skipper had intended to let <strong>the</strong> his boat drift into<br />

line with <strong>the</strong> stern <strong>of</strong> <strong>the</strong> passenger vessel as <strong>the</strong><br />

slack on <strong>the</strong> towline was taken up. It seems that <strong>the</strong><br />

workboat did not turn as fast as expected for when<br />

<strong>the</strong> weight came on <strong>the</strong> workboat was still lying at<br />

an angle <strong>of</strong> about 140° to <strong>the</strong> fore and aft line <strong>of</strong><br />

<strong>the</strong> tow. It appears that <strong>the</strong> skipper realising <strong>the</strong><br />

danger abruptly put his engines full ahead intending<br />

to swing his vessel into line with <strong>the</strong> tow. Before<br />

<strong>the</strong> workboat could turn <strong>the</strong> tow started to pull<br />

<strong>the</strong> workboat along with it. The workboat listed<br />

to starboard and a combination <strong>of</strong> <strong>the</strong> workboat’s<br />

engines, <strong>the</strong> river current and <strong>the</strong> forward motion<br />

<strong>of</strong> <strong>the</strong> tow dragged <strong>the</strong> starboard quarter under,<br />

with <strong>the</strong> result that <strong>the</strong> workboat capsized. The<br />

eye <strong>of</strong> <strong>the</strong> towline from <strong>the</strong> passenger vessel to <strong>the</strong><br />

workboat had been placed over <strong>the</strong> bitts. There was<br />

no means <strong>of</strong> releasing <strong>the</strong> towline in an emergency.<br />

Root Cause:<br />

Equipment design failure.<br />

Financial Cost:<br />

The workboat, although eventually refloated, was<br />

a constructive total loss. The measures taken to<br />

prevent pollution toge<strong>the</strong>r with <strong>the</strong> fees <strong>of</strong> lawyers<br />

and consultants exceeded US$14,000. The skipper’s<br />

family was compensated by <strong>the</strong> State Workers’<br />

Compensation scheme.<br />

Footnote: Following <strong>the</strong> incident ano<strong>the</strong>r<br />

Member <strong>of</strong> <strong>the</strong> Club designed an automatic quick<br />

release towing hook specifically for small craft/<br />

workboats. Full details <strong>of</strong> <strong>the</strong> ‘Detach-Matic’<br />

hook can be obtained from Navimar Corporation<br />

Ltee in Quebec, Canada, telephone number<br />

(418) 692 4830.<br />

Issue Date: 01/01/02<br />

Case No. 23773<br />

210 211


Personal Injury/Illness<br />

Personal Injury/Illness<br />

Delayed Action has Painful Result<br />

Handling <strong>of</strong> Heavy Cargo Load Without Rope Tails Leads to Crushed Fingers<br />

The Incident:<br />

This claim involved a work boat<br />

which developed an engine<br />

fault. The fault was reported<br />

to <strong>the</strong> General Manager, who<br />

subsequently arranged for <strong>the</strong><br />

company fitter to attend, although<br />

he could not do so immediately.<br />

The following morning, before <strong>the</strong><br />

fitter had attended and carried<br />

out <strong>the</strong> repairs, a new boatman<br />

took <strong>the</strong> boat out onto <strong>the</strong> water.<br />

Whilst manoeuvring alongside<br />

ano<strong>the</strong>r vessel <strong>the</strong> engine went<br />

astern instead <strong>of</strong> ahead, contrary<br />

to <strong>the</strong> control lever, and <strong>the</strong> boat<br />

landed heavily against <strong>the</strong> vessel<br />

causing <strong>the</strong> boatman to fall. This<br />

incident resulted in <strong>the</strong> crewman<br />

suffering multiple rib fractures and<br />

a broken arm.<br />

Observations:<br />

This incident would not have<br />

occurred if procedures had<br />

been in place to deal with <strong>the</strong><br />

reported fault. In particular<br />

no positive steps had been<br />

taken to prevent <strong>the</strong> boat from<br />

being used prior to <strong>the</strong> fault<br />

being rectified. The General<br />

Manager reportedly gave verbal<br />

instructions not to use <strong>the</strong> boat,<br />

but this clearly was not sufficient.<br />

When any item <strong>of</strong> machinery is<br />

known to be defective, positive<br />

action must be taken to prevent<br />

fur<strong>the</strong>r use until <strong>the</strong> problem<br />

has been rectified. This applies<br />

to all types <strong>of</strong> equipment no<br />

matter how important it is to a<br />

vessel’s operation.<br />

Root Cause:<br />

Inadequate maintenance<br />

procedures.<br />

Issue Date: 19/05/08<br />

Case No. 39892<br />

The Incident:<br />

This incident occurred on board<br />

a harbour craft servicing ships in<br />

<strong>the</strong> anchorage at Singapore. The<br />

vessel had carried a load <strong>of</strong> stores<br />

and spare gear out to <strong>the</strong> oceangoing<br />

vessel and was backloading<br />

a 14 ton piece <strong>of</strong> machinery. The<br />

small vessel was rolling slightly in<br />

<strong>the</strong> swell and while conditions<br />

were not ideal it was considered<br />

safe for <strong>the</strong> operation to proceed.<br />

The machine was lowered from<br />

<strong>the</strong> ocean-going ship to just<br />

above deck level where it was<br />

suspended while our Member’s<br />

crew adjusted its position. One<br />

<strong>of</strong> <strong>the</strong> crew members involved<br />

inadvertently placed his hand<br />

in a position where it could be<br />

trapped and realising <strong>the</strong> danger<br />

immediately tried to retract it,<br />

but his hand was caught by <strong>the</strong><br />

load. Fortunately he was able to<br />

pull his hand clear before <strong>the</strong> full<br />

pressure <strong>of</strong> <strong>the</strong> load came to bear.<br />

Never<strong>the</strong>less he suffered serious<br />

crush injuries to <strong>the</strong> middle and<br />

index fingers <strong>of</strong> his right hand.<br />

Observations:<br />

This incident illustrates <strong>the</strong><br />

dangers that crew members can<br />

be exposed to if <strong>the</strong>y have to<br />

work in close proximity to heavy<br />

loads being landed on deck. If this<br />

load had been fitted with rope<br />

tails it would have allowed <strong>the</strong><br />

crew members to remain at a safe<br />

distance from <strong>the</strong> load while final<br />

positioning was carried out.<br />

Root Cause:<br />

Inadequate safety procedures.<br />

Issue Date: 01/01/02<br />

Case No. 20766<br />

212 213


Operations<br />

Size does matter<br />

The Incident:<br />

This incident occurred when two tugs were employed<br />

in shifting a floating dry dock <strong>of</strong> approximately 3,400<br />

tonnes into deep water so that she could be ballasted<br />

down to sail out a vessel within.<br />

The operation required <strong>the</strong> dock to be manoeuvred<br />

across <strong>the</strong> port approach channel, down which a<br />

supply vessel was navigating. In order to give this<br />

vessel more sea room, <strong>the</strong> tugs towing <strong>the</strong> dock eased<br />

<strong>of</strong>f. The dock <strong>the</strong>n started to drift towards vessels<br />

moored at a nearby berth and despite <strong>the</strong> best efforts<br />

<strong>of</strong> <strong>the</strong> tugs, <strong>the</strong> dock continued towards <strong>the</strong> moored<br />

vessels, eventually making contact with one.<br />

Observations:<br />

Two factors played a part in <strong>the</strong> cause <strong>of</strong><br />

this incident. The bollard pull <strong>of</strong> <strong>the</strong> tugs was<br />

considered insufficient for <strong>the</strong> size <strong>of</strong> <strong>the</strong> dock.<br />

A strong current was flowing at <strong>the</strong> time <strong>of</strong> <strong>the</strong><br />

operation and <strong>the</strong> tugs were not <strong>of</strong> sufficient<br />

power to regain control. Secondly, nei<strong>the</strong>r <strong>the</strong><br />

dry dock operations department nor <strong>the</strong> tug<br />

masters took it upon <strong>the</strong>mselves to inform <strong>the</strong><br />

port control <strong>of</strong> <strong>the</strong> operation.<br />

Had this been done, <strong>the</strong> manoeuvre would<br />

have probably been delayed until <strong>the</strong> channel<br />

was clear or <strong>the</strong> inbound vessel prevented<br />

from entering <strong>the</strong> channel.<br />

Financial Cost:<br />

Whilst damage claimed was extensive we<br />

eventually concluded settlement in <strong>the</strong><br />

modest sum <strong>of</strong> US$14,737.<br />

Trading Area:<br />

Europe and Middle East<br />

Issue Date: 03/02/10<br />

Case No. 44485<br />

All in all <strong>the</strong> operation was very poorly planned.<br />

214 215


Section 7<br />

Barges<br />

217


Barges<br />

Operations<br />

You Get What You Pay For<br />

The Incident:<br />

This incident involved a dumb barge loading<br />

containers using her own gear. Whilst positioning a<br />

20 foot container on <strong>the</strong> barge <strong>the</strong> eye plate used<br />

to secure <strong>the</strong> topping lift block sheared away from<br />

<strong>the</strong> tripod mast. The container, derrick boom and<br />

gear all fell onto containers al<strong>read</strong>y loaded on <strong>the</strong><br />

barge. Three 40 foot and two 20 foot containers<br />

in addition to <strong>the</strong> one being loaded were damaged.<br />

Fortunately <strong>the</strong>re were no injuries to any <strong>of</strong> <strong>the</strong><br />

crew or stevedores.<br />

Observations:<br />

Investigations showed that <strong>the</strong> eye plate appears to<br />

have been repaired some time prior to <strong>the</strong> incident<br />

and <strong>the</strong> standard <strong>of</strong> <strong>the</strong> welding was very poor.<br />

There was minimal penetration in places and <strong>the</strong><br />

remainder <strong>of</strong> <strong>the</strong> welding was uneven. The surveyor<br />

was <strong>of</strong> <strong>the</strong> opinion that <strong>the</strong> repair work had been<br />

carried out by poorly trained personnel. Needless<br />

to say this is entirely unacceptable, especially<br />

when <strong>the</strong> safe working load (SWL) <strong>of</strong> <strong>the</strong> derrick<br />

(approximately 30 tons) is taken into consideration.<br />

Whenever major repairs are carried out on lifting<br />

gear or <strong>the</strong> associated fittings, a specialist company<br />

should be used that employs fully trained staff. Upon<br />

completion <strong>of</strong> <strong>the</strong>se repairs <strong>the</strong> gear should be<br />

pro<strong>of</strong> tested and a record entered in <strong>the</strong> Register <strong>of</strong><br />

Lifting Appliances and Cargo Handling Gear.<br />

Root Cause:<br />

Inadequate maintenance procedures.<br />

Financial Cost:<br />

US$14,541<br />

Issue Date: 22/02/07<br />

Case No. 43088<br />

218 219


Contact Us<br />

London Office<br />

Singapore Office<br />

Vancouver Office<br />

Charles Hume<br />

Chief Executive<br />

Email: charles.hume@shipowners.co.uk<br />

Skype: charles.hume<br />

Ralph Coton<br />

Business Services Director<br />

Email: ralph.coton@shipowners.co.uk<br />

Skype: ralph.d.coton<br />

Ian Edwards<br />

Underwriting Services Development Manager<br />

Email: ian.edwards@shipowners.co.uk<br />

Skype: ian.edwards11<br />

Adam Howe<br />

Underwriting Manager<br />

Email: adam.howe@shipowners.co.uk<br />

Skype: adam.howe18<br />

Britt Pickering<br />

Claims Manager<br />

Email: britt.pickering@shipowners.co.uk<br />

Skype: britt.pickering<br />

Louise Hall<br />

Loss Prevention Manager - London<br />

Email: louise.hall@shipowners.co.uk<br />

Skype: louise.hall4<br />

Simon Swallow<br />

Commercial Director<br />

Email: simon.swallow@shipowners.co.uk<br />

Skype: simon.swallow1<br />

Lawrence Aspinall<br />

Finance Director<br />

Email: lawrence.aspinall@shipowners.co.uk<br />

Skype: lawrence.aspinall<br />

Mark Harrington<br />

Underwriting Manager<br />

Email: mark.harrington@shipowners.co.uk<br />

Skype: mark.harrington83<br />

William Tobin<br />

Underwriting Manager<br />

Email: william.tobin@shipowners.co.uk<br />

Skype: william.tobin3<br />

Kevin Lowe<br />

Finance Manager<br />

Email: kevin.lowe@shipowners.co.uk<br />

Skype: kevin.lowe2983<br />

The <strong>Shipowners</strong>’ Protection Limited<br />

St Clare House, 30-33 Minories,<br />

London, EC3N 1BP<br />

Tel: +44 (0) 207 488 0911<br />

Fax: +44 (0) 207 480 5806<br />

Email: info@shipowners.co.uk<br />

David Heaselden<br />

Principal Officer / Director<br />

Loss Prevention Manager<br />

Email: david.heaselden@shipowners.com.sg<br />

Skype: davidh2009<br />

Steve Randall<br />

General Manager / Director<br />

Email: steve.randall@shipowners.com.sg<br />

Skype: sd.randall<br />

<strong>Shipowners</strong>’ Asia Pte Ltd<br />

6 Temasek Boulevard<br />

#36-05 Suntec Tower 4<br />

Singapore 038986<br />

Tel: +65 (65) 930420<br />

Fax: +65 (65) 930449<br />

Email: info@shipowners.com.sg<br />

www.shipownersclub.com<br />

Rosemary Adams<br />

General Manager / Head <strong>of</strong> Underwriting Vancouver Branch<br />

Email: rosemary.adams@shipownersclub.ca<br />

Skype: rosemary.adams<br />

<strong>Shipowners</strong>’ North America Protection Limited<br />

1157-409 Granville Street<br />

Vancouver, British Columbia<br />

V6C 1T2<br />

Tel: +1 604 681 5999<br />

Fax: +1 604 681 3946<br />

www.shipownersclub.com<br />

Luxembourg Office<br />

Pascal Herrmann<br />

General Manager<br />

Email: pascal.herrmann@shipowners.lu<br />

The <strong>Shipowners</strong>’ Mutual Protection<br />

& Indemnity Association<br />

16 Rue Notre-Dame<br />

L-2240 Luxembourg<br />

Tel: +352 229 7101<br />

Fax: +352 229 7102<br />

Email: info@shipowners.lu<br />

www.shipownersclub.com<br />

www.shipownersclub.com<br />

220


The <strong>Shipowners</strong>’ Protection Limited<br />

St Clare House, 30-33 Minories, London EC3N 1BP<br />

Tel: +44 (0)20 7488 0911 Fax: +44 (0)20 7480 5806<br />

Email: info@shipowners.co.uk<br />

www.shipownersclub.com<br />

October 2010

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