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Loss Prevention<br />
Case Studies
Introduction<br />
Contents<br />
Case studies are summaries <strong>of</strong> claims that have<br />
been notified to <strong>the</strong> Club. We produce <strong>the</strong>se to<br />
raise awareness <strong>of</strong> <strong>the</strong> causation <strong>of</strong> claims and <strong>the</strong>ir<br />
outcome so that o<strong>the</strong>r Members can benefit from <strong>the</strong><br />
misfortune <strong>of</strong> o<strong>the</strong>rs and pass this knowledge on to all<br />
relevant sectors <strong>of</strong> <strong>the</strong>ir organisations.<br />
The case studies within this publication are arranged by vessel type and <strong>the</strong>n<br />
categorised by area <strong>of</strong> claim e.g. Navigation, Personal Injury/Illness and Operations.<br />
We hope that Members will find <strong>the</strong> following compilation <strong>of</strong> case studies useful.<br />
David Heaselden<br />
David Heaselden<br />
Loss Prevention Manager
Section 1<br />
Dry Cargo Vessels<br />
3
Dry Cargo:<br />
Bulk<br />
Personal Injury/Illness<br />
Only Use Equipment for it’s Designated Purpose<br />
The Incident:<br />
In this case <strong>the</strong> barge concerned was secured<br />
alongside, working cargo. A coastal vessel <strong>the</strong>n<br />
entered <strong>the</strong> port and without obtaining permission<br />
from <strong>the</strong> terminal moored alongside (double<br />
banked) to <strong>the</strong> barge. After berthing <strong>the</strong> crew <strong>of</strong><br />
<strong>the</strong> coastal vessel reportedly went ashore by passing<br />
through <strong>the</strong> accommodation <strong>of</strong> <strong>the</strong> barge. It was<br />
at this time (1035 hrs) that <strong>the</strong> crew <strong>of</strong> <strong>the</strong> barge<br />
noticed that a breast line at <strong>the</strong> after end <strong>of</strong> <strong>the</strong><br />
barge had parted and <strong>the</strong>refore proceeded aft to<br />
replace it. Upon arriving at <strong>the</strong> stern <strong>the</strong>y found one<br />
<strong>of</strong> <strong>the</strong> crew members from <strong>the</strong> coastal vessel lying<br />
injured on <strong>the</strong> port side <strong>of</strong> <strong>the</strong> main deck adjacent<br />
to <strong>the</strong> accommodation. It appeared he had been<br />
struck by <strong>the</strong> rope as it parted. The barge’s crew<br />
immediately reported <strong>the</strong> matter to <strong>the</strong>ir shore<br />
<strong>of</strong>fice who in turn informed <strong>the</strong> Hong Kong Marine<br />
Department and o<strong>the</strong>r <strong>of</strong>ficials. Shortly afterwards<br />
police <strong>of</strong>ficers attended <strong>the</strong> barge along with an<br />
ambulance and <strong>the</strong> fire department. Personnel from<br />
<strong>the</strong> ambulance were unable to board <strong>the</strong> barge<br />
on account <strong>of</strong> <strong>the</strong> prevailing heavy sea conditions.<br />
Therefore oxygen equipment was passed to <strong>the</strong><br />
barge’s crew who were duly instructed on its use.<br />
The firemen <strong>the</strong>n boarded <strong>the</strong> barge and hoisted<br />
<strong>the</strong> injured person ashore where he was taken to<br />
hospital. Unfortunately <strong>the</strong> injured person died later<br />
in hospital.<br />
Observations:<br />
The nylon rope (8 inches in circumference) had<br />
been used as a mooring line and was observed in<br />
poor condition. The eye splice had been extensively<br />
cut with only a few strands remaining which were<br />
rust stained. The vessel’s crew noted that <strong>the</strong> rope<br />
had been used for towing prior to being utilised as a<br />
mooring line. It is imperative that ropes are utilised<br />
for <strong>the</strong>ir intended use. Once <strong>the</strong>y have been used<br />
to perform a function <strong>the</strong>y should not be reused<br />
for o<strong>the</strong>r purposes. Ropes should be subject to<br />
regular examination including telltale signs <strong>of</strong> wear<br />
(powdering in <strong>the</strong> case <strong>of</strong> nylon ropes).<br />
Root Cause:<br />
Incorrect use <strong>of</strong> vessel equipment.<br />
Financial Cost:<br />
US$43,362.<br />
Issue Date: 05/02/08<br />
Case No. 50055<br />
4 5
Cargo<br />
Loading During Rain Causes Cargo Claim<br />
The Incident:<br />
A 1,200 ton gearless bulk carrier was discharging her cargo <strong>of</strong> rape seed meal. Shortly<br />
after discharge commenced cargo operations were suspended during a heavy rain<br />
shower. The crew had some difficulties in reopening <strong>the</strong> hatch covers and as a result<br />
discharge was delayed.<br />
Following this incident stevedores requested that discharge continue during periods <strong>of</strong><br />
rain. The Master asked for written authorisation and this was reportedly promised by <strong>the</strong><br />
stevedores. On <strong>the</strong> strength <strong>of</strong> <strong>the</strong> promise <strong>of</strong> a letter <strong>of</strong> authorisation to work in <strong>the</strong><br />
rain <strong>the</strong> Master allowed discharge to continue in <strong>the</strong> rain and made no attempt to cover<br />
<strong>the</strong> hold during lunch breaks.<br />
When a cargo claim for wet damage was presented by <strong>the</strong> consignee <strong>the</strong> stevedores<br />
refuted any knowledge <strong>of</strong> a letter <strong>of</strong> authorisation to permit working during periods <strong>of</strong> rain.<br />
Observations:<br />
The only people with <strong>the</strong> power to authorise <strong>the</strong><br />
discharge <strong>of</strong> water-sensitive cargo during periods <strong>of</strong><br />
rain are <strong>the</strong> shippers or consignees. Stevedores do<br />
not normally have <strong>the</strong> authority to do so.<br />
In many parts <strong>of</strong> <strong>the</strong> world stevedores are paid by<br />
ton <strong>of</strong> cargo loaded or discharged with <strong>the</strong> result<br />
that interruptions to <strong>the</strong> cargo operations because<br />
<strong>of</strong> rain represent a loss <strong>of</strong> income. When requested<br />
to continue loading or discharging water-sensitive<br />
cargoes in <strong>the</strong> rain Masters should ensure that <strong>the</strong>y<br />
have received written authority to do so from <strong>the</strong><br />
shipper or consignee or someone acting with <strong>the</strong>ir<br />
authority. In cases where <strong>the</strong> authorisation is given<br />
by persons o<strong>the</strong>r than <strong>the</strong> shipper or consignee <strong>the</strong><br />
Master should ensure that <strong>the</strong> person authorising<br />
<strong>the</strong> operation has <strong>the</strong> power to do so o<strong>the</strong>rwise<br />
responsibility for damage to <strong>the</strong> cargo may remain<br />
with <strong>the</strong> ship.<br />
Root Cause:<br />
Non compliance with good cargo<br />
operational practices.<br />
Financial Cost:<br />
17.5 tons <strong>of</strong> cargo were damaged with a market<br />
value <strong>of</strong> over US$3,000.<br />
Issue Date: 01/02/02<br />
Case No. 23451<br />
6 7
Navigation<br />
Grounding as a Result <strong>of</strong> Poor Navigational Practices<br />
The Incident:<br />
This case concerns <strong>the</strong> grounding<br />
<strong>of</strong> a vessel in mid-afternoon<br />
during a coastal passage. At <strong>the</strong><br />
time <strong>of</strong> <strong>the</strong> grounding visibility<br />
was good with a light easterly<br />
breeze, smooth sea and no swell.<br />
The Master was on <strong>the</strong> bridge<br />
chatting to <strong>the</strong> <strong>of</strong>ficer <strong>of</strong> <strong>the</strong><br />
watch and <strong>the</strong>re was also a deck<br />
cadet on <strong>the</strong> bridge.<br />
The vessel was on a regular<br />
run between two ports in an<br />
area <strong>of</strong> relatively shallow water,<br />
liberally scattered with coral<br />
reefs. The Admiralty Pilot advises<br />
mariners that charts <strong>of</strong> <strong>the</strong> area<br />
were based on old surveys, (few<br />
systematic surveys have been<br />
carried out), and that much <strong>of</strong><br />
<strong>the</strong> information is derived from<br />
lines <strong>of</strong> soundings taken by vessels<br />
on passage. The working chart<br />
carried <strong>the</strong> following caution:<br />
Unsurveyed Areas<br />
No hydrographic survey has been conducted and<br />
accordingly mariners attempting to enter <strong>the</strong>se<br />
areas should proceed with extreme caution as<br />
unidentified shoals, reefs and o<strong>the</strong>r navigational<br />
hazards may exist.<br />
The chart shows a recommended track for<br />
transiting <strong>the</strong> area which passed to <strong>the</strong> south <strong>of</strong><br />
an <strong>of</strong>fshore reef. The vessel’s course line did not<br />
follow <strong>the</strong> recommended track. Instead <strong>the</strong> Master<br />
inked in a course which cut a corner, passing to <strong>the</strong><br />
north <strong>of</strong> <strong>the</strong> reef through an area clearly marked as<br />
unsurveyed. The Master had apparently regularly<br />
followed that route when a junior <strong>of</strong>fice on a smaller<br />
vessel. His departure from <strong>the</strong> recommended track<br />
was increased by <strong>the</strong> second mate who, after fixing<br />
<strong>the</strong> vessel’s position at 16.00 hrs, decided to alter<br />
course to cut <strong>the</strong> corner even more, taking <strong>the</strong><br />
vessel fur<strong>the</strong>r into unsurveyed waters.<br />
Observations:<br />
The grounding was <strong>the</strong> result <strong>of</strong> sub-standard<br />
navigational practices. The Master and Owners<br />
had allowed a culture <strong>of</strong> corner-cutting to<br />
develop. Subsequent investigation revealed that<br />
recommended tracks were <strong>of</strong>ten ignored when a<br />
straight line between two points would save a little<br />
distance. In many cases this took <strong>the</strong> vessel into<br />
close proximity to shallow water whilst saving only<br />
minimal time and distance.<br />
Numerous o<strong>the</strong>r areas <strong>of</strong> sub-standard navigational<br />
practices were revealed including failure to correct<br />
charts in accordance with <strong>the</strong> latest Notices to<br />
Mariners. This working chart had not been corrected<br />
for over two years and <strong>the</strong> Admiralty Pilot for <strong>the</strong> area<br />
was missing <strong>the</strong> latest supplement which contained<br />
information relevant to <strong>the</strong> area <strong>of</strong> grounding.<br />
In addition it appears that almost total reliance was<br />
placed on GPS despite being in close proximity to<br />
a steep coastline with numerous features, giving a<br />
good clear radar echo and ample opportunity to<br />
take visual bearings. The working chart is endorsed<br />
with <strong>the</strong> caution:<br />
SATELLITE-DERIVED POSITIONS<br />
Positions obtained from satellite navigation<br />
systems are normally referred to <strong>the</strong> WGS Datum;<br />
adjustments for plotting such positions cannot be<br />
determined for this chart. Mariners must determine<br />
<strong>the</strong> position <strong>of</strong> <strong>the</strong>ir vessel in relation to <strong>the</strong> charted<br />
positions <strong>of</strong> dangers and navigational features by<br />
visual or radar means.<br />
Fortunately <strong>the</strong> vessel suffered no major damage in<br />
<strong>the</strong> grounding and was refloated within 12 hours.<br />
The Master was relieved <strong>of</strong> his command.<br />
ROOT CAUSE:<br />
Inadequate navigational practices.<br />
FINANCIAL COST:<br />
Issue Date: 01/02/02<br />
Case No.28862<br />
8 9
Navigation<br />
Intermittent Faults can be more Serious than a Permanent One<br />
The Incident:<br />
The Club has recently dealt with a number <strong>of</strong> claims<br />
that have been caused by known intermittent faults<br />
occurring at <strong>the</strong> wrong time.<br />
This particular incident involved a 500 gt Dry Cargo<br />
vessel fitted with a main engine gearbox.<br />
After loading a cargo <strong>of</strong> stone <strong>the</strong> vessel proceeded<br />
on her laden passage without problem. The discharge<br />
port was located inland from <strong>the</strong> coast requiring<br />
passage through locks and a canal. The vessel entered<br />
<strong>the</strong> lock without event, but upon departing, <strong>the</strong><br />
Master experienced difficulties engaging <strong>the</strong> gearbox<br />
from ahead to astern. After several attempts <strong>the</strong><br />
problem “disappeared” and <strong>the</strong> vessel left <strong>the</strong> lock.<br />
Shortly afterwards <strong>the</strong> decision was taken to<br />
moor <strong>the</strong> vessel alongside a layby berth and whilst<br />
manoeuvring alongside <strong>the</strong> gearbox again failed to<br />
engage astern. As a result <strong>the</strong> vessel made heavy<br />
contact with <strong>the</strong> quay, she came <strong>of</strong>f and after several<br />
fur<strong>the</strong>r attempts <strong>the</strong> gearbox successfully engaged<br />
and <strong>the</strong> vessel was safely ber<strong>the</strong>d.<br />
The damage to <strong>the</strong> vessel was severe enough to<br />
warrant <strong>the</strong> attendance <strong>of</strong> a Class surveyor. As can<br />
be seen from <strong>the</strong> photograph above, <strong>the</strong> quay was<br />
also badly damaged as was a section <strong>of</strong> public road<br />
that ran along it.<br />
Observations:<br />
The Master and Chief Engineer had both recently<br />
joined <strong>the</strong> vessel and were not aware <strong>of</strong> any<br />
previous problems with <strong>the</strong> gearbox. However, <strong>the</strong><br />
vessel’s Superintendent upon hearing <strong>of</strong> <strong>the</strong> incident<br />
advised <strong>the</strong> Master that it was a known problem and<br />
had been experienced on previous occasions.<br />
It is very disappointing to note that <strong>the</strong> previous<br />
Master and Chief Engineer did not consider<br />
problems engaging astern movement <strong>of</strong> <strong>the</strong> vessel<br />
serious enough to warrant advising <strong>the</strong>ir reliefs, or<br />
that <strong>the</strong> ship’s managers via <strong>the</strong> superintendent did<br />
not take any positive action in trying to solve <strong>the</strong><br />
problem. At least <strong>the</strong> relief Master should have been<br />
advised to take suitable precautions until such time<br />
as <strong>the</strong> fault had been rectified.<br />
Root Cause:<br />
Onboard maintenance programme failure.<br />
Financial Cost:<br />
The cost to <strong>the</strong> Member is in excess <strong>of</strong> US$45,000.<br />
Issue Date: 30/07/03<br />
Case No. 39809<br />
The Member was fortunate that <strong>the</strong> incident took<br />
place after entry into <strong>the</strong> lock; if <strong>the</strong> vessel had hit<br />
<strong>the</strong> lock gates <strong>the</strong> incident could have had very<br />
serious repercussions.<br />
Intermittent faults should be considered serious on<br />
two counts. Firstly <strong>the</strong>y are notoriously difficult to<br />
detect and rectify by <strong>the</strong>ir very nature and secondly,<br />
because <strong>the</strong>y are intermittent, complacency arises<br />
and quite <strong>of</strong>ten contingency plans do not take into<br />
account any recurrence, when in fact <strong>the</strong>y should.<br />
10 11
Operations<br />
Crate Dropped During Lowering<br />
The Incident:<br />
Please note that this Case Study<br />
has been provided by The<br />
Nautical Institute’s International<br />
and Confidential Marine Accident<br />
Reporting Scheme (MARS)<br />
- Report No. 200824<br />
On a ship at anchor, a crate<br />
containing machinery spares,<br />
reeved with two webbing<br />
slings, was being lowered into<br />
<strong>the</strong> engine room through <strong>the</strong><br />
engine room hatch using <strong>the</strong><br />
ship’s stores crane. During <strong>the</strong><br />
lowering process, a corner <strong>of</strong><br />
<strong>the</strong> base <strong>of</strong> <strong>the</strong> crate caught on<br />
a section <strong>of</strong> ducting immediately<br />
below <strong>the</strong> hatch coaming,<br />
became unbalanced and tipped<br />
through <strong>the</strong> slings, falling to<br />
<strong>the</strong> deck below. The impact<br />
destroyed <strong>the</strong> crate; however,<br />
<strong>the</strong>re were no injuries or damage<br />
o<strong>the</strong>r than that <strong>the</strong> spares were<br />
rendered unusable.<br />
Root cause/contributory factors<br />
1. Failure to sling <strong>the</strong> crate properly; webbing slings<br />
not tight around <strong>the</strong> top <strong>of</strong> <strong>the</strong> crate;<br />
2. Ship rolling slightly at anchorage, causing <strong>the</strong> crate<br />
to swing during passage through <strong>the</strong> hatch;<br />
3. Failure to conduct/review formal risk assessment<br />
prior to <strong>the</strong> lifting operation;<br />
4. It is thought that <strong>the</strong> spare part was inadequately<br />
secured inside <strong>the</strong> crate and as <strong>the</strong> crate tilted, <strong>the</strong><br />
internal shift <strong>of</strong> weight assisted <strong>the</strong> ‘tipping’ motion;<br />
5. The crate’s height was greater than <strong>the</strong> o<strong>the</strong>r two<br />
dimensions, which made it more prone to tipping;<br />
6. The crate had no fitting to prevent <strong>the</strong> slings from<br />
slipping <strong>of</strong>f in case <strong>the</strong> load became unbalanced;<br />
7. ‘Routine task’ complacency and inadequate<br />
understanding <strong>of</strong> risk assessment among<br />
<strong>the</strong> ratings.<br />
Corrective actions<br />
1. The company issued notices to Masters and<br />
safety bulletins on risk assessment, work planning<br />
and safe lifting techniques.<br />
2. Crane operator familiarisation training was<br />
conducted on board and will be supplemented<br />
by fur<strong>the</strong>r computer based or practical training in<br />
crane operations and rigging/slinging.<br />
3. Permit to work system presently applying only<br />
to lifts within hazardous areas to be extended to<br />
include all lifting tasks.<br />
4. Investigate and solicit vessel proposals for a steel<br />
cage/box to be used for lifting operations into <strong>the</strong><br />
engine room.<br />
Lessons learnt<br />
1. Expensive and relatively fragile components<br />
should be given a higher level <strong>of</strong> planning and<br />
supervision.<br />
2. Although a task review was conducted during<br />
<strong>the</strong> initial work planning, it was not documented<br />
and should have been followed up with a risk<br />
assessment and a tool box meeting.<br />
3. There was a failure to assess <strong>the</strong> risks adequately,<br />
specifically vessel motion and <strong>the</strong> possibility <strong>of</strong> <strong>the</strong><br />
crate contents shifting.<br />
Issue Date: 15/04/08<br />
Case No. 12388<br />
12 13
Miscellaneous<br />
Smoking is Not Good for Your Health<br />
The Incident:<br />
This case involves a vessel on which 1.5 million<br />
cigarettes (150 boxes) were discovered in <strong>the</strong><br />
fore peak hidden under a tarpaulin during a search<br />
by <strong>the</strong> Customs and Federal Police. The search<br />
was thought to be <strong>the</strong> result <strong>of</strong> a ‘tip <strong>of</strong>f’ by <strong>the</strong><br />
European Bureau for Fraud.<br />
During subsequent interviews <strong>the</strong> Master and<br />
Chief Mate denied all knowledge <strong>of</strong> <strong>the</strong> smuggling<br />
but a crew member confessed, admitting full and<br />
sole responsibility. He stated that he purchased <strong>the</strong><br />
cigarettes with money obtained from <strong>the</strong> sale <strong>of</strong><br />
his apartment, transported <strong>the</strong> cigarettes by van<br />
to <strong>the</strong> vessel and brought <strong>the</strong> cigarettes on board<br />
<strong>the</strong> vessel without assistance. He alleged that on<br />
<strong>the</strong> vessel’s arrival in <strong>the</strong> discharge port he was to<br />
liaise with a Russian man only known to him by <strong>the</strong><br />
name <strong>of</strong> ‘Sergei’.<br />
The body was recovered two months later and<br />
despite <strong>the</strong> fact his left ankle was tightly bound<br />
with rope <strong>the</strong> inquest concluded death by<br />
drowning with no obvious signs <strong>of</strong> violence.<br />
Observations:<br />
Criminal charges were initially brought against <strong>the</strong><br />
seaman, <strong>the</strong> Master and our Members. Due to <strong>the</strong><br />
seaman’s death <strong>the</strong> criminal charges against him have<br />
been dropped. No civil charges have been made as<br />
<strong>the</strong> cigarettes have been seized.<br />
Root Cause:<br />
Illegal smuggling.<br />
Financial Cost:<br />
A nominal fine was incurred.<br />
Issue Date: 17/03/08<br />
Case No: 48633<br />
A week later, while <strong>the</strong> authorities were still<br />
investigating <strong>the</strong> case and prior to obtaining an order<br />
to seize <strong>the</strong> vessel or formally make charges, <strong>the</strong><br />
vessel was allowed to depart. During <strong>the</strong> following<br />
voyage <strong>the</strong> seaman concerned went missing. A full<br />
vessel search was immediately made which lead to<br />
<strong>the</strong> discovery <strong>of</strong> a suicide note in his cabin. It stated<br />
again that he was fully and solely responsible.<br />
Article 265 Section 3 <strong>of</strong> <strong>the</strong> Belgian Customs Code<br />
provides that in cases like this Members could be<br />
held vicariously liable for fines and costs which are<br />
imposed on conviction <strong>of</strong> <strong>the</strong> Master. Accordingly, it<br />
may also be possible for Members to be found liable<br />
to pay not only a fine imposed directly on <strong>the</strong>m but<br />
also any fine imposed on <strong>the</strong> Master.<br />
14 15
Dry Cargo:<br />
General<br />
Personal Injury/Illness<br />
Crane Collapse Results in Death <strong>of</strong> Bystander<br />
The Incident:<br />
This incident involves a gearless dry cargo vessel<br />
which had been equipped with a large mobile crane<br />
to enable it to operate at berths without cargo<br />
handling equipment. The crane had been designed<br />
for industrial operations ashore. Its tracks had been<br />
removed and it was temporarily bolted to <strong>the</strong> deck<br />
<strong>of</strong> <strong>the</strong> vessel. The crane was fitted with a jib 120<br />
foot long and had a maximum capacity <strong>of</strong> 136 tons<br />
at an 18 foot radius <strong>of</strong> operation. As a heavy lift was<br />
being discharged <strong>the</strong> vessel listed slightly and <strong>the</strong><br />
crane jib collapsed. The jib fell on a vehicle killing <strong>the</strong><br />
occupant. The ship itself was undamaged but <strong>the</strong><br />
cargo was a total loss.<br />
Observations:<br />
The design <strong>of</strong> <strong>the</strong> crawler crane was typical <strong>of</strong><br />
its type, having a long narrow latticework boom.<br />
These cranes are designed for use on a level steady<br />
surface where <strong>the</strong> boom acts merely as a strut in<br />
compression and is not subjected to sideways or<br />
twisting forces. In this case as <strong>the</strong> load was slowly<br />
swung over <strong>the</strong> vessel’s side, <strong>the</strong> vessel began to<br />
list causing <strong>the</strong> load to swing out <strong>of</strong> <strong>the</strong> plane <strong>of</strong> <strong>the</strong><br />
jib. The list also increased <strong>the</strong> effective radius <strong>of</strong><br />
operation, increasing <strong>the</strong> stress. The combination<br />
<strong>of</strong> increased load and side force caused <strong>the</strong> jib to<br />
fail at its base where it was attached to <strong>the</strong> body <strong>of</strong><br />
<strong>the</strong> crane.<br />
Extreme care must be taken to avoid excessive<br />
side loads on cranes not designed for marine use.<br />
Detailed guidance from <strong>the</strong> crane’s manufacturers<br />
and national authorities should be sought. As a<br />
general rule however <strong>the</strong> vessel should not be<br />
allowed to list more than 5° during <strong>the</strong> discharge<br />
operation and <strong>the</strong> load should never exceed 50% <strong>of</strong><br />
<strong>the</strong> crane’s safe working load for operation on land.<br />
The vessel’s stability was adequate but in order<br />
to counteract <strong>the</strong> anticipated list as <strong>the</strong> load was<br />
swung towards <strong>the</strong> wharf, orders were given to<br />
deballast <strong>the</strong> double bottom tanks on that side.<br />
The deballasting had not been completed at <strong>the</strong><br />
time <strong>the</strong> load was moved horizontally and <strong>the</strong><br />
free surface effect <strong>of</strong> <strong>the</strong> liquid in <strong>the</strong> partially<br />
filled tanks served to increase <strong>the</strong> vessel’s list. The<br />
number <strong>of</strong> slack tanks must be kept to a minimum<br />
when heavy loads are handled.<br />
Financial Cost:<br />
The cargo claim was settled for US$500 in line with<br />
<strong>the</strong> package limitation contained in <strong>the</strong> bill <strong>of</strong> lading.<br />
The claim <strong>of</strong> <strong>the</strong> vehicle driver was covered by his<br />
motor insurers who ra<strong>the</strong>r surprisingly failed to<br />
subrogate <strong>the</strong>ir claim against our Member before it<br />
became time-barred. The owners faced a number<br />
<strong>of</strong> prosecutions brought for alleged breaches <strong>of</strong> <strong>the</strong><br />
Canada Shipping Act and <strong>the</strong> Tackle Regulation,<br />
most <strong>of</strong> which were quashed at trial. Despite a<br />
very favourable resolution <strong>of</strong> <strong>the</strong> claims, <strong>the</strong> costs<br />
incurred in investigating and defending <strong>the</strong> Member<br />
reached US$33,000.<br />
Root Cause:<br />
Incorrect operation <strong>of</strong> equipment.<br />
Issue Date: 01/02/02 Case No. 16415<br />
16 17
Cargo<br />
Flammable Gases Cause Explosion<br />
The Incident:<br />
This incident involved a large explosion on board a<br />
general cargo vessel when flammable gases given<br />
<strong>of</strong>f by <strong>the</strong> cargo were ignited by an electrical spark.<br />
The explosion killed two crew members, injured<br />
several more and caused severe damage to <strong>the</strong> ship.<br />
The vessel’s forward hatch covers were blown <strong>of</strong>f,<br />
landing on and severely damaging two tugs moored<br />
nearby. Extensive damage was caused to surrounding<br />
buildings and a nearby papermill was shut down for a<br />
week following <strong>the</strong> explosion.<br />
Observations:<br />
The vessel was loading a cargo <strong>of</strong> spent pot liner, <strong>the</strong><br />
carbon-based lining <strong>of</strong> an aluminium smelter which<br />
absorbs impurities from <strong>the</strong> metal. It eventually<br />
becomes saturated and has to be replaced. The<br />
impurities in <strong>the</strong> spent pot liner react slowly with<br />
water producing inflammable gases.<br />
Our investigations revealed that <strong>the</strong> cargo loaded<br />
into number 1 hatch had come from two different<br />
storage areas. Wet reacted cargo from an open<br />
stockpile had been mixed with dry unreacted<br />
cargo which had been stored in a closed shed.<br />
Moisture from <strong>the</strong> wea<strong>the</strong>red cargo migrated to<br />
<strong>the</strong> dry, causing it to react with <strong>the</strong> result that an<br />
accumulation <strong>of</strong> inflammable gases built up in <strong>the</strong><br />
hold and fan rooms overnight. These gases were<br />
ignited by an electrical contactor operating <strong>the</strong><br />
hydraulic system for <strong>the</strong> hatch covers.<br />
The shippers, although aware <strong>of</strong> <strong>the</strong> problem<br />
<strong>of</strong> inflammable gases, did not advise owners or<br />
charterers <strong>of</strong> <strong>the</strong> danger, nor did <strong>the</strong>y provide<br />
<strong>the</strong> vessel with a <strong>copy</strong> <strong>of</strong> <strong>the</strong>ir material safety<br />
data sheet. Information on spent pot lining was<br />
not available from <strong>the</strong> IMDG Code, <strong>the</strong> IMO<br />
Code <strong>of</strong> Safe Practice for Solid Bulk Cargoes, <strong>the</strong><br />
Dangerous Bulk Materials Regulations or any o<strong>the</strong>r<br />
<strong>of</strong>ficial publication.<br />
The explosion could have been avoided if all <strong>the</strong> pot lining had been wea<strong>the</strong>red prior to<br />
shipment or proper steps had been taken by <strong>the</strong> shipper to ensure that wet cargo was<br />
kept separate from dry unreacted cargo. The shippers should have provided <strong>the</strong> vessel<br />
with safety data sheets. Appropriate measures could <strong>the</strong>n have been taken to ensure<br />
that <strong>the</strong> cargo was kept adequately ventilated and <strong>the</strong> accumulation <strong>of</strong> explosive gas<br />
could have been avoided.<br />
Root Cause:<br />
Unsafe loading practice.<br />
Financial Cost:<br />
The claims arising out <strong>of</strong> <strong>the</strong> explosion totalled<br />
over US$30 million. In <strong>the</strong> end <strong>the</strong>y were settled<br />
for just under US$11 million with <strong>the</strong> shippers <strong>of</strong><br />
<strong>the</strong> cargo bearing by far <strong>the</strong> greatest proportion.<br />
Never<strong>the</strong>less <strong>the</strong> costs <strong>of</strong> investigation, defending<br />
<strong>the</strong> various legal actions and with a very modest<br />
contribution towards <strong>the</strong> settlements brought<br />
<strong>the</strong> cost to our Members <strong>the</strong> charterers to<br />
US$1.3 million.<br />
Issue Date: 01/01/02<br />
Case No. 15646<br />
18 19
Miscellaneous<br />
Corrosion – The Hidden Enemy<br />
The Incident:<br />
Please note that this case study has been provided<br />
by <strong>the</strong> MAIB Safety Digest 2/2007, Case 6.<br />
After completing <strong>the</strong> weekly planned maintenance<br />
routine on a rescue boat and its crane, it was usual<br />
for <strong>the</strong> crew to lower <strong>the</strong> boat to <strong>the</strong> water for<br />
training purposes while alongside. The boat was<br />
lowered and manoeuvred in <strong>the</strong> water for a short<br />
time and <strong>the</strong>n brought back to be hoisted on board.<br />
As <strong>the</strong> boat was being hoisted, <strong>the</strong> wire rope parted<br />
and <strong>the</strong> boat fell into <strong>the</strong> sea.<br />
Fortunately, <strong>the</strong> company had al<strong>read</strong>y identified this<br />
as a high risk operation and had stopped <strong>the</strong> practice<br />
<strong>of</strong> having <strong>the</strong> crew in <strong>the</strong> boat while hoisting or<br />
lowering during training exercises. There were no<br />
injuries, and <strong>the</strong> boat was not damaged.<br />
On investigation, it was found that a new wire rope<br />
had been fitted 14 months previously, and it had<br />
passed a thorough examination about five months<br />
before <strong>the</strong> incident. It was also inspected/greased<br />
on a weekly basis as part <strong>of</strong> <strong>the</strong> ship’s planned<br />
maintenance programme. Despite <strong>the</strong> checks, <strong>the</strong><br />
incipient corrosion had not been discovered and<br />
<strong>the</strong> wire eventually failed at <strong>the</strong> top <strong>of</strong> <strong>the</strong> steel ball<br />
counter weight.<br />
The accelerated corrosion was partly due to <strong>the</strong><br />
harsh environment in which <strong>the</strong> rescue boat and<br />
its crane were located, at <strong>the</strong> aft end <strong>of</strong> <strong>the</strong> vessel.<br />
The ball weight had a crevice at <strong>the</strong> top where <strong>the</strong><br />
wire passed through, and this formed an ideal trap<br />
for sea water, salt and sulphur deposits from nearby<br />
exhaust outlets to accumulate and obstruct regular<br />
inspection.<br />
The investigation discovered that unsuitable grease<br />
had been applied, and this had not been effective in<br />
lubricating <strong>the</strong> wire core and served to obscure <strong>the</strong><br />
underlying corrosion (see photograph <strong>of</strong> wire and<br />
crane ball indicating <strong>the</strong> point <strong>of</strong> failure).<br />
The failed segments <strong>of</strong> <strong>the</strong> wire rope were sent<br />
to a laboratory for testing, and <strong>the</strong> subsequent<br />
report confirmed that <strong>the</strong> wire rope had failed<br />
through ductile tensile fractures <strong>of</strong> wires wasted<br />
by corrosion. The laboratory was also able to<br />
confirm that a contributory cause <strong>of</strong> <strong>the</strong> failure was<br />
inadequate maintenance greasing over a significant<br />
period <strong>of</strong> time.<br />
The body was recovered two months later and<br />
despite <strong>the</strong> fact his left ankle was tightly bound<br />
with rope <strong>the</strong> inquest concluded death by<br />
drowning with no obvious signs <strong>of</strong> violence.<br />
Conclusion:<br />
1. The inspection <strong>of</strong> all wire ropes should be<br />
thorough, and should include <strong>the</strong> removal <strong>of</strong> old<br />
grease to assess <strong>the</strong> condition <strong>of</strong> <strong>the</strong> wire rope<br />
before re-coating with fresh wire lubricant.<br />
2. Senior staff should regularly monitor planned<br />
maintenance procedures which are carried out<br />
by crew.<br />
3. Consideration should be given to <strong>the</strong> use <strong>of</strong> a<br />
thinner self penetrating lubricant on seldom used<br />
wire ropes, especially where <strong>the</strong>y are used or<br />
stored in a harsh corrosive environment.<br />
Issue Date: 09/12/07<br />
Case No: 12377<br />
20 21
Dry Cargo:<br />
Containers<br />
Cargo<br />
Capsize During Loading<br />
The Incident:<br />
As <strong>the</strong> last few containers were being loaded on <strong>the</strong><br />
deck <strong>of</strong> a 3,000 gross ton inter-island cargo vessel<br />
she capsized and sank alongside <strong>the</strong> dock, damaging<br />
<strong>the</strong> dock as she went down. The Port Authority<br />
issued a wreck removal order. The Club invited<br />
tenders for <strong>the</strong> removal operation and a contract<br />
was finally agreed with a Singapore-based salvage<br />
company. The wreck removal was effected using a<br />
large sheerlegs which had to be towed over 2,000<br />
miles to <strong>the</strong> site <strong>of</strong> <strong>the</strong> accident. The wreck was cut<br />
up into manageable sections and dumped at sea.<br />
The berth was finally cleared some five months<br />
after <strong>the</strong> ship went down. The majority <strong>of</strong> <strong>the</strong> cargo<br />
was a total loss.<br />
Observations:<br />
Our investigations revealed that <strong>the</strong> cause <strong>of</strong> <strong>the</strong> loss was an error in<br />
calculating <strong>the</strong> vessel’s stability. The Chief Officer had failed to make<br />
proper allowance for <strong>the</strong> height <strong>of</strong> a stow <strong>of</strong> bagged cement in <strong>the</strong><br />
lower hold when calculating <strong>the</strong> vessel’s vertical centre <strong>of</strong> gravity. As<br />
a result his calculations produced an over-optimistic prediction <strong>of</strong> <strong>the</strong><br />
vessel’s stability on completion <strong>of</strong> loading. There was no established<br />
procedure on this ship for an independent check <strong>of</strong> <strong>the</strong> Chief Officer’s<br />
calculation. Had <strong>the</strong>re been one it is highly likely that <strong>the</strong> mistake<br />
would have been noticed and <strong>the</strong> loss <strong>of</strong> <strong>the</strong> vessel avoided.<br />
Root Cause:<br />
Error in stability calculation.<br />
Financial Cost:<br />
Cargo claims totalling over US$3 million were submitted to <strong>the</strong><br />
owners. By using package limitation and defences available to <strong>the</strong><br />
owners under <strong>the</strong> Hague Rules, those claims were finally settled for<br />
less than US$500,000.<br />
The costs <strong>of</strong> removing <strong>the</strong> wreck <strong>of</strong> <strong>the</strong> vessel approached<br />
US$1.5 million.<br />
Claims by <strong>the</strong> Port Authority and individual crew members brought<br />
<strong>the</strong> total cost <strong>of</strong> <strong>the</strong> claim to almost US$2.2 million.<br />
Issue Date: 01/01/02 Case No. 18006<br />
22 23
Cargo<br />
Stability Needs Careful Attention<br />
The Incident:<br />
A Feeder Container vessel had completed cargo<br />
operations at one berth and was in <strong>the</strong> process<br />
<strong>of</strong> shifting to a second berth. A harbour tug<br />
commenced pushing <strong>the</strong> vessel towards <strong>the</strong> berth<br />
when <strong>the</strong> Member’s vessel began to heel over.<br />
When heeled over to approximately 10 to 15<br />
degrees, containers began to fall <strong>of</strong>f <strong>the</strong> vessel; <strong>the</strong><br />
tug stopped pushing, and this action in conjunction<br />
with <strong>the</strong> loss <strong>of</strong> containers enabled <strong>the</strong> vessel to<br />
return to near upright.<br />
Observations:<br />
The subsequent investigations showed that poor<br />
operational practices were allowed on board,<br />
with very little regard given to <strong>the</strong> safety <strong>of</strong> <strong>the</strong><br />
vessel. The centre <strong>of</strong> gravity (KG) <strong>of</strong> <strong>the</strong> vessel<br />
was determined to be well above <strong>the</strong> maximum<br />
permitted and no account had been taken <strong>of</strong> <strong>the</strong><br />
numerous free surfaces in <strong>the</strong> ballast tanks. To<br />
make matters worse, it was calculated that <strong>the</strong><br />
vessel was in fact 400t overloaded, resulting in a<br />
reduction in <strong>the</strong> freeboard <strong>of</strong> 30cms less than <strong>the</strong><br />
minimum permitted.<br />
These factors combined to result in a drastic<br />
reduction <strong>of</strong> transverse stability which was<br />
insufficient to withstand <strong>the</strong> forces created by <strong>the</strong><br />
pushing tug.<br />
Ironically, <strong>the</strong> top tiers <strong>of</strong> containers had not been<br />
secured but this allowed <strong>the</strong> containers to fall <strong>of</strong>f<br />
and <strong>the</strong> vessel returned to <strong>the</strong> upright.<br />
One <strong>of</strong> <strong>the</strong> contributing factors to <strong>the</strong> overloading<br />
was <strong>the</strong> under declaration <strong>of</strong> <strong>the</strong> containers<br />
weights by <strong>the</strong> shipper. This case highlights <strong>the</strong><br />
need to monitor <strong>the</strong> vessel’s condition at all times.<br />
By observing <strong>the</strong> drafts, <strong>the</strong> overloading would<br />
have been noted at an early stage and <strong>the</strong> vessel’s<br />
lack <strong>of</strong> adequate stability detected.<br />
Root Cause:<br />
Failure to observe stability requirements.<br />
Financial Cost:<br />
The total cost <strong>of</strong> this claim was in excess <strong>of</strong><br />
US$660,000; a great deal <strong>of</strong> this was accounted for<br />
in recovering containers that sank in <strong>the</strong> approach<br />
channel to <strong>the</strong> berth.<br />
Issue Date: 01/08/07<br />
Case No. 42200<br />
24 25
Cargo<br />
Be Prepared<br />
The Incident:<br />
This incident occurred on a 316 TEU feeder container vessel/bulk carrier immediately<br />
after loading had been completed.<br />
On completion <strong>of</strong> loading <strong>the</strong> vessel had a 1° list to starboard. This slowly increased.<br />
Corrective action was taken, but despite this <strong>the</strong> list continued to increase. By <strong>the</strong> time<br />
it had reached approximately 15°, a number <strong>of</strong> containers fell <strong>of</strong>f <strong>the</strong> top tier into <strong>the</strong><br />
harbour waters. The vessel <strong>the</strong>n violently rolled to port. The list increased until <strong>the</strong><br />
water line had reached <strong>the</strong> hatch coamings and progressive flooding started to take<br />
place. Fortunately more containers fell <strong>of</strong>f <strong>the</strong> top tier, reducing <strong>the</strong> list. The situation<br />
was eventually brought under control by discharging cargo and <strong>the</strong> vessel returned to<br />
an even keel.<br />
Observations:<br />
This incident was caused by a poorly prepared<br />
stow plan resulting in <strong>the</strong> vessel having negative<br />
stability upon completion <strong>of</strong> loading. The onboard<br />
calculations were incorrectly executed, as <strong>the</strong>y<br />
appear not to have taken <strong>the</strong> effects <strong>of</strong> free surface<br />
into account, so masking <strong>the</strong> true stability condition<br />
<strong>of</strong> <strong>the</strong> vessel.<br />
Feeder container vessels are renowned for<br />
<strong>the</strong>ir short turn round times and frequent cargo<br />
changes. Operators <strong>of</strong> <strong>the</strong>se vessels should ensure<br />
procedures are in place to minimise <strong>the</strong> potential<br />
for errors. Shore prepared stow plans must be<br />
checked for accuracy, preferably by a second<br />
person before <strong>the</strong>y are issued. Means should<br />
be provided to assist ship’s staff in assessing <strong>the</strong><br />
stability condition <strong>of</strong> <strong>the</strong> vessel so as to reduce<br />
<strong>the</strong> possibilities <strong>of</strong> errors being made in hastily<br />
completed calculations. This could take <strong>the</strong> form <strong>of</strong><br />
computers or encouragement to use prepared pro<br />
forma. Owners should satisfy <strong>the</strong>mselves that <strong>the</strong><br />
senior <strong>of</strong>ficers on board are fully familiar with <strong>the</strong><br />
stability requirements <strong>of</strong> <strong>the</strong>ir vessel.<br />
Root Cause:<br />
Inadequate lashing.<br />
Financial Cost:<br />
This turned out to be a very expensive claim as<br />
enormous efforts had to be made to locate <strong>the</strong><br />
sunken containers that fell overboard. The final<br />
cost was in <strong>the</strong> region <strong>of</strong> US$580,000.<br />
Issue Date: 01/01/02<br />
Case No. 34857<br />
26 27
Cargo<br />
Complacency Rules<br />
The Incident:<br />
This claim arose on a river craft specifically designed<br />
for a container feeder service between two<br />
terminals.<br />
Whilst manoeuvring <strong>of</strong>f one <strong>of</strong> <strong>the</strong> terminals with<br />
a cargo <strong>of</strong> 92 twenty and forty foot containers, <strong>the</strong><br />
vessel experienced a squall and started rolling as she<br />
turned beam on to <strong>the</strong> wind.<br />
A number <strong>of</strong> containers moved as <strong>the</strong> vessel rolled,<br />
striking adjacent containers. The lashings on two <strong>of</strong><br />
<strong>the</strong> containers struck consequently failed and two<br />
forty foot units were lost overboard.<br />
Observations:<br />
This claim arose because <strong>of</strong> poor operational<br />
practices on board. Investigations showed that <strong>the</strong><br />
lashing system employed was far from satisfactory.<br />
Local regulations did not require operators to have<br />
approved securing manuals and <strong>the</strong> operators did<br />
not have any requirements or guidelines <strong>of</strong> <strong>the</strong>ir<br />
own. Consequently <strong>the</strong> securing <strong>of</strong> <strong>the</strong> containers<br />
was left to <strong>the</strong> crew who relied on <strong>the</strong>ir experience.<br />
No procedures had been established requiring<br />
calculation <strong>of</strong> <strong>the</strong> vessel’s stability and <strong>the</strong>refore <strong>the</strong><br />
Master had no indication <strong>of</strong> <strong>the</strong> stability condition <strong>of</strong><br />
<strong>the</strong> vessel (e.g. too large or too small a GM) when<br />
she sailed.<br />
The lashing system did not follow normal acceptable<br />
practices and a number <strong>of</strong> deficiencies came to light<br />
during <strong>the</strong> Club’s investigations:<br />
• <strong>the</strong> lashing gear was not certified or provided<br />
with identification marks;<br />
• <strong>the</strong> amount <strong>of</strong> lashing gear used was insufficient.<br />
Where used, twist locks were only applied to<br />
two corners <strong>of</strong> each container and not all four<br />
and only minimal wire lashings were used<br />
(see pictures)<br />
• in-board containers were not secured at all;<br />
• <strong>the</strong> leads for <strong>the</strong> lashing wires were totally<br />
inappropriate and bulldog wire rope grips were<br />
insufficient in number, positioning and size;<br />
• it is doubtful whe<strong>the</strong>r <strong>the</strong> lashing gear utilised was<br />
in fact <strong>of</strong> sufficient strength for <strong>the</strong> task required<br />
<strong>of</strong> it;<br />
• no account appeared to have been taken <strong>of</strong> <strong>the</strong><br />
differences in height between standard and high<br />
cube units, which prevented <strong>the</strong> satisfactory use<br />
<strong>of</strong> bridge fittings;<br />
• no maintenance programme was in place for <strong>the</strong><br />
upkeep <strong>of</strong> <strong>the</strong> lashing gear.<br />
Root Cause:<br />
Inadequate lashing.<br />
Financial Cost:<br />
Salvage teams fortunately were able to recover<br />
<strong>the</strong>se containers <strong>the</strong>refore <strong>the</strong> Members have only<br />
been liable for <strong>the</strong>ir salvage and loss <strong>of</strong> contents.<br />
This is estimated to cost US$7,000.<br />
Issue Date: 18/06/03<br />
Case No. 37556<br />
28 29
Operations<br />
It will be Alright – But it Wasn’t<br />
The Incident:<br />
This incident involved loading containers into a hold<br />
that contained water and was compounded by <strong>the</strong> fact<br />
that <strong>the</strong> bilge pumping system was not operational.<br />
On completion <strong>of</strong> discharging, water was noted<br />
lying on <strong>the</strong> tank top and efforts to remove it failed<br />
because <strong>the</strong> bilge pumping system was found to be<br />
inoperative. Time constraints apparently prevented<br />
any o<strong>the</strong>r means to remove <strong>the</strong> water to be utilised.<br />
Loading was <strong>the</strong>n commenced and <strong>the</strong> vessel<br />
subsequently sailed.<br />
During <strong>the</strong> course <strong>of</strong> <strong>the</strong> voyage <strong>the</strong> hold bilge levels<br />
were reportedly monitored although some doubt<br />
exists as to whe<strong>the</strong>r or not <strong>the</strong> bilge sounding pipes<br />
were clear enabling soundings to be taken. It would<br />
appear that during <strong>the</strong> voyage, <strong>the</strong> bilge levels did in<br />
fact rise.<br />
Once <strong>the</strong> hold in question was discharged, <strong>the</strong><br />
majority <strong>of</strong> <strong>the</strong> lower tier <strong>of</strong> containers were found<br />
to have had <strong>the</strong>ir bases immersed in water.<br />
Observations:<br />
Notwithstanding <strong>the</strong> source <strong>of</strong> <strong>the</strong> water leak into<br />
<strong>the</strong> hold, <strong>the</strong> prime cause <strong>of</strong> this claim was <strong>the</strong> poor<br />
condition <strong>of</strong> <strong>the</strong> hold bilge pumping system. Access<br />
to bilge wells can be restricted due to <strong>the</strong> compact<br />
nature <strong>of</strong> container stowage and it is not always<br />
possible to use portable pumps to remove cargo<br />
hold bilge water if <strong>the</strong> main system fails. Therefore<br />
it is <strong>of</strong> <strong>the</strong> utmost importance to ensure that <strong>the</strong><br />
bilge pumping arrangement is regularly tested<br />
and maintained in full working order. Similarly <strong>the</strong><br />
sounding pipes must be kept clear at all times.<br />
The water entered <strong>the</strong> hold through cracks which<br />
had developed at <strong>the</strong> base <strong>of</strong> <strong>the</strong> cell guides where<br />
<strong>the</strong>y connect with <strong>the</strong> tank top. During <strong>the</strong> course<br />
<strong>of</strong> loading and discharging, <strong>the</strong>se guides suffer<br />
considerable physical stress and if <strong>the</strong> bases are<br />
weakened through corrosion at all, cracks will<br />
eventually occur. It is important <strong>the</strong>refore that <strong>the</strong>se<br />
areas are inspected regularly and repairs carried out<br />
promptly.<br />
It is apparent that <strong>the</strong> amount <strong>of</strong> water noted in <strong>the</strong><br />
hold on completion <strong>of</strong> discharging and during <strong>the</strong><br />
voyage was not considered significant, but obviously<br />
no allowance was made for <strong>the</strong> fact that <strong>the</strong> level<br />
will rise and fall when <strong>the</strong> vessel rolls and pitches in<br />
a seaway. Any water in a cargo hold is unacceptable<br />
and should be removed as soon as it is detected.<br />
Root Cause:<br />
Insufficient maintenance.<br />
Financial Cost:<br />
This claim was settled for US$60,000.<br />
Issue Date: 17/06/03<br />
Case No. 38930<br />
30 31
Operations<br />
Free Water and Poor Maths Result in Delays<br />
The Incident:<br />
This incident took place on a 25 year old 370 TEU<br />
feeder container ship. Shortly before arriving at<br />
<strong>the</strong> pilot station, an unexplained port list suddenly<br />
developed. The list was corrected and “sounding<br />
round” showed <strong>the</strong>re to be about 100 cm <strong>of</strong> water in<br />
her hold.<br />
Until ber<strong>the</strong>d, <strong>the</strong> vessel had flopped one way<br />
or ano<strong>the</strong>r on a number <strong>of</strong> occasions, each time<br />
corrected by moving ballast. Alongside she lay with<br />
a 15° list against <strong>the</strong> quay.<br />
The Chief Officer carried out an assessment <strong>of</strong> <strong>the</strong> stability and deemed<br />
<strong>the</strong> vessel to be unstable. The port authority subsequently refused to give<br />
permission for cargo operations to commence until <strong>the</strong> vessel was upright,<br />
<strong>the</strong> cause <strong>of</strong> <strong>the</strong> listing was determined and stability was confirmed by <strong>the</strong><br />
Classification Society.<br />
Efforts to pump out <strong>the</strong> hold bilge were thwarted by choked suctions.<br />
The services <strong>of</strong> a local salvage company were engaged to pump out <strong>the</strong><br />
hold and remove <strong>the</strong> top tier <strong>of</strong> containers in order to regain positive<br />
stability. The ballast tanks were closely monitored during this operation<br />
and it became apparent that water from two ballast tanks was entering<br />
<strong>the</strong> hold. The stability calculations were reworked and showed <strong>the</strong> vessel<br />
to have positive stability. This was later confirmed by <strong>the</strong> Classification<br />
Society.<br />
Permission for cargo operations to commence was given nearly three days<br />
after <strong>the</strong> vessel’s arrival at <strong>the</strong> port.<br />
Observations:<br />
The incident was caused by free water in <strong>the</strong> cargo<br />
hold.<br />
Choked hold bilge suctions prevented <strong>the</strong> water<br />
being pumped out by <strong>the</strong> ship’s staff.<br />
Investigations showed that <strong>the</strong> vessel had sustained<br />
two fractures in <strong>the</strong> tank top. These were believed<br />
to have been caused by <strong>the</strong> heavy landing <strong>of</strong><br />
containers during loading. The problem was fur<strong>the</strong>r<br />
exacerbated by <strong>the</strong> fact that <strong>the</strong> heeling tank filling<br />
pipe had corroded through. Ironically <strong>the</strong>refore,<br />
ballast water used to correct <strong>the</strong> list increased <strong>the</strong><br />
leakage into <strong>the</strong> hold, aggravating <strong>the</strong> problem.<br />
The Master was criticised for not conducting a<br />
more thorough investigation at <strong>the</strong> time <strong>of</strong> <strong>the</strong> initial<br />
listing.<br />
A regular systematic daily sounding programme is<br />
a well established procedure <strong>of</strong> good seamanship<br />
and would give an early indication <strong>of</strong> any problem.<br />
It would do away with <strong>the</strong> need to engage in <strong>the</strong><br />
dangerous practice <strong>of</strong> entering enclosed spaces to<br />
visually check <strong>the</strong> hold.<br />
The difficulties in pumping out <strong>the</strong> hold once <strong>the</strong><br />
water had entered were reportedly due to <strong>the</strong><br />
suctions being choked with debris. This highlights <strong>the</strong><br />
need for <strong>the</strong> holds to be kept free <strong>of</strong> rubbish and <strong>the</strong><br />
regular proving <strong>of</strong> <strong>the</strong> pumping arrangements. The<br />
provision <strong>of</strong> a hold bilge alarm would have given a<br />
very early indication <strong>of</strong> <strong>the</strong> water entering <strong>the</strong> hold.<br />
The original erroneous stability calculation was a<br />
major contributing factor to <strong>the</strong> delay suffered by<br />
<strong>the</strong> vessel. This should have been carried out prior<br />
to leaving <strong>the</strong> load port. Third party calculations can<br />
not be relied upon.<br />
The base <strong>of</strong> cell guides which carry <strong>the</strong> brunt <strong>of</strong><br />
heavy container movements, should be inspected<br />
on a regular basis so that corrosion and weakness<br />
can be detected at an early stage.<br />
Root Cause:<br />
Inadequate maintenance procedures.<br />
Financial Cost:<br />
The total claim is expected to be in <strong>the</strong> region <strong>of</strong><br />
US$75,000 to US$100,000.<br />
Issue Date: 01/01/02<br />
Case No. 32771<br />
32 33
Dry Cargo:<br />
Ro-Ro<br />
Cargo<br />
Premature Signing for Cargo Consignment Causes Hangover<br />
The Incident:<br />
This case involves cargo <strong>the</strong>ft within <strong>the</strong> port area. A brewery shipped<br />
a consignment <strong>of</strong> 282 cartons <strong>of</strong> beer on three shrink wrapped pallets<br />
between two depots in south east Asia. There was no direct shipping<br />
service between <strong>the</strong> depots. The beer was <strong>the</strong>refore shipped to an<br />
intermediate port where it was discharged for trans-shipment. The<br />
beer was loaded onto trucks for delivery to our Member’s vessel. As<br />
was <strong>the</strong>ir custom, our Member signed for receipt <strong>of</strong> <strong>the</strong> beer at <strong>the</strong>ir<br />
dock gate <strong>of</strong>fice. The truck and its consignment <strong>of</strong> beer disappeared<br />
somewhere between <strong>the</strong> dock gate <strong>of</strong>fice and <strong>the</strong> ship’s side. As a<br />
result <strong>of</strong> poor communications between <strong>the</strong> ship and <strong>the</strong> dock <strong>of</strong>fice,<br />
<strong>the</strong> disappearance <strong>of</strong> <strong>the</strong> beer was not noticed and it was only after<br />
<strong>the</strong> voyage was completed and a claim for non-delivery was received<br />
from <strong>the</strong> brewery that <strong>the</strong> circumstances came to light. The brewery<br />
was able to produce <strong>the</strong> road hauliers documents signed by <strong>the</strong><br />
shipowner showing that <strong>the</strong> beer had been delivered and had been<br />
accepted into <strong>the</strong> care <strong>of</strong> <strong>the</strong> shipowner. As a result <strong>the</strong> owners had to<br />
pay for <strong>the</strong> loss.<br />
Observations:<br />
<strong>Shipowners</strong> accepting cargo into <strong>the</strong>ir custody<br />
must take reasonable precautions to prevent loss<br />
or damage <strong>of</strong> <strong>the</strong> cargo. The custom and practice<br />
at <strong>the</strong> load port was for shipowners to accept<br />
consignments at <strong>the</strong> dock gate ra<strong>the</strong>r than at <strong>the</strong><br />
ship’s side. There was however no system for<br />
controlling or monitoring <strong>the</strong> progress <strong>of</strong> <strong>the</strong> cargo<br />
from <strong>the</strong>re to <strong>the</strong> ship. In this case <strong>the</strong> loss could<br />
have been avoided ei<strong>the</strong>r by only signing for <strong>the</strong><br />
cargo when it had been actually delivered to <strong>the</strong><br />
vessel itself or ensuring that proper procedures<br />
were in place for monitoring <strong>the</strong> progress <strong>of</strong> <strong>the</strong><br />
cargo after acceptance at <strong>the</strong> dock gate.<br />
Root Cause:<br />
Lack <strong>of</strong> shore procedures.<br />
Financial Cost:<br />
The cost to <strong>the</strong> shipowner exceeded US$5,000.<br />
Issue Date: 01/01/02<br />
Case No. 17180<br />
34 35
Cargo<br />
Poor Lashing Procedures Cause Destruction<br />
The Incident:<br />
During a voyage across <strong>the</strong> English Channel in<br />
heavy wea<strong>the</strong>r some vehicles on <strong>the</strong> car decks<br />
broke <strong>the</strong>ir lashings with <strong>the</strong> result that 18 lorries,<br />
<strong>the</strong>ir cargoes and three cars were damaged,<br />
resulting in many claims.<br />
Observations:<br />
Surveyors appointed by <strong>the</strong> Club reported that <strong>the</strong><br />
principal cause <strong>of</strong> <strong>the</strong> damage was <strong>the</strong> ship’s crew’s<br />
failure to properly lash <strong>the</strong> articulated vehicles. Our<br />
surveyors reported that <strong>the</strong>re was no company<br />
operating manual on board giving <strong>the</strong> crew guidance<br />
on car deck operations and safety. M-Notices and<br />
IMO publications were also unavailable. The Master<br />
had given no standing orders relating to car deck<br />
safety, nor had he set wea<strong>the</strong>r criteria above which<br />
cargo should be lashed.<br />
Root Cause:<br />
Inadequate lashing.<br />
Financial Cost:<br />
The damage to <strong>the</strong> vehicles amounted<br />
to US$128,150.<br />
Issue Date: 01/01/02<br />
Case No. 21978<br />
The majority <strong>of</strong> <strong>the</strong> damage was caused by a<br />
number <strong>of</strong> articulated vehicles which were only<br />
secured by four lashings, one at each corner <strong>of</strong> <strong>the</strong><br />
combined vehicles. This lashing system was totally<br />
inadequate for vehicles that did not form a rigid<br />
unit. In each case <strong>the</strong> damage was caused by <strong>the</strong><br />
vehicles jack-knifing, i.e. hinging at <strong>the</strong> joint between<br />
<strong>the</strong> tractor and trailer units. The jack-knifing<br />
resulted in <strong>the</strong> general slackening <strong>of</strong> <strong>the</strong> lashings<br />
which were <strong>the</strong>n subjected to shock loadings<br />
from <strong>the</strong> movement <strong>of</strong> ship and vehicles, with <strong>the</strong><br />
consequence that <strong>the</strong>y eventually parted.<br />
The claims that resulted from this incident were<br />
completely avoidable. Lashing <strong>the</strong> vehicles in<br />
accordance with IMO guidelines would have<br />
prevented <strong>the</strong> jack-knifing and consequent damage.<br />
Companies operating ro-ro ferries are now required<br />
to provide <strong>the</strong>ir vessels with a comprehensive cargo<br />
securing manual and Masters should issue standing<br />
instructions on when lashing is required and who<br />
has responsibility for ensuring that it is done.<br />
36 37
Section 2<br />
Tankers<br />
39
Tankers:<br />
Petroleum<br />
Personal Injury/Illness<br />
Explosion in Dockyard<br />
The Incident:<br />
A small tanker went into a repair yard to have damage to her<br />
starboard bow repaired. The vessel habitually carried premium<br />
motor spirit in all her cargo tanks and prior to arriving at <strong>the</strong> yard<br />
had cleaned and gas freed <strong>the</strong> tanks by filling <strong>the</strong>m to overflowing<br />
with seawater. Before hot work commenced <strong>the</strong> owners brought<br />
in a surveyor to test for explosive atmosphere and issue a gas free<br />
certificate. The certificate declared <strong>the</strong> vessel fit for hot work and<br />
indicated that all cargo tanks had been tested and found gas free.<br />
As shipyard workers started to cut away <strong>the</strong> damaged section an<br />
explosion occurred in <strong>the</strong> fore peak tank, severely damaging <strong>the</strong><br />
vessel and badly injuring two workers.<br />
Observations:<br />
The explosion almost certainly occurred as a result<br />
<strong>of</strong> an accumulation <strong>of</strong> explosive vapours in <strong>the</strong> fore<br />
peak tank. The reason for <strong>the</strong> accumulation was<br />
never discovered. The c<strong>of</strong>fer dam separating <strong>the</strong><br />
fore peak tank from <strong>the</strong> cargo tanks was found<br />
to be clean, dry and free <strong>of</strong> cargo vapours. The<br />
incident highlights <strong>the</strong> desirability <strong>of</strong> testing <strong>the</strong><br />
atmosphere in all enclosed spaces on tankers prior<br />
to commencing hot work.<br />
In this case <strong>the</strong>re was no formal contract between<br />
<strong>the</strong> vessel’s owners and <strong>the</strong> repair yard. The<br />
question <strong>of</strong> responsibility for ensuring that <strong>the</strong><br />
vessel was fit for hot work to be carried out was<br />
not clear. We would recommend that owners<br />
ensure this subject is addressed in every repair<br />
contract and that where possible <strong>the</strong> shipyard be<br />
given this responsibility.<br />
Root Cause:<br />
Insufficient safety procedures.<br />
Financial Cost:<br />
The entire fore part <strong>of</strong> <strong>the</strong> vessel had to be replaced<br />
at a cost <strong>of</strong> US$200,000. Claims by <strong>the</strong> injured<br />
workers were met by <strong>the</strong> shipyard’s insurers. In<br />
addition to this surveyor’s fees exceeding US$4,000<br />
were incurred.<br />
Issue Date: 01/01/02<br />
Case No. 20590<br />
40 41
Personal Injury/Illness<br />
Injury During Unmooring Operation<br />
The Incident:<br />
This accident involves a serious injury during<br />
unmooring operations as <strong>the</strong> vessel prepared to<br />
sail. The crew had been sent to stations and <strong>the</strong><br />
vessel had been singled up while awaiting customs<br />
clearance. The last two lines on <strong>the</strong> foredeck were<br />
those permanently stored on <strong>the</strong> windlass drums.<br />
At 08.30 customs clearance was obtained and<br />
<strong>the</strong> order was given to let go forward. When <strong>the</strong><br />
foredeck crew tried to slack down <strong>the</strong> line on <strong>the</strong><br />
starboard drum for letting go it would not do so.<br />
During efforts to free <strong>the</strong> rope <strong>the</strong> chief <strong>of</strong>ficer’s<br />
foot was caught in <strong>the</strong> machinery, resulting in very<br />
serious injuries to his toes.<br />
Observations:<br />
The berth had been exposed to a heavy swell<br />
which had caused <strong>the</strong> vessel to surge continually<br />
whilst alongside. The surging action had resulted<br />
in <strong>the</strong> mooring rope on <strong>the</strong> starboard windlass<br />
drum becoming buried in itself. When it became<br />
necessary to slacken down <strong>the</strong> line it jammed. The<br />
chief <strong>of</strong>ficer attempted to pull <strong>the</strong> line clear and<br />
in <strong>the</strong> process put his foot on <strong>the</strong> winch-bearing<br />
A-frame support forward <strong>of</strong> <strong>the</strong> starboard drum.<br />
The A-frame support is close to <strong>the</strong> drum face<br />
which had four flat bar stiffeners welded to it. The<br />
stiffeners passed close to <strong>the</strong> support, creating a<br />
guillotine-like effect. The mate’s foot was caught in<br />
<strong>the</strong> gap when <strong>the</strong> drum rotated and despite wearing<br />
steel-capped safety boots he was severely injured.<br />
The mate was fortunate as immediate hospitalisation and extensive microsurgery<br />
managed to save his toes.<br />
Following this incident <strong>the</strong> winch drums were modified to prevent a recurrence.<br />
This accident highlights <strong>the</strong> dangers <strong>of</strong> working too close to winches. The accident would<br />
have been avoided if <strong>the</strong> chief <strong>of</strong>ficer had employed a method <strong>of</strong> freeing <strong>the</strong> rope which<br />
did not involve close proximity to <strong>the</strong> machinery. One possible method might have been<br />
to put a stopper on <strong>the</strong> mooring rope while continuing to veer, thus using <strong>the</strong> power <strong>of</strong><br />
<strong>the</strong> winch to free <strong>the</strong> rope without creating <strong>the</strong> necessity for personnel to be in close<br />
proximity to it.<br />
Root Cause:<br />
Defect with equipment design.<br />
Financial Cost:<br />
Issue Date: 01/01/02<br />
Case No. 28781<br />
42 43
Personal Injury/Illness<br />
Severe Injuries Result From Failure to Follow Proper Procedures.<br />
The Incident:<br />
This incident occurred on board a tanker lying at anchor in<br />
sheltered waters. The vessel had been having trouble with its SSB<br />
radio and <strong>the</strong> radio <strong>of</strong>ficer had been instructed to investigate this<br />
problem.<br />
Shortly after lunch <strong>the</strong> Master was awakened from his afternoon<br />
nap by a loud thump. When he investigated he found <strong>the</strong> radio<br />
<strong>of</strong>ficer lying injured on <strong>the</strong> deck having fallen 18 metres from <strong>the</strong><br />
mast. The radio <strong>of</strong>ficer who had broken both legs, an arm, a rib and<br />
sustained internal injuries, was evacuated immediately to hospital<br />
where he was placed in intensive care.<br />
This company had compiled and provided <strong>the</strong> ship with a safety<br />
manual which included detailed instructions for working al<strong>of</strong>t. In<br />
addition several copies <strong>of</strong> <strong>the</strong> Code <strong>of</strong> Safe Working Practices for<br />
Merchant Seamen were available on board for <strong>the</strong> crew’s use. The<br />
radio <strong>of</strong>ficer had not complied with <strong>the</strong> requirements <strong>of</strong> ei<strong>the</strong>r <strong>the</strong><br />
Code or <strong>the</strong> safety manual. He was working alone and had not<br />
advised <strong>the</strong> duty deck <strong>of</strong>ficer that he would be working al<strong>of</strong>t. He<br />
was not wearing a safety harness.<br />
Observations:<br />
Although <strong>the</strong> owners had provided <strong>the</strong> vessel with a considerable<br />
quantity <strong>of</strong> safety documentation, that in itself was insufficient to<br />
instil a safety-conscious attitude amongst <strong>the</strong> crew. Unless senior<br />
management take a close interest in enforcing a proper safety<br />
regime on board, a safety culture will not develop within <strong>the</strong><br />
company. If safety consciousness had been highly developed, <strong>the</strong><br />
radio <strong>of</strong>ficer would probably not have considered working al<strong>of</strong>t<br />
without taking <strong>the</strong> proper precautions.<br />
Root Cause:<br />
Insufficient safety environment.<br />
Financial Cost:<br />
The owners had to pay substantial compensation to <strong>the</strong> radio <strong>of</strong>ficer<br />
even though he was primarily responsible for <strong>the</strong> accident occurring.<br />
The total cost to <strong>the</strong> company after costs were taken into account<br />
was almost US$40,000.<br />
Issue Date: 01/01/02<br />
Case No. 23194<br />
44 45
Cargo<br />
Deviation from Agreed Discharge Plan Leads to Cocktail<br />
The Incident:<br />
The vessel involved in this case is a coastal tanker carrying a full cargo <strong>of</strong> four grades <strong>of</strong><br />
lubricating oil. The vessel arrived at <strong>the</strong> discharge berth where she was due to discharge<br />
into both shore tanks and barges moored alongside. After <strong>the</strong> ship was ullaged and samples<br />
taken, a written discharge plan was agreed between <strong>the</strong> ship and <strong>the</strong> terminal. The plan<br />
was signed by <strong>the</strong> ship’s <strong>of</strong>ficers but retained by <strong>the</strong> terminal with no <strong>copy</strong> being left on<br />
board. The details <strong>of</strong> <strong>the</strong> plan were recorded in <strong>the</strong> duty <strong>of</strong>ficer’s note<strong>book</strong>. It had been<br />
agreed that initially two parcels, 500 SN and 100 SN, would be discharged to <strong>the</strong> shore<br />
followed by 200 SN and 150 SN.<br />
The 500 SN and 100 SN manifolds were prepared for <strong>the</strong> cargo hoses. After <strong>the</strong> 500 SN<br />
hose had been connected <strong>the</strong> jetty operator asked whe<strong>the</strong>r <strong>the</strong> second open manifold<br />
was for 150 SN. The duty <strong>of</strong>ficer advised him that it was <strong>the</strong> 100 SN manifold. The jetty<br />
operator told <strong>the</strong> duty <strong>of</strong>ficer that he wanted <strong>the</strong> 150 SN not <strong>the</strong> 100 SN. The duty<br />
<strong>of</strong>ficer reminded <strong>the</strong> jetty operator that it had been agreed in writing that <strong>the</strong> 100 SN<br />
would be discharged before <strong>the</strong> 150 SN. Despite this <strong>the</strong> jetty operator continued to insist<br />
that he wanted 150 SN and as a result <strong>the</strong> manifolds were changed over and <strong>the</strong> hose<br />
connected to <strong>the</strong> 150 SN manifold. After approximately 1½ pumping <strong>the</strong> shore asked <strong>the</strong><br />
vessel to stop despite <strong>the</strong> fact <strong>the</strong>re was approximately 70 metric tons left on board. On<br />
investigation it turned out that despite what <strong>the</strong> jetty operator had said, <strong>the</strong> terminal had<br />
been adhering to <strong>the</strong> original discharge plan with <strong>the</strong> result that 180 tons <strong>of</strong> 150 SN had<br />
been pumped into <strong>the</strong> wrong tank, contaminating <strong>the</strong> 220 tons <strong>of</strong> 100 SN it contained.<br />
Observations:<br />
The vessel had followed <strong>the</strong> correct procedure up<br />
until <strong>the</strong> time <strong>the</strong> second cargo hose was connected.<br />
At that point <strong>the</strong> duty <strong>of</strong>ficer agreed to deviate from<br />
<strong>the</strong> written plan without proper authorisation. If<br />
<strong>the</strong> <strong>of</strong>ficer on watch had insisted that a new cargo<br />
discharge plan had been drawn up or <strong>the</strong> original<br />
one amended in writing, <strong>the</strong> confusion within <strong>the</strong><br />
terminal would have become apparent and <strong>the</strong><br />
contamination would have been avoided.<br />
Root Cause:<br />
Non compliance with procedures.<br />
Financial Cost:<br />
The shipowners and terminal operators negotiated<br />
a commercial settlement with <strong>the</strong> owners <strong>of</strong> <strong>the</strong> oil.<br />
The cost <strong>of</strong> investigating this incident and obtaining<br />
<strong>the</strong> legal advice on which negotiations were based<br />
amounted to US$17,000.<br />
Issue Date: 01/01/02<br />
Case No. 20662<br />
46 47
Cargo<br />
The Cost <strong>of</strong> Ensuring <strong>the</strong> Vessel’s Turnaround<br />
Time can be Outweighed by <strong>the</strong> Final Overall Cost<br />
The Incident:<br />
This claim involved a 5000gt products tanker<br />
discharging two grades <strong>of</strong> cargo simultaneously.<br />
During <strong>the</strong> course <strong>of</strong> <strong>the</strong> discharge cross grade<br />
contamination occurred.<br />
The vessel is designed so that she can carry<br />
a maximum <strong>of</strong> three grades <strong>of</strong> cargo whilst<br />
maintaining two valve separation and on this<br />
particular occasion two grades were carried.<br />
Loading was completed without incident.<br />
Discharge <strong>of</strong> <strong>the</strong> two grades was commenced<br />
simultaneously utilising No.1 pump for one grade<br />
and No.3 for <strong>the</strong> second grade. During <strong>the</strong><br />
course <strong>of</strong> <strong>the</strong> discharge, No.1 pump developed<br />
a leak at <strong>the</strong> forward seal and <strong>the</strong> pump became<br />
unserviceable. The pump was stopped and<br />
<strong>the</strong> pipelines set up to discharge <strong>the</strong> unleaded<br />
gasoline via No.2 cargo pump. The discharge was<br />
continued. At some stage <strong>the</strong>reafter <strong>the</strong> terminal<br />
advised <strong>the</strong> vessel that contamination between<br />
grades had been noted ashore.<br />
Observations:<br />
The design <strong>of</strong> <strong>the</strong> vessel is such that two valve<br />
separation can only be maintained when each <strong>of</strong> <strong>the</strong><br />
three pumps is used on its own designated tanks<br />
or <strong>the</strong> two outside pumps (nos 1 & 3) are utilised;<br />
whenever consecutive pumps are lined up on tanks<br />
<strong>of</strong> one <strong>of</strong> <strong>the</strong> o<strong>the</strong>r systems <strong>the</strong>n only one valve<br />
separation is possible. Unfortunately in this incident,<br />
<strong>the</strong> decision to utilise No.2 pump on No.1 system<br />
cargo tanks resulted in single valve separation<br />
between <strong>the</strong> two grades. (It is believed that during<br />
<strong>the</strong> stripping phase <strong>of</strong> discharging one <strong>of</strong> <strong>the</strong> grades,<br />
<strong>the</strong> pressure differential across <strong>the</strong> valve allowed <strong>the</strong><br />
contamination to take place).<br />
Two valve separation between grades is considered<br />
<strong>the</strong> minimum acceptable by <strong>the</strong> petroleum industry<br />
as <strong>the</strong> likelihood <strong>of</strong> two valves failing at <strong>the</strong> same<br />
time is considered to be acceptably less than <strong>the</strong><br />
failure <strong>of</strong> a single valve. [Failure can be caused by: i)<br />
a defective seal; ii) debris lying in <strong>the</strong> valve seat; and<br />
iii) <strong>the</strong> valve not being closed fully].<br />
In this incident, <strong>the</strong> decision to continue discharging<br />
both grades simultaneously after <strong>the</strong> pump<br />
failure was wrong, however it is not known what<br />
commercial pressures, if any, were placed upon <strong>the</strong><br />
vessel to expedite <strong>the</strong> discharge.<br />
In such circumstances if shore terminals insist on<br />
ships continuing operations, <strong>the</strong> representative<br />
making <strong>the</strong> request should be made fully aware<br />
<strong>of</strong> <strong>the</strong> possible consequences and requested to<br />
accept <strong>the</strong> responsibility for any adverse effects. If<br />
responsibility is to lie with <strong>the</strong> Master and vessel,<br />
<strong>the</strong>n <strong>the</strong> operation should be continued within <strong>the</strong><br />
limitations <strong>of</strong> <strong>the</strong> vessel’s design.<br />
Root Cause:<br />
Failure to comply with vessel design.<br />
Financial Cost:<br />
The cost <strong>of</strong> this claim is US$110,000.<br />
Issue Date: 01/01/02<br />
Case No. 37817<br />
48 49
Cargo<br />
Two Valves are Better than One<br />
The Incident:<br />
This vessel was a small parcel tanker time chartered to an oil major,<br />
plying between two <strong>of</strong> <strong>the</strong>ir terminals. The vessel was fitted with five<br />
sets <strong>of</strong> cargo wing tanks, fed by a ring main pipeline system. On <strong>the</strong><br />
voyage in question <strong>the</strong> vessel was ordered to load two grades <strong>of</strong> motor<br />
spirit. The first, unleaded petrol, was loaded into 2 and 4 wing tanks.<br />
This was followed by leaded petrol being loaded into 1 and 5 wing tanks.<br />
Number 3 wing tanks remained empty.<br />
On arrival at <strong>the</strong> discharge berth both grades were to be discharged<br />
ashore simultaneously, <strong>the</strong> leaded petrol was to be discharged using<br />
<strong>the</strong> portside pump/line system and <strong>the</strong> unleaded via <strong>the</strong> starboard<br />
side pump/line system. Shortly after discharge commenced <strong>the</strong><br />
starboard pump broke down. As a consequence 1 and 5 wing tanks<br />
were completely discharged whereafter <strong>the</strong> line was flushed with fresh<br />
water and disconnected. The unleaded hose was <strong>the</strong>n connected to <strong>the</strong><br />
portside pump/line system which was <strong>the</strong>n used to discharge <strong>the</strong> second<br />
parcel. Shortly after discharge resumed terminal personnel informed<br />
<strong>the</strong> vessel that measurement <strong>of</strong> shore tanks indicated that an additional<br />
90 cubic metres <strong>of</strong> product had been discharged with <strong>the</strong> first parcel <strong>of</strong><br />
leaded petrol. Discharge operations were stopped and an investigation<br />
was mounted. The investigation revealed that a crossover gate valve in<br />
number 2 port cargo tank had not been properly closed, with <strong>the</strong> result<br />
that unleaded petrol had been drawn from <strong>the</strong> starboard line system<br />
and discharged with <strong>the</strong> leaded petrol.<br />
Observations:<br />
The tanker’s ring main system only permitted single valve separation<br />
between <strong>the</strong> two grades <strong>of</strong> cargo with <strong>the</strong> result that <strong>the</strong> failure <strong>of</strong><br />
a valve or operator error in <strong>the</strong> manipulation <strong>of</strong> <strong>the</strong> valves would<br />
inevitably result in cross contamination. Subsequent to this incident<br />
<strong>the</strong> vessel’s pipeline system was modified to give proper segregation<br />
between cargo grades.<br />
Root Cause:<br />
Failure to comply with vessel design requirement.<br />
Financial Cost:<br />
On this occasion <strong>the</strong> oil company was able to resolve <strong>the</strong> problem<br />
<strong>of</strong> <strong>the</strong> contaminated fuel by blending and no cargo claim was made.<br />
Never<strong>the</strong>less <strong>the</strong> costs <strong>of</strong> investigating <strong>the</strong> matter amounted to<br />
approximately US$1,000.<br />
Issue Date: 01/01/02<br />
Case No. 19597<br />
50 51
Cargo<br />
Poor Tanker Practices Leads to Expensive Delay for Member.<br />
The Incident:<br />
This tanker had been chartered to a company which had a contract <strong>of</strong><br />
affreightment with a major oil company. The vessel was ordered to load<br />
premium motor spirit and automotive diesel oil at two separate berths.<br />
The motor spirit was loaded in 2 wings and 4 wings at <strong>the</strong> first berth<br />
and <strong>the</strong> automotive diesel oil was loaded in 1 and 3 wings at <strong>the</strong> second<br />
berth. On arrival at <strong>the</strong> discharge port <strong>the</strong> cargo in 2 wings was rejected<br />
by <strong>the</strong> consignee as being <strong>of</strong>f-spec. The remaining cargo was found<br />
to be within <strong>the</strong> specification and was discharged. After discharge <strong>the</strong><br />
shore tank was sampled and it was discovered that not only were both<br />
parcels <strong>of</strong>f-specification but <strong>the</strong> outturn <strong>of</strong> volume <strong>of</strong> <strong>the</strong> motor spirit<br />
had apparently increased by over 100 tons while <strong>the</strong> volume <strong>of</strong> diesel<br />
oil had decreased by a similar figure. The contaminated oils could not be<br />
reprocessed at <strong>the</strong> discharge port and <strong>the</strong> vessel was delayed for over<br />
seven weeks while owners, charterers and <strong>the</strong> oil company argued over<br />
<strong>the</strong> disposal <strong>of</strong> <strong>the</strong> contaminated oil. The terminal lodged a claim for<br />
US$420,000, this being <strong>the</strong> value <strong>of</strong> <strong>the</strong> entire cargo.<br />
Observations:<br />
A thorough investigation by surveyors appointed<br />
by <strong>the</strong> Club revealed that <strong>the</strong> vessel had only been<br />
designed to carry a single grade <strong>of</strong> cargo, with<br />
<strong>the</strong> result that it was impossible to follow normal<br />
tanker practice in separating different grades <strong>of</strong><br />
product by two or more valves. The surveyors also<br />
discovered that after completing loading at <strong>the</strong> first<br />
berth, certain valves were left open, allowing <strong>the</strong><br />
cargo in 2 wings to become contaminated with<br />
diesel oil. The surveyor’s investigation also showed<br />
that during <strong>the</strong> discharge operation some more<br />
valves were opened in error, contaminating <strong>the</strong><br />
remainder <strong>of</strong> <strong>the</strong> cargo. The surveyors were critical<br />
<strong>of</strong> <strong>the</strong> method and effectiveness <strong>of</strong> line-clearing at<br />
<strong>the</strong> discharge port.<br />
Root Cause:<br />
Failure to comply with ship design requirements.<br />
Financial Cost:<br />
In this case <strong>the</strong> owners were extremely fortunate<br />
as <strong>the</strong> provisions <strong>of</strong> <strong>the</strong> charter party enabled <strong>the</strong>m<br />
to pass responsibility for cargo contamination on<br />
to <strong>the</strong> charterers. Never<strong>the</strong>less <strong>the</strong> costs <strong>of</strong> <strong>the</strong><br />
investigation alone amounted to US$17,000. In<br />
addition to this <strong>the</strong> owners were unable to trade<br />
<strong>the</strong> vessel for approximately two months.<br />
This vessel is no longer entered in <strong>the</strong> Club.<br />
Issue Date: 01/01/02<br />
Case No. 18724<br />
52 53
Cargo<br />
Master’s Commercial Awareness could have Reduced Claim<br />
The Incident:<br />
The claim arose on board a coastal tanker carrying<br />
premium motor spirit. The bill <strong>of</strong> lading was issued<br />
using <strong>the</strong> shore terminal’s figures. As this figure was<br />
greater than <strong>the</strong> quantity calculated a letter <strong>of</strong> protest<br />
was issued by <strong>the</strong> Master to <strong>the</strong> loading terminal.<br />
At <strong>the</strong> discharge port <strong>the</strong> vessel’s cargo pumps<br />
lost suction before <strong>the</strong> tanks were completely<br />
dry. It proved impossible to regain suction and <strong>the</strong><br />
cargo remaining on board was considered to be<br />
unpumpable. On completion <strong>of</strong> discharge <strong>the</strong> vessel<br />
was heavily trimmed by <strong>the</strong> stern with <strong>the</strong> result<br />
that <strong>the</strong> cargo residues lay in wedges at <strong>the</strong> ends <strong>of</strong><br />
<strong>the</strong> cargo tanks aft <strong>of</strong> <strong>the</strong> sounding pipes. The actual<br />
quantity remaining on board could not <strong>the</strong>refore be<br />
accurately assessed.<br />
The receiving terminal claimed short delivery <strong>of</strong><br />
over 50 metric tons based solely on <strong>the</strong> difference<br />
between <strong>the</strong> bill <strong>of</strong> lading figure and <strong>the</strong> shore outturn<br />
figure.<br />
At <strong>the</strong> next berth surveyors appointed by <strong>the</strong> Club<br />
attended on board and by reducing <strong>the</strong> vessel’s trim<br />
were able to accurately establish <strong>the</strong> amount <strong>of</strong><br />
cargo remaining on board. It was found to be just<br />
under 22 metric tons and not over 50 as alleged<br />
by <strong>the</strong> consignee. The value <strong>of</strong> <strong>the</strong> difference was<br />
approximately US$7,000. The evidential value <strong>of</strong> our<br />
surveyor’s report was however seriously weakened<br />
because <strong>the</strong> survey took place some time after<br />
discharge had been completed, when consignee’s<br />
representatives were not in attendance.<br />
Observations:<br />
If <strong>the</strong> vessel’s Master had reduced <strong>the</strong> vessel’s trim and properly<br />
quantified <strong>the</strong> unpumpable ROB before leaving <strong>the</strong> discharge berth<br />
while <strong>the</strong> consignee’s surveyor was still in attendance, <strong>the</strong> owners<br />
would have been in a much stronger position to resist <strong>the</strong> short<br />
delivery claim.<br />
Root Cause:<br />
Insufficient operation procedures.<br />
Financial Cost:<br />
It was possible to negotiate a settlement <strong>of</strong> <strong>the</strong> short landing claim<br />
however <strong>the</strong> total cost including surveyor’s fees exceeded US$9,000.<br />
Issue Date: 01/01/02<br />
Case No. 19772<br />
54 55
Cargo<br />
Out <strong>of</strong> Sight Really Can Mean Out <strong>of</strong> Mind<br />
The Incident:<br />
This claim involved a products tanker delivering<br />
contaminated cargo on three consecutive voyages.<br />
On <strong>the</strong> first two occasions <strong>the</strong> terminal accepted <strong>the</strong><br />
cargo, but although finally accepting it <strong>the</strong> third time<br />
it was with some reluctance.<br />
During <strong>the</strong> course <strong>of</strong> each <strong>of</strong> <strong>the</strong> three discharges<br />
<strong>the</strong> products to varying degrees were found to<br />
be contaminated with water. Blending or fur<strong>the</strong>r<br />
refining was required to return <strong>the</strong> products to <strong>the</strong><br />
original specifications.<br />
The cause <strong>of</strong> <strong>the</strong> contamination proved difficult<br />
to find because <strong>the</strong> water was noted to have very<br />
low chlorides which indicated (incorrectly) that<br />
<strong>the</strong> contamination was not caused by seawater. In<br />
addition, during <strong>the</strong> final discharge <strong>the</strong> contamination<br />
was noted to be intermittent.<br />
It was finally assumed that <strong>the</strong> water was entering<br />
<strong>the</strong> cargo tanks through defective valve glands –<br />
although <strong>the</strong> cargo sample from <strong>the</strong> tanks was within<br />
specification!<br />
Upon completion <strong>of</strong> <strong>the</strong> third discharge <strong>the</strong> vessel<br />
sailed and anchored <strong>of</strong>f <strong>the</strong> port.<br />
Fur<strong>the</strong>r investigation by <strong>the</strong> crew at this time<br />
determined that “several years” prior to this spate<br />
<strong>of</strong> contaminations, <strong>the</strong> vessel had experienced cargo<br />
leaking out through a sea valve. As a result a 6mm<br />
blank was inserted on <strong>the</strong> outboard side <strong>of</strong> <strong>the</strong> sea<br />
valve, and unfortunately this had been forgotten. As<br />
time passed <strong>the</strong> blank had corroded through and<br />
when ballasting, unbeknown to <strong>the</strong> ship’s crew, a<br />
section <strong>of</strong> <strong>the</strong> pipeline filled with water. When cargo<br />
was subsequently being discharged, this water was<br />
<strong>the</strong>n drawn into <strong>the</strong> cargo.<br />
Observations:<br />
Whenever a blank is inserted into a pipeline it<br />
should be made as conspicuous as possible and all<br />
staff associated with cargo operations made aware<br />
<strong>of</strong> its existence, including subsequent crews.<br />
In addition, a blank inserted in a pipeline as a result<br />
<strong>of</strong> a leaking valve is only a temporary measure and<br />
should not be left in place for years on end. The<br />
efficiency <strong>of</strong> <strong>the</strong> overhaul <strong>of</strong> ship side valves during<br />
dry docking must also be questioned.<br />
Root Cause:<br />
Insufficient maintenance procedures.<br />
Financial Cost:<br />
Because <strong>the</strong> receivers accepted most <strong>of</strong> <strong>the</strong><br />
contaminated cargoes without complaint, <strong>the</strong> overall<br />
cost <strong>of</strong> this claim is US$5,000.<br />
Issue Date: 01/01/02<br />
Case No. 38847<br />
56 57
Cargo<br />
Poor Line Washing Probably Caused Contamination<br />
The Incident:<br />
This is a case <strong>of</strong> cargo contamination on board a parcel tanker. On its previous voyage <strong>the</strong><br />
tanker carried a full cargo <strong>of</strong> gas oil. After discharge <strong>the</strong> tanks were washed in preparation<br />
for carrying a number <strong>of</strong> high quality products. Prior to loading <strong>the</strong> tanks were inspected<br />
by an independent inspector and passed as being clean, dry and suitable for <strong>the</strong> products<br />
to be loaded. A number <strong>of</strong> products were <strong>the</strong>n loaded including a parcel <strong>of</strong> solvent C9 in<br />
4 wings. On arrival at discharge port <strong>the</strong> samples <strong>of</strong> <strong>the</strong> solvent taken by <strong>the</strong> consignees’<br />
surveyor showed a slight change in colour. Gas chromatography analysis revealed that <strong>the</strong><br />
product had been contaminated by very small quantities <strong>of</strong> gas oil. Consignees claimed that<br />
<strong>the</strong> slight change in colour was sufficient to render <strong>the</strong> product unmarketable and rejected<br />
<strong>the</strong> entire consignment. The contaminated cargo was eventually sold to a salvage buyer for<br />
less than half its original value.<br />
Observations:<br />
This incident highlights <strong>the</strong> importance <strong>of</strong> tank cleaning and line washing in preparation<br />
for <strong>the</strong> carriage <strong>of</strong> high grade products and chemicals. In this case <strong>the</strong> cause <strong>of</strong> <strong>the</strong><br />
contamination was never properly determined. The vessel’s tank coatings were in good<br />
condition and <strong>the</strong> tanks had been passed by an independent surveyor. The most likely<br />
source <strong>of</strong> contamination seems to be inadequate or incomplete line washing, with <strong>the</strong><br />
result that a plug <strong>of</strong> <strong>the</strong> previous cargo became trapped in <strong>the</strong> pipeline system. It is vital<br />
that line washing be arranged in such a way as to ensure that every section <strong>of</strong> <strong>the</strong> pipeline<br />
system is thoroughly flushed through during <strong>the</strong> process.<br />
Root Cause:<br />
Inadequate line washing.<br />
Financial Cost:<br />
The total cost <strong>of</strong> this claim after <strong>the</strong> proceeds <strong>of</strong> <strong>the</strong> salvage sale had been taken into<br />
account exceeded US$73,000.<br />
Issue Date: 01/01/02<br />
Case No. 24249<br />
58 59
Navigation<br />
With <strong>the</strong> Tide is Against Convention<br />
The Incident:<br />
This incident occurred when a 1,500 GRT tanker was berthing at an<br />
oil jetty. During <strong>the</strong> berthing manoeuvre <strong>the</strong> vessel’s bow came into<br />
contact with <strong>the</strong> hose gantry on <strong>the</strong> jetty, damaging both <strong>the</strong> gantry and<br />
two cargo hoses. In his statement <strong>the</strong> Master alleged that <strong>the</strong> cause <strong>of</strong><br />
<strong>the</strong> contact was <strong>the</strong> vessel failing to respond to an astern engine order.<br />
Observations:<br />
According to both <strong>the</strong> Chief Engineer and Engineering Officer <strong>of</strong><br />
<strong>the</strong> watch, <strong>the</strong>re was no mechanical problem during <strong>the</strong> berthing<br />
operation. Subsequent investigation by a surveyor revealed that <strong>the</strong><br />
Master had been attempting to berth with <strong>the</strong> tide under his stern. It<br />
is highly likely that <strong>the</strong> Master simply misjudged <strong>the</strong> effect <strong>of</strong> <strong>the</strong> tide<br />
when applying astern power. This accident would probably have been<br />
avoided if <strong>the</strong> Master had adopted a conventional uptide approach to<br />
<strong>the</strong> berth.<br />
Root Cause:<br />
Human error.<br />
Financial Cost:<br />
The costs <strong>of</strong> repairs to <strong>the</strong> jetty exceeded US$46,000.<br />
Issue Date: 01/01/02<br />
Case No. 20910<br />
60 61
Navigation<br />
Member’s Involvement with Delay to Deep Sea Vessel Proves Expensive.<br />
The Incident:<br />
This incident involved a small bunker barge which had<br />
been engaged to supply lube oil to an ocean going<br />
vessel at anchor. During <strong>the</strong> bunkering operation <strong>the</strong><br />
deep sea vessel’s gangway had been lowered and<br />
used to provide access to and from <strong>the</strong> bunker barge.<br />
After bunker operations had been completed <strong>the</strong><br />
crew did not hoist <strong>the</strong> gangway before casting <strong>of</strong>f<br />
<strong>the</strong> barge’s mooring lines. As <strong>the</strong> barge manoeuvred<br />
away from <strong>the</strong> side <strong>of</strong> <strong>the</strong> ocean going vessel it came<br />
into contact with, and damaged, <strong>the</strong> ship’s gangway.<br />
Although <strong>the</strong> negligence <strong>of</strong> <strong>the</strong> deep sea vessel’s crew<br />
was a major contributing factor in this loss, <strong>the</strong> Club<br />
was advised that <strong>the</strong> barge would be held liable for<br />
not exercising sufficient care while manoeuvring away<br />
from <strong>the</strong> vessel’s side.<br />
Observations:<br />
This claim illustrates how a relatively minor incident<br />
can be greatly inflated if <strong>the</strong> damage causes delay to<br />
a large vessel. In this case <strong>the</strong> problem could have<br />
been avoided if <strong>the</strong> bunker barge had insisted on <strong>the</strong><br />
gangway being raised clear before departing.<br />
Root Cause:<br />
Failure to comply with procedures.<br />
Financial Cost:<br />
Repairs to <strong>the</strong> accommodation ladder took four<br />
days and cost US$13,000. In addition to <strong>the</strong> cost <strong>of</strong><br />
repairs <strong>the</strong> owners <strong>of</strong> <strong>the</strong> deep sea vessel claimed<br />
four days’ loss <strong>of</strong> hire which when combined<br />
with additional port dues, survey fees and o<strong>the</strong>r<br />
miscellaneous expenses brought <strong>the</strong> total claim<br />
against our Member to almost US$36,000. Although<br />
we were successful in negotiating a settlement at a<br />
reduced figure, <strong>the</strong> total cost to <strong>the</strong> barge owners<br />
after surveyors’ and correspondents’ fees had been<br />
paid exceeded US$27,000.<br />
Issue Date: 01/01/02<br />
Case No. 20339<br />
62 63
Navigation<br />
Rushed Approach Results in Collision<br />
The Incident:<br />
In <strong>the</strong> early hours a bunker tanker finished loading a cargo <strong>of</strong> fuel oil<br />
and left <strong>the</strong> berth bound for <strong>the</strong> anchorage to await <strong>the</strong> arrival <strong>of</strong> <strong>the</strong><br />
deep sea vessel she was to service. The anchorage was crowded and<br />
<strong>the</strong> vessel worked through <strong>the</strong> moored vessels at slow speed looking for<br />
a suitable spot to drop <strong>the</strong> anchor. The vessel came upon a clear area<br />
and <strong>the</strong> Master made a snap decision to anchor in that spot. The tanker<br />
had <strong>the</strong> wind on her starboard quarter and a 2 knot following tide. To<br />
bring <strong>the</strong> vessel head to wind and tide <strong>the</strong> helm was put hard aport and<br />
<strong>the</strong> engine full astern. Unfortunately <strong>the</strong> Master totally misjudged <strong>the</strong><br />
strength <strong>of</strong> <strong>the</strong> tide and <strong>the</strong> vessel was swept broadside onto <strong>the</strong> bows<br />
<strong>of</strong> an anchored vessel. Number 3 cargo oil tank was breached and over<br />
20 cubic metres <strong>of</strong> heavy fuel oil spilled into <strong>the</strong> water.<br />
Observations:<br />
This incident would probably have been avoided if<br />
<strong>the</strong> Master had not been in such a hurry to anchor<br />
and had adopted a more conventional approach.<br />
Instead <strong>of</strong> trying to swing <strong>the</strong> vessel immediately<br />
he should have continued on until he could turn his<br />
vessel safely and approach <strong>the</strong> anchorage position<br />
heading into wind and tide. The method <strong>of</strong> approach<br />
adopted prevented him properly assessing <strong>the</strong><br />
effects <strong>of</strong> wind and tide on his vessel and as a result<br />
he completely misjudged his approach.<br />
Root Cause:<br />
Human error.<br />
Financial Cost:<br />
In addition to <strong>the</strong> cost <strong>of</strong> repairs to <strong>the</strong> anchored<br />
tanker <strong>the</strong> owners received a substantial claim from<br />
<strong>the</strong> Port Authority for oil pollution monitoring and<br />
clean up operations. This brought <strong>the</strong> total cost<br />
excluding <strong>the</strong> cost <strong>of</strong> damage to his own vessel to<br />
over US$82,000.<br />
Issue Date: 01/01/02<br />
Case No. 19193<br />
64 65
Navigation<br />
But We’ve Always Done it That Way<br />
The Incident:<br />
We have been advised <strong>of</strong> <strong>the</strong> following case,<br />
featured in <strong>the</strong> Marine Accident Investigation Branch<br />
(MAIB) safety digest No1/2007 (see below link for<br />
<strong>the</strong> document) that we feel will be <strong>of</strong> great interest<br />
to our Members.<br />
“Poor bridge team management practices while<br />
approaching and entering a narrow channel led<br />
directly to <strong>the</strong> grounding <strong>of</strong> a 1,845gt tanker. It had<br />
been <strong>the</strong> early hours <strong>of</strong> <strong>the</strong> morning and <strong>the</strong> vessel<br />
was returning to her usual load port, in ballast. The<br />
bridge watch consisted <strong>of</strong> an <strong>of</strong>ficer <strong>of</strong> <strong>the</strong> watch, a<br />
lookout and <strong>the</strong> Master.<br />
The vessel had passed through <strong>the</strong> same channel a<br />
few days earlier on her loaded passage, and reciprocal<br />
courses had been chosen for <strong>the</strong> return passage.<br />
The planned track involved a 40 degree alteration<br />
<strong>of</strong> course just one ship’s length before <strong>the</strong> entrance<br />
to <strong>the</strong> channel. The bridge that spanned <strong>the</strong> narrow<br />
passage at its entrance had a white transit light which<br />
marked <strong>the</strong> centre <strong>of</strong> <strong>the</strong> bridge and <strong>the</strong> channel.<br />
As <strong>the</strong> vessel approached <strong>the</strong> channel at full speed,<br />
<strong>the</strong> Master took <strong>the</strong> con, switched <strong>the</strong> helm to hand<br />
steering and, against company instructions, started<br />
to steer <strong>the</strong> vessel himself towards and through<br />
<strong>the</strong> narrow entrance. The <strong>of</strong>ficer <strong>of</strong> <strong>the</strong> watch<br />
was looking on without a defined monitoring role.<br />
However, he had plotted a position on <strong>the</strong> chart,<br />
which showed <strong>the</strong> vessel to be north <strong>of</strong> <strong>the</strong> charted<br />
course line, and <strong>the</strong> Master had altered <strong>the</strong> vessel’s<br />
heading slightly in an attempt to partly compensate.<br />
Before <strong>the</strong> vessel had moved far towards her track,<br />
<strong>the</strong> Master decided to steer directly for <strong>the</strong> white<br />
light which indicated <strong>the</strong> centre <strong>of</strong> <strong>the</strong> bridge’s span.<br />
The vessel had recently been fitted with an<br />
electronic chart system following a similar accident<br />
on ano<strong>the</strong>r <strong>of</strong> <strong>the</strong> company’s ships. The Master<br />
could see <strong>the</strong> electronic chart display, but was not<br />
using it o<strong>the</strong>r than to give him a rough indication<br />
<strong>of</strong> her position. He had never received any formal<br />
training in <strong>the</strong> use <strong>of</strong> this equipment.<br />
As <strong>the</strong> vessel passed under <strong>the</strong> centre <strong>of</strong> <strong>the</strong> bridge,<br />
<strong>the</strong> Master used 10 degrees <strong>of</strong> port helm to bring<br />
her around 40 degrees to <strong>the</strong> required heading for<br />
passage. No allowance, mental or o<strong>the</strong>rwise, had<br />
been made for <strong>the</strong> vessel’s advance and, unsurprisingly,<br />
she grounded on <strong>the</strong> sou<strong>the</strong>rn edge <strong>of</strong> <strong>the</strong> channel.<br />
The vessel sustained significant hull damage. She was<br />
holed in one segregated ballast tank but, fortunately,<br />
<strong>the</strong>re was no pollution as a result <strong>of</strong> <strong>the</strong> incident.<br />
Observations:<br />
1. The MAIB has frequently heard it argued that it<br />
is unrealistic to expect coastal shipping to adopt<br />
<strong>the</strong> navigational practices that would normally be<br />
found on deep sea vessels, because <strong>of</strong> <strong>the</strong> nature<br />
<strong>of</strong> <strong>the</strong> trade and <strong>the</strong> size <strong>of</strong> crews. Owners and<br />
Masters must ensure that <strong>the</strong>y do not use this<br />
argument to justify bad practice and complacency.<br />
2. The wheelhouse was well manned with qualified<br />
personnel, but <strong>the</strong> team was not used effectively<br />
to ensure <strong>the</strong> vessel’s safe passage. In this case,<br />
a better arrangement would have been for <strong>the</strong><br />
seaman to have steered <strong>the</strong> vessel while <strong>the</strong><br />
OOW plotted positions and <strong>the</strong> Master oversaw<br />
<strong>the</strong> whole safe operation.<br />
3. Passage planning was ineffective. A planned track<br />
that allowed <strong>the</strong> vessel to alter course and steady<br />
up on <strong>the</strong> new heading well before <strong>the</strong> entrance<br />
to <strong>the</strong> channel would have ensured this accident<br />
was avoided. Reciprocal courses were chosen<br />
for expediency, without consideration <strong>of</strong> this and<br />
possibly o<strong>the</strong>r factors. The use <strong>of</strong> parallel indexing<br />
techniques would have helped to ensure <strong>the</strong><br />
vessel was on, and maintaining, <strong>the</strong> correct track.<br />
4. Some <strong>of</strong> <strong>the</strong>se lessons had been discovered by<br />
<strong>the</strong> company as a result <strong>of</strong> a very similar accident<br />
a few months previously. However, <strong>the</strong> lessons<br />
had not been effectively communicated to this<br />
vessel or her Master. It is an unfortunate truth<br />
that accidents are a key source <strong>of</strong> useful safety<br />
advice, and every effort should be taken to learn<br />
and promulgate <strong>the</strong> lessons so that recurrence<br />
can be avoided”.<br />
Source <strong>of</strong> information - Marine Accident<br />
Investigation Branch (MAIB) safety digest No1/2007<br />
- http://www.maib.gov.uk/publications/safety_<br />
digests/2007/safety_digest_1_2007.cfm<br />
Root Cause:<br />
Insufficient navigation procedures.<br />
Issue Date: 18/04/07<br />
Case No. 12480<br />
66 67
Navigation<br />
Insufficient Ballast Causes Loss <strong>of</strong> Control While Berthing<br />
The Incident:<br />
This incident involved damage to a loading arm<br />
at a small oil jetty. The oil jetty in question was<br />
specifically designed for small vessels and is typical <strong>of</strong><br />
many in <strong>the</strong> region. The berth consisted <strong>of</strong> a central<br />
section containing <strong>the</strong> loading arms on ei<strong>the</strong>r side<br />
<strong>of</strong> which was a mooring dolphin connected to <strong>the</strong><br />
berth by walkways.<br />
The incident occurred as <strong>the</strong> tanker was<br />
manoeuvring alongside <strong>the</strong> berth. The tanker was<br />
berthing in a light condition without tug assistance.<br />
The forward draft was only 0.6 metres. The wind<br />
was blowing onto <strong>the</strong> berth as <strong>the</strong> Master made<br />
his approach into <strong>the</strong> current. As he stopped<br />
his vessel parallel to <strong>the</strong> berth, <strong>the</strong> high windage<br />
forward caused <strong>the</strong> bows to fall <strong>of</strong>f. The bow <strong>of</strong><br />
<strong>the</strong> vessel entered <strong>the</strong> space between <strong>the</strong> dolphin<br />
and <strong>the</strong> berth, coming to rest with <strong>the</strong> vessel’s bow<br />
in contact with <strong>the</strong> central section. To extricate<br />
himself <strong>the</strong> Master put his engines astern and in <strong>the</strong><br />
process <strong>the</strong> fo’c’sle railing caught <strong>the</strong> end loading<br />
arm, severely damaging it.<br />
Observations:<br />
Cargo loading arms on small jetties are particularly<br />
susceptible to damage by ships as <strong>the</strong>y are usually<br />
mounted close to <strong>the</strong> edge <strong>of</strong> <strong>the</strong> berth. This<br />
incident could have been avoided by ballasting <strong>the</strong><br />
forward end <strong>of</strong> <strong>the</strong> tanker to reduce <strong>the</strong> windage<br />
and increase <strong>the</strong> grip <strong>of</strong> <strong>the</strong> forefoot in <strong>the</strong> water.<br />
If operational considerations made this undesirable<br />
<strong>the</strong>n <strong>the</strong> assistance <strong>of</strong> a tug should have been sought.<br />
Root Cause:<br />
Inadequate operational considerations.<br />
Financial Cost:<br />
The cost <strong>of</strong> repairs to <strong>the</strong> loading arm exceeded<br />
US$100,000.<br />
Issue Date: 01/01/02<br />
Case No. 20614<br />
68 69
Navigation<br />
Know Your Ship<br />
The Incident:<br />
This accident occurred as a 3,000 GRT tanker attempted to berth alongside an oil jetty in<br />
marginal conditions without tug assistance. The vessel was trying to berth for <strong>the</strong> fourth<br />
time, <strong>the</strong> three prior approaches had to be aborted because <strong>of</strong> <strong>the</strong> effects <strong>of</strong> wind and<br />
current. On this occasion <strong>the</strong> approach to <strong>the</strong> berth was going well with <strong>the</strong> vessel due<br />
to dock portside to. As she approached <strong>the</strong> berth <strong>the</strong> helm was put hard astarboard,<br />
<strong>the</strong> forward spring sent way and <strong>the</strong> engines put astern. The vessel did not respond to<br />
<strong>the</strong> helm and <strong>the</strong> ship’s port bow landed heavily on <strong>the</strong> jetty, damaging <strong>the</strong> concrete<br />
structure and <strong>the</strong> fendering system.<br />
Observations:<br />
The Club appointed a surveyor to investigate <strong>the</strong> occurrence. The surveyor discovered<br />
that <strong>the</strong> vessel was fitted with a lefthanded propeller. The transverse thrust generated<br />
when a lefthanded propeller is run astern tends to cant <strong>the</strong> bow to port ra<strong>the</strong>r than<br />
to starboard as is <strong>the</strong> case with <strong>the</strong> more usual righthanded propeller. It is likely that in<br />
<strong>the</strong> marginal circumstances <strong>the</strong> transverse thrust generated when <strong>the</strong> engines were put<br />
astern was sufficient to counteract <strong>the</strong> effect <strong>of</strong> putting <strong>the</strong> helm hard astarboard.<br />
Root Cause:<br />
Crew unfamiliar with <strong>the</strong>ir vessel.<br />
Financial Cost:<br />
The cost <strong>of</strong> repairs to <strong>the</strong> jetty including survey costs totalled US$15,500.<br />
Issue Date: 01/01/02<br />
Case No. 22217<br />
70 71
Navigation<br />
Good Seamanship is Still as Important as Ever<br />
The Incident:<br />
This case involves damage to a deep sea vessel while unberthing a bunkering barge.<br />
The deep sea vessel was lying head to tide which was running at approximately 1 knot.<br />
The wind was blowing on her starboard bow at about force 3 to 4. The bunker barge<br />
was secured alongside her starboard side. After delivering <strong>the</strong> fuel <strong>the</strong> Captain <strong>of</strong> <strong>the</strong><br />
bunker barge gave instructions to single up to one headline and <strong>the</strong> forward spring. By<br />
steaming gently ahead into <strong>the</strong> spring and heaving on <strong>the</strong> headline <strong>the</strong> stern was sprung<br />
<strong>of</strong>f to an angle <strong>of</strong> about 30°. The lines were let go and <strong>the</strong> engines put slow astern. With<br />
<strong>the</strong> bunker barge in a light condition <strong>the</strong> bows were high in <strong>the</strong> water and as she moved<br />
away <strong>the</strong> wind caught <strong>the</strong> bows, swinging <strong>the</strong>m towards <strong>the</strong> deep sea vessel. The Captain<br />
<strong>of</strong> <strong>the</strong> bunker barge stopped his engines in <strong>the</strong> hope <strong>of</strong> s<strong>of</strong>tening <strong>the</strong> contact, <strong>the</strong> wind<br />
however continued to push <strong>the</strong> vessel’s bows to leeward with increasing speed until she<br />
collided with <strong>the</strong> deep sea vessel, scraping down her side.<br />
Observations:<br />
In conditions such as <strong>the</strong>se it is essential that full<br />
account is taken <strong>of</strong> <strong>the</strong> effects <strong>of</strong> wind and tide.<br />
Bold and decisive action must be taken and full use<br />
made <strong>of</strong> engine and rudder. If <strong>the</strong> Captain <strong>of</strong> <strong>the</strong><br />
bunker barge had put his engines to full astern after<br />
springing his stern out it is quite possible that he<br />
would have gained sufficient stern way to carry his<br />
ship clear <strong>of</strong> <strong>the</strong> ocean going vessel before much<br />
damage was done. In stopping his engines he left his<br />
vessel at <strong>the</strong> mercy <strong>of</strong> <strong>the</strong> wind and rendered <strong>the</strong><br />
collision inevitable.<br />
With <strong>the</strong> prevailing wind and current <strong>the</strong> Master<br />
<strong>of</strong> <strong>the</strong> bunker barge should have let go forward<br />
and held onto his stern spring, steaming astern as<br />
necessary to spring <strong>the</strong> bow <strong>of</strong>f. The current on <strong>the</strong><br />
bow would have been sufficient to counteract <strong>the</strong><br />
effects <strong>of</strong> <strong>the</strong> wind and <strong>the</strong> transverse thrust from<br />
<strong>the</strong> propeller as she moved <strong>of</strong>f ahead would help lift<br />
<strong>the</strong> bunker barge’s stern clear <strong>of</strong> <strong>the</strong> deep sea vessel.<br />
Root Cause:<br />
Human error.<br />
Financial Cost:<br />
This owner was fortunate for although <strong>the</strong> damage<br />
to <strong>the</strong> deep sea vessel extended for some distance<br />
down its side <strong>the</strong> indentation was not deep enough<br />
to worry <strong>the</strong> class society and as a result a claim was<br />
not pursued.<br />
Issue Date: 01/01/02<br />
Case No. 22496<br />
72 73
Operations<br />
Luck has Staring Role in Preventing Pollution<br />
The Incident:<br />
A bunker tanker was engaged in delivering bunkers<br />
to an ocean going vessel. The transfer plan was to<br />
discharge numbers 2 and 5 tanks simultaneously<br />
using a separate pump on each tank but discharging<br />
into a common line. As <strong>the</strong> oil transfer commenced<br />
it was noted that <strong>the</strong> discharge pressure gauge<br />
on <strong>the</strong> pump connected to number 5 cargo tank<br />
showed no appreciable <strong>read</strong>ing. As <strong>the</strong>re was no<br />
improvement after a few minutes all pumping was<br />
stopped and <strong>the</strong> matter was investigated.<br />
The pump was found to be full <strong>of</strong> air which was bled<br />
out through <strong>the</strong> air cock valve. As <strong>the</strong> pumps were<br />
restarted number 5 cargo oil tank overflowed on<br />
to <strong>the</strong> deck. Both pumps were stopped, all valves<br />
closed. Fortunately <strong>the</strong> oil spill was contained on <strong>the</strong><br />
deck <strong>of</strong> <strong>the</strong> bunker barge.<br />
Observations:<br />
The problem with <strong>the</strong> cargo pump had allowed<br />
oil pumped from number 2 cargo tank into <strong>the</strong><br />
common discharge line to flow back into number 5<br />
cargo oil tank. This flow would have continued even<br />
after <strong>the</strong> pumps were stopped as gravity would have<br />
caused <strong>the</strong> oil in <strong>the</strong> discharge line to siphon back<br />
into <strong>the</strong> bunker tanker below. Had <strong>the</strong> vessel been<br />
fitted with high-level alarms it is likely that this spill<br />
could have been avoided. Adhering to good tanker<br />
practice by starting <strong>the</strong> discharge from one tank at<br />
a time and positively confirming that oil was flowing<br />
out <strong>of</strong> <strong>the</strong> tank before starting <strong>the</strong> next one would<br />
have done much to avoid <strong>the</strong> problem.<br />
Root Cause:<br />
Ship design failure.<br />
Financial Cost:<br />
In this instance although no oil reached <strong>the</strong> water,<br />
<strong>the</strong> company received a bill from <strong>the</strong> Port Authority<br />
for more than US$600. In addition to this <strong>the</strong> owner<br />
faced additional costs in disposing <strong>of</strong> <strong>the</strong> oil on deck<br />
and cleaning <strong>the</strong> vessel.<br />
Issue Date: 01/01/02<br />
Case No. 22382<br />
74 75
Operations<br />
Hose Bursts Under Pressure<br />
The Incident:<br />
In recent months, <strong>the</strong> Club has been involved in a<br />
large number <strong>of</strong> pollution incidents which have been<br />
caused by transfer hoses bursting during bunkering<br />
operations. The following is a typical example.<br />
The Member’s vessel was employed in <strong>the</strong> process <strong>of</strong><br />
transferring 600mt <strong>of</strong> heavy fuel oil into a receiving<br />
ship. She was tied up starboard side alongside and <strong>the</strong><br />
transfer was being effected by using one cargo pump<br />
and a 30 metre long 6 inch diameter cargo hose.<br />
The Bunker Requisition Form was agreed between<br />
both parties indicating a pumping rate <strong>of</strong> 200 mt/hr<br />
with a maximum manifold pressure <strong>of</strong> 2kg/cm2 . The<br />
transfer began at 0950.<br />
At 1125 a bang was heard and oil was seen leaking<br />
out <strong>of</strong> a section <strong>of</strong> <strong>the</strong> transfer hose lying on <strong>the</strong> deck<br />
<strong>of</strong> <strong>the</strong> Member’s vessel. Pumping operations were<br />
stopped and both crews implemented measures to<br />
reduce <strong>the</strong> spilling <strong>of</strong> oil into <strong>the</strong> harbour. After a<br />
short while <strong>the</strong> harbour authorities’ launch arrived<br />
and undertook clean up operations to minimise <strong>the</strong><br />
effects <strong>of</strong> <strong>the</strong> oil spill.<br />
Observations:<br />
At <strong>the</strong> time <strong>of</strong> <strong>the</strong> incident, <strong>the</strong> receiving vessel had<br />
40 metric tonnes <strong>of</strong> <strong>the</strong> stem left to receive and <strong>the</strong><br />
cause <strong>of</strong> <strong>the</strong> hose bursting was considered to have<br />
been over pressurisation when <strong>the</strong> tank valves were<br />
possibly closed in as <strong>the</strong> receiving vessel’s tanks<br />
were being topped <strong>of</strong>f.<br />
However investigations carried out by <strong>the</strong> Club<br />
surveyor showed <strong>the</strong> condition <strong>of</strong> <strong>the</strong> cargo hoses<br />
to be poor. Several splits were noted in <strong>the</strong> outer<br />
covering. The point at which <strong>the</strong> hose burst was<br />
located within a section <strong>of</strong> hose that had been<br />
parcelled to give protection against chaffing so any<br />
deformations or damage to this section would not<br />
be <strong>read</strong>ily apparent. What <strong>the</strong> condition <strong>of</strong> <strong>the</strong> hose<br />
played in <strong>the</strong> incident is unknown.<br />
Notwithstanding any regulations, if hoses (or any<br />
equipment) exhibit defects <strong>the</strong>y should be tested<br />
immediately and measures taken to replace <strong>the</strong>m.<br />
Satisfactory test results only show <strong>the</strong> hose is in an<br />
acceptable condition at <strong>the</strong> time <strong>of</strong> testing. It does<br />
not provide a guarantee <strong>the</strong> hose’s condition will<br />
remain satisfactory when subjected to fur<strong>the</strong>r wear<br />
and tear. It should also be borne in mind that bunker<br />
vessels, by <strong>the</strong> very nature <strong>of</strong> <strong>the</strong>ir work, place<br />
a greater burden on <strong>the</strong>ir equipment than o<strong>the</strong>r<br />
tanker types and <strong>the</strong>refore <strong>the</strong>ir equipment should<br />
be examined on a more frequent basis.<br />
Root Cause:<br />
Inadequate maintenance programme.<br />
The Member had complied with <strong>the</strong> local authority<br />
requirements for <strong>the</strong> testing <strong>of</strong> <strong>the</strong> hose which<br />
required a pressure test to be carried out twice<br />
every five years with a maximum interval between<br />
tests <strong>of</strong> three years. The regulations do not make<br />
any reference to <strong>the</strong> general condition <strong>of</strong> <strong>the</strong> hose.<br />
Because <strong>of</strong> <strong>the</strong> poor condition, <strong>the</strong> Club only agreed<br />
to provide security when it was proven that <strong>the</strong><br />
local regulations had been complied with.<br />
Financial Cost:<br />
The Club put up security for US$40,000 to cover<br />
<strong>the</strong> port authority costs.<br />
Issue Date: 01/01/02 Case No. 39324<br />
76 77
Pollution<br />
Pollution<br />
Good Record Keeping Wins <strong>the</strong> Day<br />
New Ship, New Crew – Same Old Problems<br />
The Incident:<br />
This incident occurred during bunkering operations in<br />
sheltered waters. The bunker tanker was delivering<br />
gas oil to an ocean going vessel when <strong>the</strong> gaskets on<br />
<strong>the</strong> strainer box on board <strong>the</strong> deep sea vessel burst,<br />
with <strong>the</strong> result that gas oil spilt over <strong>the</strong> deck and into<br />
<strong>the</strong> sea. The deep sea vessel was fined by <strong>the</strong> Port<br />
Authority and sought indemnity for this and <strong>the</strong> cost<br />
<strong>of</strong> cleaning <strong>the</strong>ir vessel. The deep sea vessel alleged<br />
that <strong>the</strong> bunker barge had greatly exceeded <strong>the</strong><br />
agreed loading rate.<br />
Fortunately <strong>the</strong> personnel on board <strong>the</strong> bunker barge<br />
had kept proper records <strong>of</strong> <strong>the</strong> transfer operation<br />
and we were able to show quite conclusively that <strong>the</strong><br />
agreed loading rate had never been exceeded. It is<br />
likely that <strong>the</strong> increase in pressure which caused <strong>the</strong><br />
packing to burst was <strong>the</strong> result <strong>of</strong> valves being closed<br />
on <strong>the</strong> deep sea vessel.<br />
Observations:<br />
This case highlights <strong>the</strong> need to keep proper records<br />
during oil transfer operations. Had <strong>the</strong> barge’s crew<br />
not been diligent in recording events, taking regular<br />
tank soundings and noting pump speeds, we would<br />
have found it much more difficult to avoid liability.<br />
Root Cause:<br />
Inadequate maintenance programme.<br />
Financial Cost:<br />
Nil.<br />
Issue Date: 01/01/02<br />
Case No. 22494<br />
The Incident:<br />
This minor oil spill occurred during a bunkering<br />
operation in sheltered waters. The bunker barge was<br />
supplying fuel to <strong>the</strong> deep sea vessel from tanks 2 and<br />
4. As <strong>the</strong> bunkering operation neared completion<br />
tank 5, containing a different grade <strong>of</strong> oil, overflowed<br />
on to <strong>the</strong> deck. The <strong>of</strong>ficer in charge <strong>of</strong> <strong>the</strong> cargo<br />
operation promptly stopped <strong>the</strong> bunkering operation.<br />
The spill was largely contained within <strong>the</strong> vessel’s oil<br />
spill coaming where plugged scuppers prevented <strong>the</strong><br />
accumulated oil from flowing over <strong>the</strong> ship’s side.<br />
Never<strong>the</strong>less <strong>the</strong> vessel was fined by <strong>the</strong> harbour<br />
authorities.<br />
The cargo <strong>of</strong> 380 CST oil in number 5 tank was<br />
contaminated by approximately 50 tons <strong>of</strong> 180 CST<br />
oil bringing <strong>the</strong> average viscosity down to 300 CST.<br />
No claim was made by <strong>the</strong> charterers who were able<br />
to dispose <strong>of</strong> this oil with no loss <strong>of</strong> value. Surprisingly<br />
no claim for short delivery <strong>of</strong> bunkers was made by<br />
<strong>the</strong> deep sea vessel involved.<br />
Observations:<br />
The spill was caused by a crew member operating<br />
<strong>the</strong> wrong valves. This vessel had only joined <strong>the</strong><br />
fleet a week prior to <strong>the</strong> incident and <strong>the</strong> crew<br />
were unfamiliar with <strong>the</strong> vessel. The valves were not<br />
colour coded nor were <strong>the</strong>y clearly marked. The<br />
instructions given to <strong>the</strong> crewman were generic<br />
and did not specify precisely which valves should<br />
be operated. It is likely that this incident could<br />
have been avoided had <strong>the</strong> crew had more time to<br />
become familiar with <strong>the</strong> vessel, <strong>the</strong> valves been<br />
clearly marked and <strong>the</strong> crewman given precise<br />
instructions.<br />
Root Cause:<br />
Human error.<br />
Financial Cost:<br />
This Member was fortunate as <strong>the</strong> fine and costs<br />
incurred did not exceed US$6,000. It could have<br />
been much greater.<br />
Issue Date:<br />
Case No.<br />
78 79
Pollution<br />
High Loading Rate + Too Few Crew = Pollution<br />
The Incident:<br />
This incident involves an oil spill while loading a small<br />
bunker tanker. The bunker tanker had returned from<br />
supplying fuel to an ocean going vessel. It had oil<br />
remaining in numbers 2, 3 and 4 wing tanks. The plan<br />
was to load number 1 port and starboard first and<br />
<strong>the</strong>reafter top up 2, 3 and 4 wings, finishing in number<br />
4. An 8 inch hose was connected and although <strong>the</strong><br />
vessel was only due to lift 810 metric tons, <strong>the</strong> loading<br />
rate was agreed at 600 tons per hour. As number 2<br />
wings were being topped <strong>of</strong>f, <strong>the</strong> crew failed to shut<br />
<strong>the</strong> tank valves in time and oil overflowed onto <strong>the</strong><br />
deck and into <strong>the</strong> sea.<br />
Observations:<br />
Oil spills are most likely to occur when vessels are<br />
topping <strong>of</strong>f <strong>the</strong>ir tanks. Extreme caution should be<br />
exercised at this stage and adequate personnel need<br />
to be stationed on deck to ensure that <strong>the</strong>re are<br />
sufficient hands available to manipulate <strong>the</strong> valves as<br />
necessary. The loading rate should be reduced while<br />
tanks are being topped <strong>of</strong>f. This procedure should<br />
be agreed with terminal personnel in advance. This<br />
incident occurred while cargo was being loaded at<br />
<strong>the</strong> full 600 tons per hour and only one man was<br />
available to monitor <strong>the</strong> tank level and manipulate<br />
<strong>the</strong> valves. The spill could have been avoided if<br />
<strong>the</strong> loading rate had been reduced and additional<br />
personnel utilised.<br />
Root Cause:<br />
Insufficient operational procedures.<br />
Financial Cost:<br />
The cost <strong>of</strong> clean up operations and <strong>the</strong> fine<br />
imposed by <strong>the</strong> Port Authority brought <strong>the</strong> total<br />
value <strong>of</strong> this claim to almost US$9,000.<br />
Issue Date: 01/01/02<br />
Case No. 19809<br />
80 81
Tankers:<br />
Gas<br />
Miscellaneous<br />
Capsize at Sea<br />
The Incident:<br />
This case concerns <strong>the</strong> capsize and total loss <strong>of</strong><br />
a 690 ton gas tanker. The vessel was steaming<br />
between islands in <strong>the</strong> Philippines fully laden<br />
with LPG when she received a message from her<br />
charterers announcing a change <strong>of</strong> destination. On<br />
receipt <strong>of</strong> <strong>the</strong>se new orders to return to a port that<br />
<strong>the</strong>y had al<strong>read</strong>y passed, <strong>the</strong> helm was put hard to<br />
starboard while <strong>the</strong> vessel was proceeding at full<br />
speed. The vessel listed heavily into <strong>the</strong> turn and<br />
<strong>the</strong> list progressively increased until <strong>the</strong> result that<br />
<strong>the</strong> vessel capsized. Because <strong>of</strong> <strong>the</strong> buoyant nature<br />
<strong>of</strong> her cargo <strong>the</strong> tanker did not sink completely but<br />
came to rest floating vertically in <strong>the</strong> water with her<br />
fo’c’sle structure above <strong>the</strong> water level. Hull and<br />
machinery underwriters immediately declared <strong>the</strong><br />
vessel to be a total loss, leaving <strong>the</strong> owners with <strong>the</strong><br />
problem <strong>of</strong> disposing <strong>of</strong> <strong>the</strong> wreck. After a lengthy<br />
salvage operation <strong>the</strong> vessel was refloated with<br />
her cargo intact. Considerable difficulty was found<br />
in disposing <strong>of</strong> <strong>the</strong> vessel and her cargo because<br />
none <strong>of</strong> <strong>the</strong> major oil companies were prepared to<br />
let a damaged LPG tanker berth in <strong>the</strong>ir terminal.<br />
The vessel and her cargo were ultimately sold to a<br />
salvage buyer for a fraction <strong>of</strong> <strong>the</strong>ir true value.<br />
Observations:<br />
The most likely cause <strong>of</strong> <strong>the</strong> casualty is a reduction<br />
in stability caused by free surface effect <strong>of</strong> liquids on<br />
board <strong>the</strong> vessel. Subsequent investigation revealed<br />
that <strong>the</strong> vessel was having problems with leakage. In<br />
this case <strong>the</strong>re was no formal contract between <strong>the</strong><br />
vessel’s owners and <strong>the</strong> repair yard. The question<br />
<strong>of</strong> responsibility for ensuring that <strong>the</strong> vessel was<br />
fit for hot work to be carried out was not clear.<br />
We would recommend that owners ensure this<br />
subject is addressed in every repair contract and<br />
that where possible <strong>the</strong> shipyard be given this<br />
responsibility.<br />
Root Cause:<br />
Poor maintenance programme.<br />
Financial Cost:<br />
The cost <strong>of</strong> refloating and disposing <strong>of</strong> <strong>the</strong> ship and<br />
cargo exceeded US$820,000.<br />
Issue Date: 01/01/02<br />
Case No. 20524<br />
82 83
Section 3<br />
Fishing Vessels<br />
85
Fishing Vessels<br />
Personal Injury/Illness<br />
Although Out <strong>of</strong> Sight it should be Kept in Mind<br />
The Incident:<br />
This incident took place on a beam trawler and a<br />
resulted in a non-fatal injury to a crew member.<br />
During a late evening in fine wea<strong>the</strong>r conditions <strong>the</strong><br />
fishing gear was being hauled. Four crew members<br />
were positioned on <strong>the</strong> top deck waiting to attend<br />
to <strong>the</strong> beams as <strong>the</strong>y came on board.<br />
As <strong>the</strong>y cleared <strong>the</strong> water, with <strong>the</strong> derrick standing<br />
vertically, <strong>the</strong> starboard topping wire parted. It came<br />
down with some force and struck a deckhand. It was<br />
later found he had sustained a fracture to an ankle<br />
and <strong>the</strong>re is some doubt as to his ability to return to<br />
a life in <strong>the</strong> fishing industry.<br />
Observations:<br />
Unfortunately <strong>the</strong> head block was lost overboard<br />
during <strong>the</strong> incident and it is a matter <strong>of</strong> conjecture<br />
whe<strong>the</strong>r <strong>the</strong> block failed causing <strong>the</strong> wire to part or<br />
whe<strong>the</strong>r <strong>the</strong> wire parted causing <strong>the</strong> block to fail.<br />
The wire was reportedly only seven months old.<br />
The rigging arrangement for <strong>the</strong> derrick was such<br />
that <strong>the</strong> topping wire only moved between 150mm<br />
to 200mm when raising or lowering <strong>the</strong> booms,<br />
thus <strong>the</strong> length which rounded <strong>the</strong> block had been<br />
hidden from view since it was reeved.<br />
Although <strong>the</strong> skipper had in place a thorough greasing<br />
routine for <strong>the</strong> wire and blocks, <strong>the</strong> only way to<br />
examine this small section <strong>of</strong> wire was to land <strong>the</strong><br />
derrick on to a quay, which had never been carried out.<br />
Both ends <strong>of</strong> <strong>the</strong> wire were noted to be frayed<br />
which indicates that it was likely <strong>the</strong> wire had parted,<br />
destroying <strong>the</strong> block.<br />
Root Cause:<br />
Inadequate maintenance programmes.<br />
Financial Cost:<br />
The cost <strong>of</strong> this claim is US$80,000.<br />
Issue Date: 05/07/06<br />
Case No. 38878<br />
It is not uncommon for static sections <strong>of</strong> wire to<br />
corrode significantly in a short period <strong>of</strong> time and<br />
Members and Skippers should ensure that such<br />
sections <strong>of</strong> wire are frequently examined and greased.<br />
86 87
Personal Injury/Illness<br />
The Importance <strong>of</strong> Good Risk Assessment Highlighted<br />
The Incident:<br />
The accident occurred when a<br />
crew member was attending <strong>the</strong><br />
gilsen derrick guys as a catch was<br />
being brought on board. Three<br />
turns had been taken round <strong>the</strong><br />
port warping drum <strong>of</strong> <strong>the</strong> trawl<br />
winch. The drum was rotating at a<br />
steady speed as <strong>the</strong> controls had<br />
been locked in position by <strong>the</strong><br />
use <strong>of</strong> a piece <strong>of</strong> wood wedged<br />
between <strong>the</strong> control lever and<br />
frame. The crew member was<br />
tailing <strong>the</strong> rope behind <strong>the</strong> drum,<br />
surging or heaving as required<br />
when <strong>the</strong> fingers <strong>of</strong> his left hand<br />
became caught between <strong>the</strong> rope<br />
turns and <strong>the</strong> drum. There were<br />
no witnesses to <strong>the</strong> accident but<br />
it seems likely that a riding turn<br />
developed on <strong>the</strong> drum and<br />
instead <strong>of</strong> letting <strong>the</strong> rope go and<br />
stopping <strong>the</strong> winch by pulling on a<br />
small rope attached to <strong>the</strong> piece<br />
<strong>of</strong> wood, <strong>the</strong> crewman tried to<br />
clear <strong>the</strong> guy while <strong>the</strong> machinery<br />
was still rotating. Despite medical<br />
intervention he lost <strong>the</strong> tips to<br />
three fingers.<br />
Observations:<br />
There were two contributing factors to this incident.<br />
Firstly, <strong>the</strong> crew member was very inexperienced<br />
in working on a fishing vessel although <strong>the</strong> task he<br />
was involved in was not an unusual one in terms <strong>of</strong><br />
seamanship. However it appears he tried to clear <strong>the</strong><br />
riding turn whilst <strong>the</strong> winch was rotating. Secondly,<br />
despite two o<strong>the</strong>r crew members being present on<br />
deck, no one was designated to operate <strong>the</strong> winch<br />
which was left in <strong>the</strong> hauling mode by means <strong>of</strong><br />
a makeshift modification. The crew member had<br />
allegedly been told to stop <strong>the</strong> winch in <strong>the</strong> event<br />
<strong>of</strong> any problems, but failed to do so. Had a winch<br />
operator been present, stopping <strong>the</strong> winch would<br />
have been easily achieved and <strong>the</strong> accident avoided.<br />
Indeed he should have been better supervised in<br />
view <strong>of</strong> his relevant inexperience.<br />
Root Cause:<br />
Inadequate operational practices.<br />
Financial Cost:<br />
The claim was settled for US$117,000.<br />
Issue Date:<br />
Case No.<br />
88 89
Personal Injury/Illness<br />
No Excuse for Reduced Maintenance Regimes<br />
The Incident:<br />
A Skipper was killed and two women injured when <strong>the</strong> starboard<br />
derrick, which had been topped up to its fully raised position, suddenly<br />
fell down on <strong>the</strong>m as <strong>the</strong>y stood on <strong>the</strong> quayside next to <strong>the</strong> vessel. It<br />
transpired that <strong>the</strong> eye <strong>of</strong> <strong>the</strong> starboard topping lift block had failed and<br />
subsequent investigation attributed its failure to <strong>the</strong> sudden propagation<br />
<strong>of</strong> a brittle fracture from a pre-existing manufacturing defect.<br />
The claims eventually came to trial and <strong>the</strong> claimants’ primary case<br />
was that <strong>the</strong> Members had failed to put in place an adequate system <strong>of</strong><br />
inspection and maintenance <strong>of</strong> <strong>the</strong> fishing gear. The Members asserted<br />
that <strong>the</strong>ir system <strong>of</strong> inspection and maintenance was in accordance<br />
with all applicable regulations and matched prevailing standards within<br />
<strong>the</strong> industry. They contended that, in any event, any shortcomings in<br />
maintenance were not causative <strong>of</strong> <strong>the</strong> loss since <strong>the</strong> block failed as a<br />
result <strong>of</strong> a latent manufacturing defect which could not have been, and<br />
was not, detected by <strong>the</strong> exercise <strong>of</strong> reasonable diligence.<br />
Observations:<br />
The judge found that <strong>the</strong><br />
Members’ practice <strong>of</strong> leaving<br />
all aspects <strong>of</strong> maintenance and<br />
safety to <strong>the</strong> crew was indeed in<br />
accordance with industry practice<br />
but that it was “simply naive to<br />
assert that good practice cannot<br />
call for more than compliance with<br />
<strong>the</strong> relative statutory regime”. He<br />
said that <strong>the</strong>re should have been<br />
a system <strong>of</strong> planned preventative<br />
inspection and maintenance<br />
<strong>of</strong> all lifting gear blocks every<br />
six months by a person with<br />
sufficient practical experience and<br />
<strong>the</strong>oretical knowledge. He saw<br />
no reason to distinguish between<br />
<strong>the</strong> regime <strong>of</strong> inspection required<br />
<strong>of</strong> cargo ships’ derricks and lifting<br />
gear on a fishing vessel. As to<br />
causation, <strong>the</strong> metallurgist experts<br />
for both parties were agreed that<br />
<strong>the</strong> developing defect in <strong>the</strong> block<br />
would not have been detected<br />
during a routine inspection<br />
and overhaul <strong>of</strong> <strong>the</strong> vessel’s<br />
equipment. However, <strong>the</strong> judge<br />
found that <strong>the</strong> crew were wholly<br />
untrained to recognise degrees <strong>of</strong><br />
wear or corrosion in <strong>the</strong> vessel’s<br />
equipment, that <strong>the</strong>re were o<strong>the</strong>r<br />
defects in <strong>the</strong> block which were<br />
patent and that a proper system<br />
<strong>of</strong> maintenance would have<br />
required <strong>the</strong> block to have been<br />
tested with <strong>the</strong> specific intention<br />
<strong>of</strong> identifying cracks.<br />
Members’ attention is drawn to our<br />
Lookout article 06 <strong>of</strong> 2004 where<br />
a maintenance regime for lifting<br />
tackle on fishing vessels based on<br />
MCA requirements is detailed.<br />
Root Cause:<br />
Inadequate shore maintenance<br />
procedure.<br />
Financial Cost:<br />
The Members paid substantial<br />
compensation to <strong>the</strong> Skipper’s<br />
widow and <strong>the</strong> two injured<br />
women. With <strong>the</strong> associated<br />
costs, <strong>the</strong> total value <strong>of</strong> this claim<br />
was in excess <strong>of</strong> US$2,155,000.<br />
Issue Date: 27/10/05<br />
Case No. 32365<br />
90 91
Personal Injury/Illness<br />
Death from Hydrogen Sulphide Poisoning<br />
The Incident:<br />
The vessel involved in this case<br />
was a 97 foot fishing vessel<br />
which had left her home waters<br />
in Alaska to fish for albacore<br />
tuna in <strong>the</strong> South Pacific. The<br />
vessel experienced problems<br />
with her refrigeration system<br />
which culminated in a full catch<br />
<strong>of</strong> approximately 15 tons <strong>of</strong> tuna<br />
being rejected as being unfit for<br />
human consumption.<br />
The skipper decided to cut his<br />
losses and return to Alaska,<br />
hoping to sell <strong>the</strong> catch as bait. It<br />
appears however that problems<br />
with <strong>the</strong> refrigeration system<br />
worsened and six days into <strong>the</strong><br />
voyage <strong>the</strong> refrigeration system<br />
was shut down altoge<strong>the</strong>r. The<br />
three man crew started to dump<br />
<strong>the</strong> fish over <strong>the</strong> side. Nine tons<br />
were disposed <strong>of</strong> before <strong>the</strong> smell<br />
<strong>of</strong> decomposing fish became<br />
overwhelming. The Captain<br />
decided to partially flood <strong>the</strong><br />
fish hold in <strong>the</strong> hope that <strong>the</strong> fish<br />
would rapidly break down into<br />
a soup which could be pumped<br />
overboard. After leaving <strong>the</strong> fish<br />
to decompose for a few days <strong>the</strong>y<br />
commenced pumping <strong>the</strong><br />
mixture but after a short period<br />
<strong>the</strong> strum box clogged with fish<br />
remains. The skipper descended<br />
<strong>the</strong> ladder into <strong>the</strong> fish hold to<br />
try to clear <strong>the</strong> pump. Within<br />
seconds he was overcome by<br />
hydrogen sulphide gas given <strong>of</strong>f<br />
by <strong>the</strong> rotting fish. The engineer<br />
attempted to rescue him and also<br />
succumbed. The one remaining<br />
crew member was unable to<br />
operate <strong>the</strong> radio to summon<br />
assistance and steamed in <strong>the</strong><br />
general direction <strong>of</strong> Honolulu until<br />
<strong>the</strong> boat’s generator ran out <strong>of</strong><br />
fuel and <strong>the</strong> electrical supplies to<br />
<strong>the</strong> steering gear failed. At that<br />
point he abandoned ship and set<br />
<strong>of</strong>f <strong>the</strong> EPIRB. He was rescued by<br />
<strong>the</strong> US Coastguard.<br />
Observations:<br />
This unusual incident highlights <strong>the</strong> dangers <strong>of</strong><br />
entering enclosed spaces. The atmosphere <strong>of</strong><br />
any enclosed or confined space which is not<br />
continuously and adequately ventilated may be<br />
deficient in oxygen or contain flammable/toxic<br />
fumes, gases or vapours. Crews should be made<br />
aware <strong>of</strong> <strong>the</strong> dangers and instructed not to enter<br />
enclosed spaces if <strong>the</strong>re is any reason to suspect that<br />
<strong>the</strong> atmosphere may be hazardous. On no account<br />
should rescue attempts be made without wearing<br />
breathing apparatus, a rescue harness and lifeline.<br />
In this case <strong>the</strong> crew were aware that <strong>the</strong> fish were<br />
rotting but were ignorant <strong>of</strong> <strong>the</strong> effects <strong>of</strong> <strong>the</strong> gas<br />
being given <strong>of</strong>f. The vessel carried no breathing<br />
apparatus, gas testing equipment or oxygen<br />
analysing equipment. This accident could have been<br />
avoided if <strong>the</strong> crew had been aware <strong>of</strong> <strong>the</strong> risks <strong>of</strong><br />
enclosed spaces and not attempted to deal with <strong>the</strong><br />
problem without proper equipment.<br />
Root Cause:<br />
Inadequate enclosed space entry procedures.<br />
Financial Cost:<br />
The cost <strong>of</strong> this claim exceeded US$650,000.<br />
Issue Date:01/01/02<br />
Case No. 14132<br />
The survivor claimed damages for<br />
post traumatic stress disorder.<br />
Claims were made by <strong>the</strong> families<br />
<strong>of</strong> <strong>the</strong> two dead crew.<br />
92 93
Personal Injury/Illness<br />
Makeshift Platform Results in a Severe Injury<br />
The Incident:<br />
The stern trawler involved in this<br />
incident was lying in a port in<br />
Alaska undergoing repair work.<br />
The vessel’s trawl deck area<br />
was equipped with two cranes,<br />
one located at <strong>the</strong> forward<br />
starboard corner and <strong>the</strong><br />
o<strong>the</strong>r portside aft. Repair work<br />
was being carried out on <strong>the</strong><br />
starboard forward crane by<br />
independent contractors.<br />
The work involved cutting out<br />
and replacing a portion <strong>of</strong> a<br />
starboard forward crane. The<br />
after port crane was used to<br />
assist in <strong>the</strong> repair work.<br />
The contractors could not reach <strong>the</strong> damaged portion <strong>of</strong> <strong>the</strong> crane<br />
from deck level. The contractors brought a large piece <strong>of</strong> plywood<br />
on board, placed it on top <strong>of</strong> <strong>the</strong> starboard trawl winch, which was<br />
conveniently situated just aft <strong>of</strong> and adjacent to <strong>the</strong> crane. At some<br />
point during <strong>the</strong> repair work it became evident to <strong>the</strong> contractors<br />
that as <strong>the</strong>y moved about on <strong>the</strong> plywood sheet it pressed through<br />
<strong>the</strong> control ears activating <strong>the</strong> winch. The contractors approached <strong>the</strong><br />
ship’s crew to ask whe<strong>the</strong>r it would be possible to turn <strong>the</strong> hydraulic<br />
power supply to <strong>the</strong> winch <strong>of</strong>f and <strong>the</strong> ship’s crew advised that it was<br />
possible but as <strong>the</strong> deck cranes and trawl winches were operated from<br />
<strong>the</strong> same hydraulic supply, <strong>the</strong> contractors would lose <strong>the</strong> use <strong>of</strong> <strong>the</strong><br />
aft port crane. The contractors however needed power to <strong>the</strong> crane<br />
and asked that <strong>the</strong> hydraulic power be left on. Not long afterwards <strong>the</strong><br />
trawl winch was accidentally activated, trapping <strong>the</strong> foot <strong>of</strong> one <strong>of</strong> <strong>the</strong><br />
contractors’ workmen. The injuries were so severe that <strong>the</strong> workman<br />
lost <strong>the</strong> big and first toe on his left foot, which disabled him to <strong>the</strong><br />
extent that he was unable to continue with his previous occupation.<br />
Observations:<br />
This incident highlights <strong>the</strong> dangers <strong>of</strong> makeshift<br />
working platforms. This incident could have been<br />
avoided if <strong>the</strong> had erected a proper scaffolding<br />
around <strong>the</strong> crane to provide a safe platform for<br />
his men to work from. In this case despite <strong>the</strong><br />
contractor and his employees being fully aware that<br />
<strong>the</strong> movement <strong>of</strong> <strong>the</strong> plywood sheet was causing<br />
<strong>the</strong> winch to operate unexpectedly, <strong>the</strong>y took<br />
no steps to replace <strong>the</strong> plywood with a proper<br />
structure or take any steps to guard <strong>the</strong> controls.<br />
Fur<strong>the</strong>rmore <strong>the</strong> contractor’s men were still using<br />
<strong>the</strong> winch as a stepping stone to reach parts <strong>of</strong> <strong>the</strong><br />
crane knowing that it was liable to operate without<br />
warning.<br />
Root Cause:<br />
Failure <strong>of</strong> 3rd party working practices.<br />
Issue Date: 01/01/02<br />
Case No. 21949<br />
94 95
Personal Injury/Illness<br />
Importance <strong>of</strong> a Safe Means <strong>of</strong> Access<br />
The Incident:<br />
This incident occurred in harbour at <strong>the</strong> end <strong>of</strong><br />
<strong>the</strong> fishing season. The vessel was being laid up for<br />
some months and <strong>the</strong> crew had been removing<br />
<strong>the</strong>ir belongings from <strong>the</strong> vessel dock. No proper<br />
gangway had been rigged and <strong>the</strong> only access to <strong>the</strong><br />
vessel was by way <strong>of</strong> a jacob’s ladder tied to <strong>the</strong> top<br />
railing on <strong>the</strong> starboard side <strong>of</strong> <strong>the</strong> pilot house deck.<br />
As a crew member was clambering over <strong>the</strong> top <strong>of</strong><br />
<strong>the</strong> railing he lost his balance and fell approximately<br />
12 feet to <strong>the</strong> dock injuring himself.<br />
The crew member suffered a severely broken<br />
wrist which required <strong>the</strong> insertion <strong>of</strong> metal pins.<br />
He was also found to have herniated a disc in<br />
his upper spine which gave rise to neck pain and<br />
dizziness. His doctors advised him that he should<br />
not return to work at sea.<br />
Observations:<br />
This is one <strong>of</strong> <strong>the</strong> many injuries that occur every year<br />
as a result <strong>of</strong> <strong>the</strong> use <strong>of</strong> unsafe means <strong>of</strong> access to<br />
and from vessels. Small vessels <strong>of</strong>ten have greater<br />
problems ensuring safe means <strong>of</strong> access than <strong>the</strong>ir<br />
larger sisters. In this particular case it would have<br />
been difficult if not impossible to rig a conventional<br />
gangway. The accident could however have been<br />
avoided if <strong>the</strong> jacob’s ladder had been rigged<br />
adjacent to an opening in <strong>the</strong> ship’s rail which would<br />
have avoided <strong>the</strong> crew member having to clamber<br />
precariously over <strong>the</strong> ship’s rail. Alternatively a rigid<br />
vertical ladder extending above <strong>the</strong> level <strong>of</strong> <strong>the</strong><br />
vessel’s rails could have been used.<br />
Root Cause:<br />
Inadequate means <strong>of</strong> access.<br />
Financial Cost:<br />
The total cost <strong>of</strong> this claim to <strong>the</strong><br />
Shipowner was $214,114.<br />
Issue Date: 01/01/02<br />
Case No. 21160<br />
96 97
Personal Injury/Illness<br />
It Pays to Plan Ahead<br />
Root Cause:<br />
It Pays to Plan Ahead.<br />
Financial Cost:<br />
The cost <strong>of</strong> this claim was in excess <strong>of</strong> US$117,000.<br />
Issue Date: 10/06/05<br />
Case No. 26039<br />
The Incident:<br />
The Member’s vessel was tied up alongside and a diving company was employed to<br />
undertake underwater cleaning <strong>of</strong> <strong>the</strong> hull. The diver reported to <strong>the</strong> Master and <strong>the</strong>n<br />
proceeded ashore where he changed into his diving gear and entered <strong>the</strong> water.<br />
The Master remained on deck to check work being carried out on a hydraulic winch.<br />
Soon after, <strong>the</strong> Chief Engineer approached <strong>the</strong> Master and requested permission to start<br />
<strong>the</strong> main engine so that electrical power could be provided to test <strong>the</strong> winch. The Master<br />
refused permission on account <strong>of</strong> <strong>the</strong> diver being in <strong>the</strong> water. Because <strong>of</strong> language<br />
difficulties <strong>the</strong> Chief Engineer had not understood what <strong>the</strong> Master had said<br />
and proceeded to <strong>the</strong> engine room to start <strong>the</strong> engine. The diver was working in <strong>the</strong><br />
vicinity <strong>of</strong> <strong>the</strong> propeller and when <strong>the</strong> engine started he was instantly killed.<br />
Observations:<br />
The main cause <strong>of</strong> this fatality was a failure <strong>of</strong> <strong>the</strong><br />
Master to ensure that all crew members were<br />
aware <strong>of</strong> <strong>the</strong> attendance <strong>of</strong> a diver whilst <strong>the</strong> vessel<br />
was alongside. By ensuring <strong>the</strong> facts were known<br />
beforehand, <strong>the</strong> possibility <strong>of</strong> <strong>the</strong> engines being used<br />
would not have arisen. Precautionary measures could<br />
have been taken including notices being placed on <strong>the</strong><br />
starting handles and telegraphs. This case also highlights<br />
<strong>the</strong> need to ensure facts are clearly understood<br />
when language difficulties may arise due to different<br />
nationalities being employed on board. It is important<br />
that all senior crew members have at least a good<br />
working knowledge <strong>of</strong> one common language and can<br />
communicate effectively with <strong>the</strong>ir department staff.<br />
98 99
Personal Injury/Illness<br />
Heat <strong>of</strong> <strong>the</strong> Moment<br />
The Incident:<br />
The skipper <strong>of</strong> a fishing vessel was leaning into an ice<br />
box when <strong>the</strong> lid, weighing half a ton, fell on to him.<br />
He suffered serious chest injuries and has a 10%<br />
body impairment as a result. The normal procedure<br />
for opening <strong>the</strong> lid was to raise it by means <strong>of</strong> a rope<br />
and tackle and <strong>the</strong>n insert a safety prop to hold it<br />
up.<br />
Observations:<br />
Unfortunately, on this occasion <strong>the</strong> skipper relied<br />
on <strong>the</strong> rope to hold <strong>the</strong> lid open and did not use<br />
<strong>the</strong> prop. The lead <strong>of</strong> <strong>the</strong> syn<strong>the</strong>tic rope was such<br />
that it came into contact with <strong>the</strong> funnel and <strong>the</strong><br />
heat had a degrading effect on it which caused <strong>the</strong><br />
rope to eventually part. Had <strong>the</strong> safety prop been<br />
used this accident would have been prevented. In<br />
all likelihood <strong>the</strong> rope would have parted when <strong>the</strong><br />
lid was being ei<strong>the</strong>r opened or closed and <strong>the</strong> crew<br />
standing clear.<br />
This incident highlights<br />
several facts:<br />
• Never rely on a wire or rope<br />
to hold a hatch lid open. A<br />
safety prop or securing pin<br />
should always be used to<br />
secure it in <strong>the</strong> open position.<br />
Such a restraint must enable<br />
clear access to <strong>the</strong> opening.<br />
• Wherever <strong>the</strong>re is a possibility<br />
<strong>of</strong> a syn<strong>the</strong>tic rope coming into<br />
contact with an indirect heat<br />
source, it should be replaced,<br />
preferably by a wire rope or at<br />
least by a natural fibre one.<br />
• Lifting arrangements should<br />
be subjected to a thorough<br />
visual examination at regular<br />
intervals. In this particular<br />
incident, it was reported that<br />
<strong>the</strong> damaged section <strong>of</strong> rope<br />
was not obvious to a casual<br />
observer.<br />
Root Cause:<br />
Human error.<br />
Issue Date: 03/02/06<br />
Case No. 37148<br />
100 101
Personal Injury/Illness<br />
When Applying First Aid – Ensure you Know What you are Doing<br />
The Incident:<br />
This claim involved a Vietnamese<br />
fisherman who, due to <strong>the</strong> medical<br />
treatment he received on board,<br />
had his lower leg amputated.<br />
Whilst fishing, a trawl wire<br />
became entangled around <strong>the</strong><br />
propeller. During efforts to free<br />
<strong>the</strong> wire, <strong>the</strong> crewman became<br />
trapped between <strong>the</strong> wire and<br />
bulwark. As a result he suffered a<br />
fracture to his right tibia, injuries<br />
to his pelvis and serious bruising<br />
and abrasions.<br />
Shortly after <strong>the</strong> accident, <strong>the</strong><br />
victim was transferred to ano<strong>the</strong>r<br />
larger fishing vessel which was<br />
proceeding to <strong>the</strong> nearest port.<br />
Once this vessel was within range,<br />
<strong>the</strong> ship’s helicopter was used<br />
to transfer him to <strong>the</strong> nearest<br />
island with medical facilities. The<br />
medical staff at <strong>the</strong> hospital did<br />
what <strong>the</strong>y could for <strong>the</strong> fisherman<br />
but decided he needed more<br />
specialist care and arrangements<br />
were made to airlift him to <strong>the</strong><br />
main land. Upon examination <strong>the</strong><br />
attending surgeon was left with<br />
no alternative but to amputate<br />
<strong>the</strong> right leg from <strong>the</strong> knee.<br />
Observations:<br />
As a result <strong>of</strong> <strong>the</strong> accident <strong>the</strong><br />
fisherman was bleeding heavily.<br />
The fracture to <strong>the</strong> tibia was open<br />
and a tourniquet was applied to<br />
stem <strong>the</strong> bleeding. This remained<br />
in place until he reached <strong>the</strong> first<br />
hospital 14 hours later.<br />
A tourniquet can be used to<br />
restrict blood flow to limbs, but<br />
<strong>the</strong> use <strong>of</strong> such a device has to<br />
be closely monitored because<br />
by restricting <strong>the</strong> blood flow<br />
<strong>the</strong> affected part <strong>of</strong> <strong>the</strong> body<br />
undergoes metabolic changes<br />
and unless blood flow is restored<br />
it slowly dies. In <strong>the</strong> case <strong>of</strong> <strong>the</strong><br />
fisherman, <strong>the</strong> lower leg muscles<br />
had died by <strong>the</strong> time he received<br />
pr<strong>of</strong>essional medical help and <strong>the</strong><br />
surgeon was left with no alternative<br />
but to remove <strong>the</strong> lower leg.<br />
A tourniquet is no longer<br />
recommended as a means <strong>of</strong><br />
restricting blood flow from a wound.<br />
The preferred option is to apply<br />
pressure to <strong>the</strong> wound by using a<br />
heavy pad held in place by bandages<br />
or even ones hand (preferably whilst<br />
wearing disposable gloves). The<br />
blood will eventually clot and <strong>the</strong><br />
blood flow stemmed.<br />
As a matter <strong>of</strong> last resort and if it<br />
is considered absolutely necessary<br />
to use a tourniquet, <strong>the</strong>n it must<br />
be released every ten or fifteen<br />
minutes for a short time in order<br />
to supply <strong>the</strong> tissue with blood.<br />
However <strong>the</strong> wound must be<br />
covered by a heavy pad and<br />
bandage to stem any blood flow.<br />
In this case <strong>the</strong> injuries sustained,<br />
although serious, were treatable<br />
and a good if not full recovery<br />
would have been made if a<br />
tourniquet had not been used.<br />
The Administration overseeing<br />
a vessel will have requirements<br />
for <strong>the</strong> medical qualifications<br />
required to be held by a vessel’s<br />
crew, and this case highlights <strong>the</strong><br />
importance <strong>of</strong> ensuring regular<br />
training is undertaken.<br />
Root Cause:<br />
Inadequate crew training.<br />
Financial Cost:<br />
The cost <strong>of</strong> this claim was<br />
over US$77,000.<br />
Issue Date: 23/04/04<br />
Case No. 42587<br />
102 103
Personal Injury/Illness<br />
A Real Eye Opener<br />
The Incident:<br />
This claim involved a purse seine fishing vessel engaged in fishing for tuna.<br />
The Chief Engineer was working in <strong>the</strong> vessel’s workshop when a foreign body entered<br />
his eye. The eye proved painful and <strong>the</strong> Master decided to land <strong>the</strong> injured engineer<br />
ashore for medical treatment. The nearest port was three days steaming away.<br />
Doctors removed <strong>the</strong> foreign body and <strong>the</strong> vessel returned to <strong>the</strong> fishing grounds.<br />
Observations:<br />
The medical examination revealed <strong>the</strong> foreign<br />
body (a piece <strong>of</strong> rusted metal) was “lodged<br />
superficially” on <strong>the</strong> eye and was easily removed<br />
by <strong>the</strong> attending doctor.<br />
Two points arise from this incident. Firstly, if <strong>the</strong><br />
Chief Engineer had been wearing safety goggles,<br />
<strong>the</strong> chances <strong>of</strong> <strong>the</strong> metal entering <strong>the</strong> eye would<br />
have been prevented and <strong>the</strong> incident would not<br />
have occurred. Secondly it is a little surprising that<br />
no apparent attempt was made to treat <strong>the</strong> injured<br />
party on board. The foreign body was superficially<br />
lodged and <strong>the</strong> vessel carried a medical outfit<br />
compliance with flag state requirements.<br />
Financial Cost:<br />
The cost to <strong>the</strong> Member in terms <strong>of</strong> <strong>the</strong> deviation<br />
was US$15,500 comprising fuel, port and hospital<br />
costs. The cost to <strong>the</strong> Member in lost fishing time<br />
during <strong>the</strong> 7 day deviation far exceeds this amount.<br />
Issue Date: 13/06/05<br />
Case No. 43868<br />
Root Cause:<br />
Poor Safety Practices.<br />
104 105
Personal Injury/Illness<br />
Carbon Monoxide Poisoning on Fishing Vessels<br />
The Incident:<br />
An experienced crewman <strong>of</strong> a 16 metre potter,<br />
who was both working and living on board <strong>the</strong><br />
vessel, died as he slept due to carbon monoxide<br />
poisoning. This was caused by <strong>the</strong> exhaust fumes<br />
<strong>of</strong> a petrol-driven generator running inside <strong>the</strong> fish<br />
hold. The generator had been brought on board by<br />
<strong>the</strong> crewman himself to power an electric heater,<br />
TV and radio.<br />
Observations:<br />
The bulkhead between <strong>the</strong> fish hold and <strong>the</strong><br />
crewman’s sleeping cabin was nei<strong>the</strong>r watertight<br />
nor gastight.<br />
Putting a petrol generator inside <strong>the</strong> fish hold<br />
introduced a number <strong>of</strong> hazards to <strong>the</strong> vessel:<br />
Carbon Monoxide:<br />
• Has no smell or taste<br />
• Symptoms <strong>of</strong> poisoning are similar to <strong>the</strong> flu<br />
• People may not be aware <strong>the</strong>y are being poisoned<br />
Fire/Explosion:<br />
• Petrol gives <strong>of</strong>f highly flammable fumes<br />
• A petrol engine below decks can potentially cause<br />
explosive fumes<br />
• O<strong>the</strong>r neighbouring boats could also be<br />
destroyed<br />
Electrical Hazard:<br />
• Household appliances are not designed for use in<br />
conditions <strong>of</strong>ten found on board fishing vessels<br />
• Correct wiring essential<br />
When living on board a vessel it is crucial<br />
to conduct a risk assessment so that:<br />
1. Sufficient power is provided for<br />
accommodation and lighting<br />
2. There is adequate ventilation (more needed<br />
for burners and stoves)<br />
3. There are adequate alarms to warn<br />
sleeping crewmen <strong>of</strong> problems<br />
4. Crew can escape from accommodation<br />
in an emergency<br />
5. It is safe for a lone crewman to board or<br />
leave <strong>the</strong> vessel at night<br />
Source - Maritime and Coastguard Agency<br />
Email: fishing@mcga.gov.uk<br />
Issue Date: 08/06/06<br />
Case No. 12346<br />
106 107
Personal Injury/Illness<br />
Careless Action Severely Injures Colleagues<br />
The Incident:<br />
Whilst trawling <strong>the</strong> net became entangled on its<br />
reel. A crew member climbed onto <strong>the</strong> net reel to<br />
clear <strong>the</strong> tangled section. Whilst clearing <strong>the</strong> net, <strong>the</strong><br />
deck boss, who was operating <strong>the</strong> winch, moved <strong>the</strong><br />
net reel without warning and without checking that<br />
<strong>the</strong> crewman was clear. As a result <strong>the</strong> crewman fell<br />
from <strong>the</strong> winch and fractured his leg and severely<br />
damaged his kneecap.<br />
Observations:<br />
The incident was caused by <strong>the</strong><br />
failure <strong>of</strong> <strong>the</strong> winch operator to<br />
ensure all crew were clear before<br />
he operated <strong>the</strong> winch. It is not<br />
uncommon for winch controls to<br />
be positioned such that <strong>the</strong> winch<br />
operator is unsighted and in such<br />
circumstances clear procedures<br />
must be put in place to prevent<br />
<strong>the</strong> winch being turned without<br />
<strong>the</strong> prior knowledge <strong>of</strong> those<br />
working in <strong>the</strong> vicinity. Conversely,<br />
if a crew member has to approach<br />
a winch he should ensure <strong>the</strong><br />
winch operator is made aware <strong>of</strong><br />
his impending actions.<br />
Root Cause:<br />
Dangerous operational practices.<br />
Financial Cost:<br />
US$200,575.<br />
Issue Date: 03/10/07<br />
Case No. 40374<br />
As is <strong>the</strong> case with most <strong>of</strong><br />
<strong>the</strong>se incidents, saving time is<br />
considered to be more important<br />
than safety and shortcuts are<br />
taken. It is only when injuries<br />
are suffered that crew have<br />
more than enough time to<br />
reflect on <strong>the</strong> consequences <strong>of</strong><br />
compromising safety.<br />
108 109
Personal Injury/Illness<br />
Good Intentions Result in a Very Large Claim<br />
The Incident:<br />
This accident occurred to an engineer on board a<br />
fishing vessel.<br />
During fishing operations a hydraulic hose developed<br />
a leak. The vessel’s engineer was called and after<br />
examining <strong>the</strong> hose, <strong>the</strong> engineer placed his thumb over<br />
<strong>the</strong> hole and <strong>the</strong>n instructed ano<strong>the</strong>r crew member to<br />
operate <strong>the</strong> controls. As a result <strong>of</strong> this, hydraulic oil at<br />
1600 psi was injected into his thumb.<br />
The skipper was called to <strong>the</strong> scene. He examined<br />
<strong>the</strong> injury which initially resembled an insect bite.<br />
The skipper suggested that <strong>the</strong> vessel returned<br />
to port. The engineer himself opposed this idea<br />
and dismissed <strong>the</strong> injury as a trivial matter <strong>of</strong> no<br />
consequence. The skipper did not seek fur<strong>the</strong>r<br />
medical advice.<br />
The vessel returned to port three days later. By <strong>the</strong><br />
time <strong>the</strong> engineer reached hospital his thumb had<br />
swollen considerably and he was in severe pain.<br />
Over <strong>the</strong> following two years he underwent a series<br />
<strong>of</strong> operations, but despite this he has been left with<br />
a permanent disability which prevents him from ever<br />
returning to work as an engineer.<br />
Observations:<br />
Although it was clear <strong>the</strong> injury was caused by <strong>the</strong><br />
engineer’s own actions, <strong>the</strong> long term effects <strong>of</strong><br />
<strong>the</strong> injury were due to <strong>the</strong> lack <strong>of</strong> prompt medical<br />
treatment. If <strong>the</strong> injury had been treated within 12<br />
hours <strong>of</strong> <strong>the</strong> incident, it would have been unlikely that<br />
any serious or permanent injuries would have resulted.<br />
Although <strong>the</strong> skipper acted with <strong>the</strong> best intentions<br />
and was guided in his evaluation <strong>of</strong> <strong>the</strong> injury by<br />
<strong>the</strong> engineer himself, <strong>the</strong> fact that he did not obtain<br />
proper medical advice resulted in <strong>the</strong> shipowner<br />
being found liable. If <strong>the</strong>y are in any doubt a Master<br />
should always seek medical advice. Such advice is<br />
<strong>read</strong>ily available by radio and is free <strong>of</strong> charge.<br />
Root Cause:<br />
Human error.<br />
Issue Date: 01/01/02<br />
Case No. 30582<br />
110 111
Navigation<br />
When a Lookout should Lookout<br />
The Incident:<br />
This claim involves a collision<br />
between a fishing vessel and a<br />
17000 gt products tanker.<br />
The Member’s vessel, a stern<br />
trawler was proceeding to<br />
her intended fishing grounds,<br />
which required her to cross a<br />
traffic separation scheme. The<br />
Member’s vessel contravened<br />
Rule 10c <strong>of</strong> <strong>the</strong> Collision<br />
Regulations by not crossing <strong>the</strong><br />
traffic lane at right angles.<br />
The Master had left <strong>the</strong><br />
wheelhouse and an inexperienced<br />
17 year old deckhand was left<br />
alone on watch.<br />
A radar target was noted<br />
approximately 3 miles on <strong>the</strong><br />
starboard bow, and after making<br />
a visual check, <strong>the</strong> watch-keeper<br />
made <strong>the</strong> assumption that<br />
<strong>the</strong> vessel would pass clear to<br />
starboard; having made this<br />
assessment <strong>the</strong> watch-keeper paid<br />
no fur<strong>the</strong>r attention to his lookout<br />
duties. More than one vessel was<br />
in fact within <strong>the</strong> immediate vicinity<br />
and <strong>the</strong> fishing vessel collided with<br />
ano<strong>the</strong>r ship shortly <strong>the</strong>reafter.<br />
The watch-keeper realised<br />
a collision was to take place<br />
seconds before it actually<br />
occurred. He put <strong>the</strong> wheel<br />
over, but as he had not<br />
disconnected <strong>the</strong> auto pilot<br />
<strong>the</strong>re was no response.<br />
Fortunately <strong>the</strong>re was no loss<br />
<strong>of</strong> life, but each vessel sustained<br />
heavy damage.<br />
Observations:<br />
The Member’s vessel failed to maintain a proper<br />
lookout and this was compounded by <strong>the</strong> fact that<br />
an inexperienced crew member was left in charge<br />
<strong>of</strong> <strong>the</strong> watch whilst transiting an area <strong>of</strong> heavy<br />
traffic. Having noted a radar target on <strong>the</strong> starboard<br />
bow and making an initial assessment , no fur<strong>the</strong>r<br />
observations were made until it was too late.<br />
The importance <strong>of</strong> maintaining a proper lookout<br />
cannot be over emphasised nor can <strong>the</strong> need to<br />
monitor all vessels closely when navigating in busy<br />
waterways. Consideration should always be given to<br />
“doubling up” watches in <strong>the</strong>se circumstances.<br />
Root Cause:<br />
Inadequate lookout.<br />
Financial Cost:<br />
The claim is expected to be no less than<br />
US$400,000.<br />
Issue Date: 18/06/03<br />
Case No. 35122<br />
112 113
Navigation<br />
Distracted Skipper Dims Beacon Light<br />
The Incident:<br />
This incident involved an Australian cray fishing vessel. In common with <strong>the</strong> majority <strong>of</strong><br />
this fleet this small vessel is highly powered and navigates at high speed.<br />
The vessel in question had just undergone engine repairs to try to cure an overheating<br />
problem with <strong>the</strong> main engines. The skipper and one deckhand took <strong>the</strong> vessel out<br />
on sea trials. During <strong>the</strong> trials <strong>the</strong> skipper was keeping a careful eye on <strong>the</strong> engine<br />
temperature gauges. As no problems were encountered <strong>the</strong> vessel’s speed was steadily<br />
increased until she was travelling at approximately 18 knots. The skipper’s attention was<br />
so firmly fixed on <strong>the</strong> engine gauges that he failed to notice a navigational marker dead<br />
ahead. Fortunately <strong>the</strong> deckhand who had just come onto <strong>the</strong> bridge spotted <strong>the</strong> beacon<br />
before <strong>the</strong> collision, enabling <strong>the</strong> Master to kill <strong>the</strong> power. Never<strong>the</strong>less <strong>the</strong> resulting<br />
collision severely damaged <strong>the</strong> boat and <strong>the</strong> beacon.<br />
Observations:<br />
This incident emphasises <strong>the</strong> need to maintain<br />
a good lookout at all times as required by <strong>the</strong><br />
International Regulations for <strong>the</strong> Prevention <strong>of</strong><br />
Collision at Sea. Had <strong>the</strong> deckhand not arrived<br />
on <strong>the</strong> bridge at <strong>the</strong> time he did, <strong>the</strong> vessel would<br />
have undoubtedly ploughed into <strong>the</strong> beacon at full<br />
speed with possibly disastrous consequences for<br />
those on board.<br />
Root Cause:<br />
Inadequate lookout.<br />
Financial Cost:<br />
The repairs to <strong>the</strong> beacon cost A$96,500<br />
(US$76,405).<br />
Issue Date: 01/01/02<br />
Case No. 24553<br />
114 115
Navigation<br />
Total Loss<br />
The Incident:<br />
A 360 ton deep sea fishing<br />
vessel had called at Pago Pago in<br />
American Samoa for bunkers en<br />
route to her fishing grounds east<br />
<strong>of</strong> Tahiti. She left Pago Pago in <strong>the</strong><br />
afternoon, steering an easterly<br />
course set to pass nine miles north<br />
<strong>of</strong> Rose Atoll, <strong>the</strong> only US National<br />
Wildlife Reserve in <strong>the</strong> sou<strong>the</strong>rn<br />
hemisphere. At approximately 4<br />
a.m. in clear wea<strong>the</strong>r <strong>the</strong> vessel<br />
ran hard aground on <strong>the</strong> south<br />
western side <strong>of</strong> <strong>the</strong> atoll. The<br />
forward double bottom tank<br />
below <strong>the</strong> fish holds ruptured<br />
immediately and oil started to spill<br />
from <strong>the</strong> vessel. The vessel was<br />
abandoned later in <strong>the</strong> morning<br />
after <strong>the</strong> engine room began to<br />
flood. The crew were picked<br />
up by a passing vessel without<br />
serious injury or loss <strong>of</strong> life.<br />
The nearest suitable salvage<br />
vessel was 2,000 miles from <strong>the</strong><br />
site and by <strong>the</strong> time it arrived<br />
<strong>the</strong> fishing vessel had broken up,<br />
spilling nearly 100,000 gallons<br />
<strong>of</strong> gas oil bunkers. Damage<br />
to <strong>the</strong> reef caused by <strong>the</strong><br />
grounding and <strong>the</strong> toxic effects<br />
<strong>of</strong> <strong>the</strong> oil extended to a radius<br />
<strong>of</strong> approximately 1 km from<br />
<strong>the</strong> wreck. The US authorities<br />
required that a clean-up<br />
operation be mounted and <strong>the</strong><br />
remains <strong>of</strong> <strong>the</strong> vessel removed.<br />
Observations:<br />
There were only two qualified<br />
<strong>of</strong>ficers on <strong>the</strong> fishing vessel, <strong>the</strong><br />
Master and <strong>the</strong> Chief Officer.<br />
The Chief Officer’s responsibility<br />
was apparently confined to <strong>the</strong><br />
operation and maintenance <strong>of</strong><br />
<strong>the</strong> fishing gear. He was not<br />
involved in navigational duties.<br />
After sailing <strong>the</strong> Master remained<br />
on <strong>the</strong> bridge until midnight<br />
when <strong>the</strong> vessel passed south<br />
<strong>of</strong> Manua Island. Before retiring<br />
<strong>the</strong> Master set bridge watches<br />
which consisted <strong>of</strong> one senior<br />
and one junior seaman. The only<br />
instruction given to <strong>the</strong> seamen by<br />
<strong>the</strong> Master were to call him if <strong>the</strong>y<br />
saw any lights. Rose Atoll is not lit.<br />
None <strong>of</strong> <strong>the</strong> seamen given <strong>the</strong> task <strong>of</strong> keeping watch had any<br />
navigational training. They had no knowledge <strong>of</strong> <strong>the</strong> collision<br />
regulations and were not even sure in which direction <strong>the</strong> vessel<br />
was steaming. They had no knowledge <strong>of</strong> navigational hazards in <strong>the</strong><br />
vicinity and <strong>the</strong>re was no chart on <strong>the</strong> bridge. They were untrained<br />
in <strong>the</strong> use <strong>of</strong> radar and <strong>the</strong> set was switched <strong>of</strong>f. The vessel was<br />
equipped with a GPS navigation system however <strong>the</strong> watchkeepers<br />
did not know how to ascertain <strong>the</strong>ir position and were unable<br />
to check whe<strong>the</strong>r <strong>the</strong> vessel was following <strong>the</strong> course set by <strong>the</strong><br />
Master.<br />
Root Cause:<br />
Insufficient manning.<br />
Financial Cost:<br />
In addition to losing a multi million dollar vessel <strong>the</strong> owner faced a<br />
bill <strong>of</strong> over US$1 million for clean-up and was also liable for fines and<br />
penalties under American pollution laws.<br />
Issue Date: 01/01/02<br />
Case No. 21195<br />
116 117
Navigation<br />
Fatigue Causes Grounding and Total Loss<br />
The Incident:<br />
This incident involves <strong>the</strong> grounding and subsequent<br />
total loss <strong>of</strong> a seine fishing vessel. The vessel was<br />
returning to its home port at <strong>the</strong> end <strong>of</strong> <strong>the</strong> salmon<br />
fishing season. She was proceeding in company<br />
with ano<strong>the</strong>r fishing vessel owned and operated by<br />
<strong>the</strong> captain’s bro<strong>the</strong>r. The maximum speed <strong>of</strong> this<br />
vessel was approximately 4 knots less than our ship.<br />
The two bro<strong>the</strong>rs believed that travelling rafted<br />
toge<strong>the</strong>r in sheltered water would reduce <strong>the</strong>ir<br />
overall passage time. Thus when <strong>the</strong> vessels entered<br />
<strong>the</strong> Greenville Channel which forms part <strong>of</strong> <strong>the</strong><br />
Inner Passage between <strong>the</strong> <strong>of</strong>f lying islands and <strong>the</strong><br />
coast <strong>of</strong> British Columbia <strong>the</strong> vessels were lashed<br />
alongside one ano<strong>the</strong>r and proceeded as a rafted<br />
unit. In <strong>the</strong> early hours <strong>of</strong> <strong>the</strong> morning both vessels<br />
ran hard aground on a small promontory on <strong>the</strong><br />
port side <strong>of</strong> <strong>the</strong> channel at a point where <strong>the</strong>re was<br />
a slight bend to starboard. An order to remove <strong>the</strong><br />
vessels was issued by <strong>the</strong> Department <strong>of</strong> Fisheries.<br />
Observations:<br />
No agreement had been reached for controlling<br />
<strong>the</strong> navigation <strong>of</strong> <strong>the</strong> combined unit. Nei<strong>the</strong>r vessel<br />
could control <strong>the</strong> course or engines <strong>of</strong> <strong>the</strong> o<strong>the</strong>r.<br />
Both vessels were on autopilot. The wheelhouse <strong>of</strong><br />
each vessel was manned by a single watchkeeper<br />
whose only method <strong>of</strong> communication with his<br />
counterpart was by VHF radio. At <strong>the</strong> time <strong>of</strong> <strong>the</strong><br />
grounding <strong>the</strong> watchkeeper on <strong>the</strong> o<strong>the</strong>r fishing<br />
vessel had reportedly left <strong>the</strong> wheelhouse to relieve<br />
himself and <strong>the</strong> watchkeeper on our vessel had fallen<br />
asleep.<br />
At some point shortly before <strong>the</strong> grounding <strong>the</strong><br />
vessels had run into a bank <strong>of</strong> fog however this was<br />
probably not causative <strong>of</strong> <strong>the</strong> loss. The most likely<br />
explanation is that with one bridge unmanned and <strong>the</strong><br />
o<strong>the</strong>r watchkeeper asleep <strong>the</strong> vessels failed to make<br />
<strong>the</strong> slight alteration <strong>of</strong> course necessary to follow <strong>the</strong><br />
channel. The problem was probably compounded<br />
by <strong>the</strong> fact that <strong>the</strong> more powerful vessel lay on <strong>the</strong><br />
starboard side <strong>of</strong> <strong>the</strong> o<strong>the</strong>r, making <strong>the</strong> combined unit<br />
more likely to veer to port.<br />
Root Cause:<br />
Poor navigational practices.<br />
Financial Cost:<br />
The smaller vessel was a<br />
constructive total loss and<br />
<strong>the</strong> larger vessel was severely<br />
damaged. Both vessels were<br />
refloated by <strong>the</strong>ir respective<br />
owners’ efforts. Never<strong>the</strong>less<br />
<strong>the</strong> costs incurred exceeded<br />
US$20,000.<br />
Issue Date: 01/01/02<br />
Case No. 24451<br />
It is unlikely that both vessels would have grounded<br />
had <strong>the</strong>y been navigating independently. With <strong>the</strong><br />
vessels rafted side by side both on autopilot and<br />
with no system for controlling <strong>the</strong> course or <strong>the</strong><br />
engines <strong>of</strong> <strong>the</strong> o<strong>the</strong>r, <strong>the</strong> slightest error by ei<strong>the</strong>r<br />
watchkeeper would almost inevitably end in disaster.<br />
118 119
Navigation<br />
If Only he could Swim<br />
The Incident:<br />
This incident involved a boom trawler stranding<br />
whilst fishing for prawns and is one <strong>of</strong> a number<br />
<strong>of</strong> similar incidents <strong>the</strong> Club has been involved<br />
with recently.<br />
The vessel was fishing approximately 0.5 miles<br />
from <strong>the</strong> shore with <strong>the</strong> Skipper on watch, alone.<br />
At approximately 23:00 on <strong>the</strong> evening in question,<br />
<strong>the</strong> engineer advised <strong>the</strong> Skipper that a problem had<br />
developed with <strong>the</strong> hydraulic pump for <strong>the</strong> trawl<br />
winch, rendering it inoperative. The Skipper left<br />
<strong>the</strong> wheelhouse to assess <strong>the</strong> situation for himself<br />
and returned shortly afterwards to telephone<br />
his managers. Whilst on <strong>the</strong> phone, <strong>the</strong> vessel<br />
grounded. After a list <strong>of</strong> some 35º developed,<br />
<strong>the</strong> crew donned <strong>the</strong>ir lifejackets, two liferafts<br />
were launched and <strong>the</strong> vessel was abandoned.<br />
Unfortunately <strong>the</strong> cook could not swim and,<br />
on entering <strong>the</strong> water, he panicked and<br />
subsequently drowned.<br />
Observations:<br />
The prime cause <strong>of</strong> <strong>the</strong> incident<br />
was <strong>the</strong> fact that <strong>the</strong> wheelhouse<br />
was undermanned. The vessel<br />
grounded only 100 metres from<br />
<strong>the</strong> shoreline which shows that<br />
during <strong>the</strong> time <strong>the</strong> Skipper’s<br />
attention had been diverted,<br />
<strong>the</strong> wind and current had set<br />
<strong>the</strong> vessel in towards <strong>the</strong> shore.<br />
Being alone on watch <strong>the</strong> Skipper<br />
had many tasks to attend to<br />
not least <strong>the</strong> navigation <strong>of</strong> <strong>the</strong><br />
vessel, keeping a lookout and<br />
steering, all whilst operating<br />
close inshore. The failure <strong>of</strong> <strong>the</strong><br />
hydraulic pump increased <strong>the</strong><br />
demands placed on <strong>the</strong> Skipper<br />
which led to <strong>the</strong> wheelhouse<br />
being left unmanned for a period<br />
<strong>of</strong> time and navigation continuing<br />
unmonitored whilst <strong>the</strong> telephone<br />
call to <strong>the</strong> managers took place.<br />
The incident was caused by a<br />
failure on <strong>the</strong> Skipper’s part to<br />
call for suitable assistance in<br />
<strong>the</strong> wheelhouse. There were<br />
no moves to supplement <strong>the</strong><br />
wheelhouse watch whilst <strong>the</strong><br />
Skipper’s attention was diverted<br />
to <strong>the</strong> problems with <strong>the</strong><br />
hydraulic pump which is difficult<br />
to understand considering <strong>the</strong><br />
proximity <strong>of</strong> <strong>the</strong> vessel to <strong>the</strong><br />
shore. Manning levels on fishing<br />
boats, whilst in accordance with<br />
Flag State requirements do not<br />
always provide for <strong>the</strong> luxury <strong>of</strong><br />
spare qualified crew members,<br />
but when circumstances dictate,<br />
as in this case, adjustments to<br />
work routines should be made<br />
to ensure <strong>the</strong> safety <strong>of</strong> <strong>the</strong> crew<br />
and vessel.<br />
In all likelihood, had <strong>the</strong> cook<br />
been able to swim, he would not<br />
have panicked to <strong>the</strong> extent he<br />
did and would probably still be<br />
alive today. He was found wearing<br />
his lifejacket. The Flag States<br />
Code <strong>of</strong> Safe Working Practices<br />
for Fishing Vessels recommends<br />
that all fishermen should be able<br />
to swim. So do we.<br />
Root Cause:<br />
Inadequate navigational practices.<br />
Financial Cost:<br />
The cost to <strong>the</strong> Club was only<br />
US$2,776. Fortunately <strong>the</strong> vessel’s<br />
diesel oil was blown out to sea<br />
with no beach pollution taking<br />
place. The crew were covered<br />
under <strong>the</strong> Flag States Workman’s<br />
Compensation Act and <strong>the</strong><br />
Club was not required by <strong>the</strong><br />
authorities to remove <strong>the</strong> wreck<br />
even though it had grounded in a<br />
scientifically sensitive area.<br />
The cost to <strong>the</strong> cook and his<br />
family was beyond calculation.<br />
Issue Date: 01/01/02<br />
Case No. 30438<br />
120 121
Navigation<br />
Unmanned Wheelhouses Cause Collision<br />
The Incident:<br />
The vessel involved in this collision was a<br />
19 metre steel trawler which worked <strong>the</strong><br />
scallop and prawn fishery <strong>of</strong>f <strong>the</strong> coast <strong>of</strong><br />
Queensland, Australia. The vessel fished by<br />
night and anchored during <strong>the</strong> day. She was<br />
manned by a crew <strong>of</strong> two. On <strong>the</strong> morning<br />
<strong>of</strong> <strong>the</strong> collision <strong>the</strong>y finished fishing at 7<br />
a.m. The skipper set course for her home<br />
port, handing over <strong>the</strong> watch to <strong>the</strong> deck<br />
hand in late morning. In <strong>the</strong> early afternoon<br />
<strong>the</strong> vessel collided with ano<strong>the</strong>r fishing<br />
vessel which was lying at anchor.<br />
Observations:<br />
At <strong>the</strong> time <strong>of</strong> <strong>the</strong> collision nei<strong>the</strong>r vessel<br />
was keeping a proper lookout as required<br />
by <strong>the</strong> International Regulations for<br />
<strong>the</strong> Prevention <strong>of</strong> <strong>the</strong> Collisions at sea.<br />
No anchor watch had been set on <strong>the</strong><br />
anchored vessel and all her crew were<br />
turned in. The crew member that was<br />
supposed to be keeping a navigational<br />
watch on our Member’s vessel was in<br />
fact on <strong>the</strong> afterdeck cleaning when <strong>the</strong><br />
collision occurred. The vessel was not<br />
fitted with a watch alarm, nor did it have a<br />
guardring facility on <strong>the</strong> radar.<br />
Root Cause:<br />
Inadequate navigational lookout.<br />
Financial Cost:<br />
Repairs to <strong>the</strong> anchored vessel cost over<br />
A$100,000. It was out <strong>of</strong> action at <strong>the</strong> height <strong>of</strong><br />
<strong>the</strong> scallop season for over two months, giving rise<br />
to a substantial claim for loss <strong>of</strong> pr<strong>of</strong>its, which was<br />
eventually settled for A$45,000. In addition to this<br />
<strong>the</strong>re was substantial damage to our Member’s<br />
vessel and it too was out <strong>of</strong> action for a substantial<br />
period at <strong>the</strong> height <strong>of</strong> <strong>the</strong> season.<br />
Issue Date: 01/01/02<br />
Case No. 23183<br />
122 123
Navigation<br />
A fatal nap<br />
The Incident:<br />
The crew <strong>of</strong> a longline fishing vessel had to abandon<br />
ship in violent seas at night after she grounded<br />
on rocks. The skipper drowned and one crew<br />
member’s body was never recovered. Two o<strong>the</strong>r<br />
crew members were tossed against rocks in stormy<br />
seas for hours. Before <strong>the</strong> grounding, no one had<br />
been keeping an anchor watch.<br />
The 18 metre steel-hulled commercial longliner set<br />
<strong>of</strong>f on a three day voyage at a time when heavy storm<br />
warnings were issued for all <strong>of</strong> <strong>the</strong> country, and most<br />
vessels in <strong>the</strong> area were heading for safe anchorage.<br />
In <strong>the</strong> late afternoon <strong>of</strong> <strong>the</strong> second day, <strong>the</strong> skipper<br />
anchored in a large bay. To get <strong>the</strong>re, <strong>the</strong> vessel<br />
steamed about 20 nautical miles past a safe and open<br />
port and instead anchored approximately 300 metres<br />
from a rocky coastline in about two metre seas.<br />
The nearby port’s Harbour Master saw <strong>the</strong> vessel<br />
‘punching’ through <strong>the</strong> seas and thought it peculiar<br />
for <strong>the</strong> vessel to stay at sea in such conditions.<br />
About an hour before <strong>the</strong> vessel weighed anchor,<br />
a nearby wave buoy recorded wave heights <strong>of</strong> 3.2<br />
metres, reaching 6.2 metres and increasing. Soon<br />
after midnight, <strong>the</strong> crew all turned in for <strong>the</strong> night.<br />
No anchor watch was kept. The vessel was fitted<br />
with radar and a GPS, depth sounder and course<br />
plotter, but none <strong>of</strong> <strong>the</strong>se were set to supplement<br />
an anchor watch or provide an alert.<br />
At about 3 am, <strong>the</strong> crew were woken by heavy<br />
waves battering <strong>the</strong> vessel. They soon discovered<br />
<strong>the</strong> vessel had dragged her anchor and was almost<br />
aground against <strong>the</strong> rocky coastline. Wave buoy<br />
recordings show that by this time <strong>the</strong> swells had<br />
increased to 5.2 metres, reaching a maximum <strong>of</strong> 9.1<br />
metres. At <strong>the</strong> vessel’s position, <strong>the</strong> waves would have<br />
been significantly higher in <strong>the</strong> shallow water.<br />
Waves had damaged <strong>the</strong> vessel, and she was set in to<br />
<strong>the</strong> shore with big seas breaking over her. The crew<br />
attempted to recover <strong>the</strong> anchor, but <strong>the</strong> winch would<br />
not operate. Attempts to cut <strong>the</strong> anchor wire with<br />
bolt cutters failed. When <strong>the</strong> vessel hit <strong>the</strong> rocks, <strong>the</strong><br />
skipper gave <strong>the</strong> order to abandon ship and set <strong>of</strong>f a<br />
distress beacon. All four on board dived into <strong>the</strong> sea.<br />
The skipper and one crew member drowned.<br />
The two remaining crew members spent hours in<br />
<strong>the</strong> water, being smashed by waves. One suffered<br />
a collapsed lung and extensive cuts and bruising.<br />
The o<strong>the</strong>r managed to crawl onto a small beach<br />
and suffered hypo<strong>the</strong>rmia. They were eventually<br />
rescued by helicopter and flown to hospital.<br />
Observations:<br />
1. Given <strong>the</strong> wea<strong>the</strong>r conditions from <strong>the</strong> outset<br />
<strong>of</strong> <strong>the</strong> voyage and <strong>the</strong> forecast, <strong>the</strong> vessel should<br />
not have set sail. Once en route, <strong>the</strong>re were two<br />
ports within timely reach <strong>of</strong> <strong>the</strong> vessel where she<br />
could have ber<strong>the</strong>d safely.<br />
2. The position <strong>the</strong> skipper chose to anchor in was<br />
unsuitable for <strong>the</strong> conditions, but <strong>the</strong> skipper did<br />
not seek local knowledge about a better location<br />
from Marine Radio or <strong>the</strong> Harbour Master.<br />
3. No anchor watch was kept by <strong>the</strong> crew. Maritime<br />
rules require that a proper lookout is maintained<br />
at all times and, given <strong>the</strong> conditions, was essential<br />
for <strong>the</strong> safety <strong>of</strong> <strong>the</strong> vessel.<br />
4. In addition to its four crew members, <strong>the</strong> vessel<br />
was fitted with radar and a GPS, depth sounder<br />
and chart plotter, which could have been set<br />
to assist <strong>the</strong> designated watchkeepers. Failing<br />
to maintain an anchor watch appeared to be<br />
standard practice on this vessel.<br />
5. The company that had contracted <strong>the</strong> vessel had<br />
adopted a ‘hands-<strong>of</strong>f’ approach to monitoring<br />
<strong>the</strong> safety performance <strong>of</strong> vessels it contracted.<br />
The operations manager knew this vessel was<br />
departing into <strong>the</strong> storm and, despite discussing<br />
<strong>the</strong> potential catch with <strong>the</strong> crew, made no<br />
mention <strong>of</strong> <strong>the</strong> wea<strong>the</strong>r. It was company policy<br />
to nei<strong>the</strong>r require nor dissuade a crew from<br />
undertaking a particular voyage.<br />
6. The need for keeping an anchor watch,<br />
particularly in adverse wea<strong>the</strong>r or when<br />
anchored on an open coastline, should have<br />
been reinforced by <strong>the</strong> contracting company.<br />
Both factors applied in this case and <strong>the</strong> failure<br />
directly contributed to <strong>the</strong> loss <strong>of</strong> <strong>the</strong> vessel<br />
and two lives. This dangerous failing could have<br />
been identified and corrected.<br />
7. As a result <strong>of</strong> this tragedy, <strong>the</strong> contracting<br />
company was fined and required to pay<br />
reparations to <strong>the</strong> victims’ families. The court<br />
found that <strong>the</strong> company failed to implement<br />
adequate policies or processes to ensure <strong>the</strong><br />
vessel’s crew properly followed maritime rules<br />
by ensuring a proper anchor watch was kept..<br />
Trading Area:<br />
Australasia & Pacific<br />
Issue Date: 23/08/10<br />
Case No. 230810<br />
This case study has been taken from:<br />
Maritime New Zealand’s ‘lookout’ issue 17.<br />
124 125
Pollution<br />
Short Cuts can take Longer<br />
The Incident:<br />
This incident involved <strong>the</strong> inadvertent spill overboard<br />
<strong>of</strong> oil during an internal transfer <strong>of</strong> bunkers.<br />
The day prior to <strong>the</strong> oil spill, <strong>the</strong> engineers had<br />
been pumping waste oil to a shore reception facility.<br />
Because it was felt <strong>the</strong> operation would take too<br />
long utilising <strong>the</strong> standard connection as required by<br />
<strong>the</strong> MARPOL regulations, a cross connection had<br />
been fabricated to fit between <strong>the</strong> bilge and bunker<br />
systems. The waste oil was <strong>the</strong>n pumped ashore<br />
via <strong>the</strong> bunker manifold without incident. When an<br />
internal transfer <strong>of</strong> oil was commenced <strong>the</strong> following<br />
day, heavy fuel oil spilled onto deck through an open<br />
manifold connection and <strong>the</strong>n spilt overboard.<br />
Observations:<br />
The vessel was detained by <strong>the</strong><br />
harbour authorities on a number<br />
<strong>of</strong> deficiencies which came to<br />
light during investigations into<br />
<strong>the</strong> incident. These included:-<br />
1. Oil Record Book not being<br />
correctly maintained<br />
2. SOPEP not updated<br />
3. Crew not familiar with<br />
<strong>the</strong> procedures required<br />
by <strong>the</strong> SOPEP<br />
4. Unauthorised cross<br />
connection between <strong>the</strong><br />
bilge and bunker systems.<br />
Notwithstanding <strong>the</strong> illegal cross<br />
connection, <strong>the</strong> primary cause <strong>of</strong><br />
this oil spill was <strong>the</strong> fact that valves<br />
utilised during <strong>the</strong> previous day’s<br />
operation had not been closed<br />
upon completion nor had <strong>the</strong><br />
manifold connection been blanked.<br />
It is imperative that pipeline<br />
systems are fully closed down<br />
after use and when utilised again,<br />
<strong>the</strong> pipelines and valves are<br />
checked during <strong>the</strong> early stages<br />
to ensure <strong>the</strong> oil is only flowing<br />
to <strong>the</strong> required destination and<br />
nowhere else.<br />
The ironic aspect <strong>of</strong> this incident<br />
was that <strong>the</strong> time saved in<br />
pumping <strong>the</strong> waste oil ashore via<br />
<strong>the</strong> bunker system was lost in<br />
<strong>the</strong> detention <strong>of</strong> <strong>the</strong> vessel which<br />
lasted four days.<br />
Root Cause:<br />
Inadequate SOPEP procedures.<br />
Financial Cost:<br />
The cost <strong>of</strong> this incident including<br />
fines and clean up charges is<br />
estimated to be US$90,000.<br />
Issue Date: 27/10/05<br />
Case No.42370<br />
126 127
Pollution<br />
Environmentally Unfriendly Bunkering<br />
The Incident:<br />
The Club is concerned at <strong>the</strong> number <strong>of</strong> oil pollution claims arising<br />
from oil transfer operations carried out by large fishing vessels,<br />
particularly in European ports.<br />
Typical examples are:<br />
1. A 7300 GT fishing vessel was to pump <strong>the</strong> contents <strong>of</strong> her sludge<br />
tank ashore to a road tanker hired for <strong>the</strong> purpose. The hose was<br />
connected and, immediately upon commencement <strong>of</strong> pumping,<br />
oil escaped on to <strong>the</strong> deck and into <strong>the</strong> dock from <strong>the</strong> outboard<br />
connection. Investigation showed that this unused connection had<br />
been left with its valve open and blank flange missing.<br />
2. A vessel <strong>of</strong> 2417 GT commenced bunkering heavy fuel oil.<br />
Approximately 30 minutes later, personnel observed oil spilling on<br />
to <strong>the</strong> deck and into <strong>the</strong> harbour waters. The leak was traced to a<br />
loose flange on an elbow piece at <strong>the</strong> manifold connection.<br />
3. In ano<strong>the</strong>r case oil was observed spilling out <strong>of</strong> an air vent and<br />
subsequently over <strong>the</strong> vessel’s side. Investigations showed that <strong>the</strong><br />
labels on <strong>the</strong> filling connections had been incorrectly placed and<br />
<strong>the</strong> wrong tank was being filled. (It should be pointed out that this<br />
bunkering operation was usually carried out on <strong>the</strong> o<strong>the</strong>r side <strong>of</strong> <strong>the</strong><br />
vessel without incident, but due to operational reasons this was not<br />
possible on this occasion).<br />
4. During <strong>the</strong> final stages <strong>of</strong> a bunkering operation, heavy fuel<br />
oil spilled out <strong>of</strong> <strong>the</strong> receiving tanks air pipe. Operations were<br />
immediately stopped but not before a quantity <strong>of</strong> oil had run<br />
out through <strong>the</strong> scupper pipes. It is thought <strong>the</strong> cause was an air<br />
bubble in <strong>the</strong> bunker tank which probably arose because <strong>of</strong> <strong>the</strong><br />
vessel’s three degree list and large stern trim at <strong>the</strong> time. The o<strong>the</strong>r<br />
possibility was an incorrect assessment <strong>of</strong> <strong>the</strong> capacity available.<br />
Observations:<br />
To some extent, <strong>the</strong>se incidents are all attributable<br />
to lax bunkering procedures. In one case, none <strong>of</strong><br />
<strong>the</strong> vessel’s staff were on board overseeing <strong>the</strong><br />
operation. All could have been prevented with a<br />
little more conscientious monitoring <strong>of</strong> operations.<br />
Loose flanges and open ended pipes appear to be a<br />
common feature.<br />
All <strong>the</strong> vessels in question have a gross tonnage<br />
in excess <strong>of</strong> 400 tonnes, so are governed by <strong>the</strong><br />
MARPOL regulations, in particular <strong>the</strong> Shipboard<br />
Oil Pollution Emergency Plan (SOPEP) which is in<br />
place to prevent instances described above.<br />
The non-mandatory section <strong>of</strong> a vessel’s SOPEP<br />
Manual should contain <strong>the</strong> operating company’s<br />
bunkering procedures. Equally, vessels to which <strong>the</strong><br />
regulations do not apply would be well advised to<br />
have in place similar procedures.<br />
Such procedures we believe should include <strong>the</strong><br />
following requirements:<br />
1. All valves in a pipeline system not required to be<br />
opened should be confirmed as being closed.<br />
2. All flanges not in use should be blanked <strong>of</strong>f.<br />
3. A crew member should be detailed to remain on<br />
deck at or near <strong>the</strong> manifold connection during<br />
<strong>the</strong> entire operation.<br />
4. Bunkering operations should be started and<br />
completed at a slow rate until a) it is confirmed<br />
that <strong>the</strong> oil is going into <strong>the</strong> correct tank and<br />
<strong>the</strong>re are no leaks and b) <strong>the</strong> tanks are “topped<br />
<strong>of</strong>f” in a controlled manner.<br />
5. Scupper plugs should be fitted and if this is<br />
not feasible, savealls fitted around <strong>the</strong> bunker<br />
connections and air vents should be <strong>of</strong> a practical<br />
size.<br />
6. Oil spill clean up equipment and absorbents<br />
should be placed on deck.<br />
Root Cause:<br />
Inadequate bunkering procedures.<br />
Issue Date:01/01/02<br />
Case No. 35341<br />
128 129
Section 4<br />
Passenger Vessels<br />
131
Passenger Vessels<br />
Personal Injury/Illness<br />
To be Forewarned should mean you are Forearmed<br />
The Incident:<br />
Shortly after boarding <strong>the</strong> vessel, a small passenger<br />
ferry, a young girl aged 10 fell down a storeroom<br />
access. She apparently climbed out <strong>of</strong> <strong>the</strong> 2 metre<br />
deep opening via a fixed ladder <strong>of</strong> her own accord.<br />
Her parents notified <strong>the</strong> crew and alerted <strong>the</strong><br />
shore based emergency services. She was taken<br />
to hospital and spent twelve days in <strong>the</strong> Intensive<br />
Care Unit as she was diagnosed as having a<br />
ruptured spleen. Subsequently <strong>the</strong> young girl<br />
made a full recovery.<br />
Apart from <strong>the</strong> girl’s parents, <strong>the</strong>re were no<br />
witnesses to <strong>the</strong> incident.<br />
Observations:<br />
Doubt exists as to whe<strong>the</strong>r or not <strong>the</strong> hatch cover<br />
used to secure <strong>the</strong> opening was in fact closed and<br />
<strong>the</strong> view taken is that a 10 year old girl, whilst not<br />
incapable <strong>of</strong> opening such a device would be unlikely<br />
to. However, <strong>the</strong> facts are that no warning or “No<br />
Admittance” notices were posted on or in <strong>the</strong> vicinity<br />
<strong>of</strong> <strong>the</strong> hatch cover and apart from a hook, <strong>the</strong> cover<br />
was not locked to prevent unauthorised opening.<br />
During investigations into <strong>the</strong> incident, <strong>the</strong> Chief<br />
Engineer admitted that he had observed on more<br />
than one occasion young passengers opening <strong>the</strong><br />
hatch cover out <strong>of</strong> curiosity, but unfortunately he<br />
had nei<strong>the</strong>r taken any action to secure <strong>the</strong> opening<br />
or advise anyone else <strong>of</strong> what he had observed.<br />
There are no safety reasons for <strong>the</strong> hatch cover not<br />
to have been padlocked closed when not in use as it<br />
only served a storeroom. Had it been secured in this<br />
manner, this incident would not have happened.<br />
The posting <strong>of</strong> warning or prohibitive signs would<br />
have made passengers aware <strong>of</strong> <strong>the</strong> dangers and<br />
would have helped <strong>the</strong> Member’s defence.<br />
Root Cause:<br />
Insufficient safety signs.<br />
Financial Cost:<br />
The lawyers were <strong>of</strong> <strong>the</strong> opinion that <strong>the</strong> Member<br />
would be held liable for <strong>the</strong> incident as it would<br />
be very difficult and expensive to prove any<br />
contributory negligence on behalf <strong>of</strong> a minor, thus<br />
<strong>the</strong> case was settled out <strong>of</strong> court.<br />
Total cost US$34,000.<br />
Issue Date: 01/01/02 Case No. 34113<br />
132 133
Personal Injury/Illness<br />
Difficult Step Causes Passenger Injury<br />
The Incident:<br />
This incident involves an injury to an elderly<br />
lady passenger disembarking from a tourist craft<br />
operating in north eastern Australia. The craft<br />
itself was <strong>of</strong> unusual construction, being a semisubmersible<br />
vessel which was designed to allow<br />
passengers to view coral reefs through windows in<br />
<strong>the</strong> lower deck below water level.<br />
The incident occurred after <strong>the</strong> vessel had returned<br />
to <strong>the</strong> dock. The passenger and her husband had<br />
not disembarked with <strong>the</strong> main body <strong>of</strong> passengers<br />
as <strong>the</strong>y had remained on board to search for a<br />
lost piece <strong>of</strong> camera equipment. Having found <strong>the</strong><br />
missing item <strong>the</strong>y ascended to <strong>the</strong> main deck and<br />
moved towards <strong>the</strong> gangway. To do so <strong>the</strong>y had<br />
to negotiate a change in level on <strong>the</strong> upper deck<br />
where <strong>the</strong>re was a 27 cm. step. In doing so <strong>the</strong> lady<br />
stumbled and fell, severely breaking her ankle.<br />
Observations:<br />
The raised section <strong>of</strong> <strong>the</strong> upper deck was covered<br />
to within 6 cms. <strong>of</strong> <strong>the</strong> step by a black plastic mat.<br />
The lower level and <strong>the</strong> 6 cm. strip along <strong>the</strong> edge<br />
<strong>of</strong> <strong>the</strong> higher level was painted with white non-skid<br />
paint. The result was that <strong>the</strong> edge <strong>of</strong> <strong>the</strong> step was<br />
difficult to detect visually. There were no handrails<br />
and <strong>the</strong>re were no warning notices or o<strong>the</strong>r visual<br />
warnings. Although crew members had been<br />
assigned to assist passengers at <strong>the</strong> gangway close<br />
by, none were assigned to assist passengers who<br />
negotiated <strong>the</strong> step.<br />
This accident should never have been allowed to<br />
happen. Our investigations revealed that crew<br />
members assigned to <strong>the</strong> gangway had observed<br />
passengers stumbling on <strong>the</strong> step on numerous<br />
occasions. If <strong>the</strong> company had implemented a safety<br />
management system <strong>the</strong> crew members would<br />
have a means <strong>of</strong> reporting <strong>the</strong>ir observations and<br />
appropriate measures could <strong>the</strong>n have been taken<br />
to minimise <strong>the</strong> risk to passengers. Those measures<br />
could have included painting <strong>the</strong> edge <strong>of</strong> <strong>the</strong> step<br />
in high visibility paint, <strong>of</strong> contrasting colour placing<br />
appropriate warning notices in <strong>the</strong> vicinity, fitting<br />
a handrail and stationing crew members to assist<br />
frail passengers in negotiating <strong>the</strong> change in level.<br />
Alternatively it might have been possible to replace<br />
<strong>the</strong> step with a ramp.<br />
Root Cause:<br />
Inadequate access.<br />
Financial Cost:<br />
The cost <strong>of</strong> this incident exceeded US$46,000.<br />
Issue Date: 01/01/02<br />
Case No. 21142<br />
134 135
Personal Injury/Illness<br />
One for <strong>the</strong> Water<br />
The Incident:<br />
The Members’ vessel was engaged on a wine and<br />
sightseeing tour. As <strong>the</strong> boat was leaving a jetty after<br />
a stop for refreshments and sightseeing, to return<br />
down river to her home berth, a passenger appeared<br />
to stand on <strong>the</strong> bow, step over <strong>the</strong> railings and jump<br />
or dive into <strong>the</strong> water. The skipper was alerted and<br />
he immediately put <strong>the</strong> engines into neutral. Efforts<br />
were <strong>the</strong>n made to manoeuvre <strong>the</strong> vessel to pick up<br />
<strong>the</strong> passenger. However, because <strong>of</strong> <strong>the</strong> configuration<br />
<strong>of</strong> <strong>the</strong> twin hulls <strong>the</strong> passenger went under <strong>the</strong><br />
bow and between <strong>the</strong> hulls where she caught her<br />
legs in <strong>the</strong> propeller housing causing <strong>the</strong> eventual<br />
amputation <strong>of</strong> both her feet.<br />
Observations:<br />
Lawyers acting for <strong>the</strong> passenger<br />
commenced proceedings alleging<br />
that she had fallen into <strong>the</strong> water<br />
as a result <strong>of</strong> insufficient guard<br />
railings and that her retrieval<br />
from <strong>the</strong> water was delayed<br />
for some 20 minutes while <strong>the</strong><br />
Master negligently manoeuvred<br />
<strong>the</strong> vessel causing her injury. (It is<br />
important to note that <strong>the</strong> <strong>of</strong>ficial<br />
investigation by <strong>the</strong> authorities<br />
exonerated <strong>the</strong> Master from any<br />
pr<strong>of</strong>essional blame).<br />
The Members asserted in defence<br />
that <strong>the</strong> passenger deliberately<br />
jumped into <strong>the</strong> water and was<br />
entirely responsible for her own<br />
injury. Witness evidence appeared<br />
to support <strong>the</strong> Members’ position<br />
that <strong>the</strong> passenger jumped <strong>of</strong>f<br />
<strong>the</strong> boat but also confirms that<br />
she was apparently intoxicated at<br />
<strong>the</strong> time. Despite this evidence<br />
<strong>the</strong> Members bore <strong>the</strong> brunt <strong>of</strong><br />
<strong>the</strong> responsibility <strong>of</strong> this incident<br />
despite <strong>the</strong> fact that it would<br />
appear <strong>the</strong> passenger acted <strong>of</strong><br />
her own volition. This case proves<br />
that <strong>the</strong> courts hold <strong>the</strong> carrier<br />
liable in such circumstances.<br />
Members are responsible for<br />
ensuring that passengers are<br />
not permitted to board <strong>the</strong>ir<br />
vessel whilst under <strong>the</strong> apparent<br />
influence <strong>of</strong> alcohol or drugs, or<br />
to drink excessively whilst on<br />
board. If it is considered that <strong>the</strong><br />
actions <strong>of</strong> passengers may put<br />
ei<strong>the</strong>r <strong>the</strong>mselves or o<strong>the</strong>rs in<br />
danger, efforts must be made by<br />
<strong>the</strong> ship’s crew to prevent such<br />
conduct getting out <strong>of</strong> hand.<br />
Prevention is better than cure!<br />
Root Cause:<br />
Lack <strong>of</strong> passenger supervision.<br />
Financial Cost:<br />
This claim was finally settled at<br />
US$608,500.<br />
Issue Date: 05/10/05<br />
Case No. 25685<br />
136 137
Personal Injury/Illness<br />
Reminder to Carry Out Frequent Risk Assessments,<br />
Especially on Routine Matters<br />
The Incident:<br />
This case involved an embarking passenger who<br />
slipped into a gap between <strong>the</strong> vessel’s starboard<br />
gangway and <strong>the</strong> ship.<br />
The passenger, who has difficulty walking/climbing<br />
steps due to his weight, started to board <strong>the</strong> vessel<br />
assisted by two crew members. At <strong>the</strong> top <strong>of</strong> <strong>the</strong><br />
steps <strong>the</strong> passenger paused for a few moments. As<br />
he continued he lost his balance whilst lifting his<br />
foot and he fell backwards into <strong>the</strong> gap between<br />
<strong>the</strong> steps and <strong>the</strong> vessel. The passenger’s leg was<br />
crushed. Due to <strong>the</strong> passenger’s weight <strong>the</strong> two<br />
crew members that were holding <strong>the</strong> passenger’s<br />
hands fell with him, one was injured. First aid was<br />
administered to <strong>the</strong> passenger and an ambulance<br />
was called. It was later learnt <strong>the</strong> passenger had a<br />
history <strong>of</strong> health, heart and leg problems.<br />
During <strong>the</strong> incident two ABs and <strong>the</strong> Chief Officer<br />
were present, advising and monitoring passenger<br />
embarkation. The sea was calm.<br />
The passenger had two operations to rectify <strong>the</strong><br />
crushed skin on <strong>the</strong> damaged leg.<br />
Observations:<br />
Plaintiff’s lawyers alleged <strong>the</strong> vessel’s employees<br />
were negligent in that <strong>the</strong>y failed to provide and<br />
ensure suitable and safe embarkation devices or aids<br />
and/or failed to control and secure <strong>the</strong> vessel during<br />
embarkation.<br />
As stated above three <strong>of</strong> <strong>the</strong> ship’s crew were<br />
present during <strong>the</strong> embarkation operation, ample<br />
safety notices were posted and company safety<br />
procedures were in place and being followed.<br />
This event highlights <strong>the</strong> importance <strong>of</strong> carrying<br />
out risk assessments in operational matters even if<br />
ample procedures are in place.<br />
Root Cause:<br />
Lack <strong>of</strong> passenger supervision.<br />
Financial Cost:<br />
The claim was settled at S$12,500.<br />
Issue Date: 01/06/06<br />
Case No. 47804<br />
138 139
Personal Injury/Illness<br />
Expect <strong>the</strong> Unexpected<br />
The Incident:<br />
This incident involved a 21 metre<br />
twin hulled passenger vessel<br />
engaged on a sightseeing voyage.<br />
The vessel was certified to carry<br />
240 passengers and at <strong>the</strong> time<br />
<strong>of</strong> <strong>the</strong> incident she had on board<br />
121 passengers.<br />
As <strong>the</strong> voyage progressed, <strong>the</strong><br />
wea<strong>the</strong>r conditions were fair to<br />
good with a moderate easterly<br />
wind with 0.5 metre waves on a<br />
1 to 2 metre swell.<br />
Approximately 15 passengers<br />
were standing on <strong>the</strong> foredeck.<br />
As <strong>the</strong> vessel turned into<br />
a bay, <strong>the</strong> Master made an<br />
announcement over <strong>the</strong><br />
public address system advising<br />
passengers that <strong>the</strong> seas may<br />
become “more choppy” and<br />
that <strong>the</strong>y should take care when<br />
moving about <strong>the</strong> ship. Shortly<br />
afterwards, a higher than normal<br />
wave was experienced and <strong>the</strong><br />
vessel rose and fell; this wave was<br />
followed by an even larger wave<br />
which caused <strong>the</strong> vessel’s bow<br />
to rise even higher than with <strong>the</strong><br />
previous wave and <strong>the</strong>n fall into<br />
<strong>the</strong> steep trough that followed.<br />
The effect <strong>of</strong> <strong>the</strong> vessel falling<br />
into <strong>the</strong> trough was to bodily lift a<br />
number <strong>of</strong> <strong>the</strong> passengers located<br />
on <strong>the</strong> fore deck and as <strong>the</strong> bow<br />
rose quickly on <strong>the</strong> next wave,<br />
<strong>the</strong> deck came up to meet <strong>the</strong> still<br />
falling passengers. As a result four<br />
passengers were seriously injured.<br />
Observations:<br />
The wave experienced could have been described as a rogue or freak wave, but <strong>the</strong><br />
following investigation concluded that <strong>the</strong> possibility <strong>of</strong> experiencing such a wave could<br />
have been expected in <strong>the</strong> area that was being navigated. (The generation <strong>of</strong> such waves<br />
is very complex and is caused by two or more wave trains, being deflected by islands in<br />
<strong>the</strong> vicinity, meeting which can cause a resultant wave with irregular heights).<br />
None <strong>of</strong> <strong>the</strong> passengers sitting within <strong>the</strong> accommodation were hurt and careful<br />
consideration must be given as to when to allow passengers out on to <strong>the</strong> foredeck. If<br />
such practice is restricted to periods <strong>of</strong> smooth waters or when <strong>the</strong> swells are low and<br />
even, <strong>the</strong> repetition <strong>of</strong> such an incident is unlikely.<br />
The authorities found that <strong>the</strong> Master and crew handled <strong>the</strong> post incident situation in a<br />
competent manner.<br />
The above case study is based on an investigation carried out by <strong>the</strong> Transport Accident<br />
Investigation Commission <strong>of</strong> New Zealand.<br />
Issue Date: 28/07/05<br />
Case No. 11234<br />
140 141
Personal Injury/Illness<br />
Good Record Keeping would have Reduced Claim<br />
The Incident:<br />
This accident happened to an elderly female passenger whilst<br />
disembarking from a tourist vessel operating <strong>of</strong>f <strong>the</strong> west coast <strong>of</strong><br />
Australia. As she was disembarking <strong>the</strong> passenger tripped, with <strong>the</strong><br />
result that she lost her balance and fell injuring her right knee on <strong>the</strong><br />
jetty. The passenger claimed that <strong>the</strong> principal cause <strong>of</strong> <strong>the</strong> accident was<br />
inadequate lighting.<br />
The first notice <strong>of</strong> a claim came in <strong>the</strong> form <strong>of</strong> a letter from a lawyer<br />
many months after <strong>the</strong> event. On investigation we found that no<br />
contemporary records <strong>of</strong> <strong>the</strong> incident existed. The deck log could not<br />
be found, <strong>the</strong>re was no accident report, nor was <strong>the</strong>re an entry in <strong>the</strong><br />
accident <strong>book</strong>. In addition during <strong>the</strong> intervening period <strong>the</strong>re had been<br />
staff changes, with <strong>the</strong> result that only one <strong>of</strong> <strong>the</strong> deck crew could be<br />
traced. From <strong>the</strong> evidence <strong>of</strong> this one witness we learnt that it was<br />
possible that <strong>the</strong> gangway was not in use at <strong>the</strong> time <strong>of</strong> this particular<br />
incident. Apparently it had been <strong>the</strong> practice <strong>of</strong> crew not to use <strong>the</strong><br />
gangway if <strong>the</strong> state <strong>of</strong> <strong>the</strong> tide brought <strong>the</strong> deck <strong>of</strong> <strong>the</strong> vessel level with<br />
<strong>the</strong> jetty. In those circumstances <strong>the</strong> passengers were simply assisted<br />
across <strong>the</strong> narrow gap.<br />
Observations:<br />
The biggest problem <strong>the</strong> Club encountered in dealing with this case<br />
was simply lack <strong>of</strong> information. In <strong>the</strong> words <strong>of</strong> <strong>the</strong> lawyers advising <strong>the</strong><br />
Club “in <strong>the</strong> light <strong>of</strong> .... your Member’s inability to refute <strong>the</strong> plaintiff’s<br />
version <strong>of</strong> <strong>the</strong> events, we are <strong>of</strong> <strong>the</strong> opinion that you would probably<br />
be found liable”.<br />
Root Cause:<br />
Inadequate access.<br />
Financial Cost:<br />
The claim was finally settled for US$13,000. However Members should<br />
note that <strong>the</strong> costs incurred simply trying to piece toge<strong>the</strong>r what had<br />
happened exceeded $5,000.<br />
Issue Date: 01/01/02<br />
Case No. 15003<br />
142 143
Personal Injury/Illness<br />
Good Record Keeping Prevents Claim<br />
The Incident:<br />
The owners <strong>of</strong> this vessel received a letter<br />
from lawyers representing an elderly lady who<br />
alleged that she had been injured when boarding<br />
<strong>the</strong> Member’s vessel 18 months previously. No<br />
incident had been recorded in <strong>the</strong> accident<br />
<strong>book</strong> on <strong>the</strong> day in question. The Master was<br />
interviewed and was quite emphatic that if an<br />
accident had occurred and <strong>the</strong> crew been aware<br />
<strong>of</strong> it, it would have been recorded. The o<strong>the</strong>r crew<br />
no longer worked for <strong>the</strong> company and two were<br />
known to have gone abroad. The remainder were<br />
traced but had no recollection <strong>of</strong> any accidents<br />
around <strong>the</strong> date in question.<br />
To board <strong>the</strong> vessel passengers simply stepped on<br />
to <strong>the</strong> deck. The gap between <strong>the</strong> vessel and <strong>the</strong><br />
dock varied between 2 and 10 cms. The claimant<br />
alleged that as she stepped across <strong>the</strong> boat moved<br />
away from <strong>the</strong> dock and her leg slipped between<br />
<strong>the</strong> vessel and <strong>the</strong> dock whereupon <strong>the</strong> boat moved<br />
back towards <strong>the</strong> dock, crushing her leg.<br />
An investigation <strong>of</strong> her medical history revealed that<br />
<strong>the</strong> lady had suffered from osteoarthritis for some<br />
time and had been treated for <strong>the</strong> problem by her<br />
general practitioner prior to <strong>the</strong> alleged incident.<br />
There was no mention <strong>of</strong> an accident in her medical<br />
records. Some seven months after <strong>the</strong> incident<br />
was alleged to have occurred she had arthroscopic<br />
surgery on her knee joint and later underwent<br />
fur<strong>the</strong>r surgery for a total knee replacement.<br />
Surgery however was not successful and she was left<br />
with a permanent disability. It was only <strong>the</strong>n that a<br />
claim was made against <strong>the</strong> vessel owner.<br />
Observations:<br />
This case is typical <strong>of</strong> many instances where<br />
claimants suffering from degenerative conditions<br />
try to link that condition to some ‘accident’ aboard<br />
a Member’s vessel in <strong>the</strong> hope <strong>of</strong> extorting large<br />
sums <strong>of</strong> money in ‘compensation’. These cases<br />
are <strong>of</strong>ten difficult to defend as first notice <strong>of</strong> <strong>the</strong><br />
problem <strong>of</strong>ten comes many months after <strong>the</strong><br />
alleged incident when it is difficult to identify <strong>the</strong><br />
crew on board at <strong>the</strong> time and when recollections<br />
are no longer fresh in <strong>the</strong> mind. It emphasises <strong>the</strong><br />
need to keep detailed records <strong>of</strong> crew and <strong>the</strong><br />
need to document every accident, however minor,<br />
to provide a body <strong>of</strong> evidence to demonstrate to<br />
a court that utmost care was taken and even <strong>the</strong><br />
most minor incidents were recorded. It is <strong>the</strong>n<br />
easier to convince a court that an unrecorded<br />
incident is unlikely to have taken place.<br />
Root Cause:<br />
Inadequate access arrangements.<br />
Financial Cost:<br />
This claim was settled at nuisance value however <strong>the</strong><br />
cost <strong>of</strong> lawyers, medical experts and investigation<br />
brought <strong>the</strong> total bill to over US$21,000.<br />
Issue Date: 01/01/02<br />
Case No. 15595<br />
144 145
Personal Injury/Illness<br />
Uncovered Hawse Pipe Leads to Expensive Passenger Trip<br />
The Incident:<br />
The vessel in question is a<br />
Mississippi type showboat<br />
steamer that carried out harbour<br />
cruises during which time<br />
passengers could enjoy meals<br />
and cabaret type entertainment.<br />
Passengers were actively<br />
encouraged to walk freely around<br />
<strong>the</strong> open decks, including <strong>the</strong><br />
fore and after decks, to enjoy <strong>the</strong><br />
views as <strong>the</strong> cruise proceeded.<br />
At approximately 21.15 on <strong>the</strong><br />
day in question, <strong>the</strong> attention<br />
<strong>of</strong> ship’s staff was drawn to <strong>the</strong><br />
fact one 57 year old female<br />
passenger had sustained injuries<br />
to her leg after falling in <strong>the</strong> bow<br />
region <strong>of</strong> <strong>the</strong> vessel. Initially <strong>the</strong><br />
injuries, although painful, were not<br />
considered severe enough to land<br />
<strong>the</strong> passenger immediately; in fact<br />
she expressed a wish to watch<br />
<strong>the</strong> evening’s entertainment. She<br />
was sent to hospital by taxi once<br />
<strong>the</strong> vessel returned to her berth<br />
later that evening.<br />
Initial medical opinion did not<br />
believe <strong>the</strong>re to be any fractures<br />
to her leg, but specialists later<br />
discovered she had in fact suffered<br />
a fracture behind her knee.<br />
Observations:<br />
Situated in <strong>the</strong> bow area <strong>of</strong> <strong>the</strong> vessel was <strong>the</strong><br />
windlass/winch arrangement and an associated<br />
hawse pipe which had not been provided with<br />
a cover (an oversight since building), leaving<br />
it exposed to all who passed by. It is not clear<br />
whe<strong>the</strong>r <strong>the</strong> fall was caused by <strong>the</strong> plaintiff stepping<br />
into <strong>the</strong> open pipe or catching her walking stick<br />
on it as she passed by. However <strong>the</strong> contributing<br />
factor to this incident is <strong>the</strong> fact <strong>the</strong> opening was<br />
not covered or fenced <strong>of</strong>f. Ano<strong>the</strong>r factor was<br />
considered to be <strong>the</strong> subdued lighting in <strong>the</strong> area<br />
with shadows masking <strong>the</strong> hazards.<br />
People who are unused to a marine environment<br />
may not appreciate dangers that are <strong>read</strong>ily<br />
apparent to a vessel’s crew. With this in mind, all<br />
areas to which passengers are permitted access<br />
must be regularly assessed for potential hazards<br />
and suitable precautions taken to prevent accidents,<br />
even if this means limiting access to non ship’s staff.<br />
Root Cause:<br />
Insufficient safety signs.<br />
Financial Cost:<br />
The case was settled at US$330,365.<br />
Issue Date: 01/01/02<br />
Case No. 23550<br />
146 147
Personal Injury/Illness<br />
Passenger Injury on Access Ramp<br />
The Incident:<br />
This incident arose on board a harbour ferry operating in smooth<br />
water. The harbour ferry was fitted with hydraulic ramps designed<br />
for <strong>the</strong> embarkation or disembarkation <strong>of</strong> passengers. The ramps had<br />
been lowered to enable passengers to board <strong>the</strong> vessel and having<br />
been positioned hydraulics were ‘locked’. Shortly after passengers<br />
started to board ano<strong>the</strong>r vessel backed into an adjacent wharf<br />
creating some wash. The combination <strong>of</strong> that wash and wave actions<br />
in <strong>the</strong> harbour caused <strong>the</strong> ferry to surge and roll. The movement<br />
resulted in <strong>the</strong> hydraulic ramp fitted to <strong>the</strong> ferry rising a few inches<br />
up <strong>of</strong>f <strong>the</strong> connecting hydraulic ramp fitted to <strong>the</strong> jetty. When <strong>the</strong><br />
vessel rolled back a passenger’s foot was trapped between <strong>the</strong><br />
ramps.<br />
Observations:<br />
Surprisingly <strong>the</strong> claimant’s lawyers did not argue<br />
that <strong>the</strong> ramp was unsafe because it did not hinge.<br />
Instead <strong>the</strong>y concentrated on <strong>the</strong> fact that <strong>the</strong><br />
wharfhand on duty had been preoccupied with tying<br />
up ano<strong>the</strong>r vessel when <strong>the</strong> accident occurred and<br />
that <strong>the</strong> ramp was unattended. Plaintiff’s lawyers<br />
alleged that had <strong>the</strong> crewman been at his place <strong>of</strong><br />
duty he could have warned passengers <strong>of</strong> <strong>the</strong> danger<br />
and prevented <strong>the</strong>m from boarding until it was safe<br />
to do so.<br />
While <strong>the</strong>re were considerable doubts about<br />
whe<strong>the</strong>r <strong>the</strong> presence <strong>of</strong> a company employee<br />
would have had any material effect on <strong>the</strong> incident,<br />
our lawyers advised that <strong>the</strong> simple fact that <strong>the</strong><br />
Member did not have an employee on <strong>the</strong> spot<br />
overseeing <strong>the</strong> boarding process would almost<br />
certainly have led <strong>the</strong> courts to <strong>the</strong> conclusion that<br />
our Member had not discharged <strong>the</strong>ir duty <strong>of</strong> care<br />
to <strong>the</strong> passenger. This illustrates <strong>the</strong> high standards<br />
that are expected from <strong>the</strong> operators <strong>of</strong> passenger<br />
vessels carrying <strong>the</strong> general public and <strong>the</strong> levels <strong>of</strong><br />
care which <strong>the</strong>y are expected to maintain.<br />
Root Cause:<br />
Inadequate access.<br />
Financial Cost:<br />
This claim was settled within <strong>the</strong> Member’s<br />
deductible.<br />
Issue Date: 01/01/02<br />
Case No. 23590<br />
148 149
Personal Injury/Illness<br />
Passenger Dies <strong>of</strong> Heat Attack Despite<br />
Determined Effort by Crew to Save Him.<br />
The Incident:<br />
The incident occurred on board a tourist vessel<br />
ferrying passengers out to a resort pontoon<br />
on <strong>the</strong> Great Barrier Reef. Although wea<strong>the</strong>r<br />
conditions were moderate a passenger succumbed<br />
to seasickness during <strong>the</strong> voyage. On arrival at <strong>the</strong><br />
pontoon most passengers <strong>the</strong>n boarded a glass<br />
bottom boat to view <strong>the</strong> flora and fauna on <strong>the</strong><br />
reef but <strong>the</strong> sick passenger and his wife remained<br />
on <strong>the</strong> pontoon. The crew provided a cabin for <strong>the</strong><br />
gentleman so that he could lie down. Some minutes<br />
later his wife called for assistance as her husband was<br />
having chest pains. The passenger had a history <strong>of</strong><br />
heart problems and it was clear that he was having<br />
a heart attack. The passenger carried medication<br />
for his condition which <strong>the</strong> crew supplemented with<br />
oxygen. The passenger was placed in a semi-sitting<br />
position with his legs elevated to reduce <strong>the</strong> strain<br />
on his heart. The Captain contacted his head <strong>of</strong>fice<br />
to arrange to evacuate <strong>the</strong> passenger. The head<br />
<strong>of</strong>fice were unable to locate a seaplane but were<br />
able to find a helicopter although that could not get<br />
to <strong>the</strong> ship for over two hours. The <strong>of</strong>fice called a<br />
doctor to <strong>the</strong> radio so that <strong>the</strong> Captain could obtain<br />
medical advice.<br />
Initially <strong>the</strong> passenger responded well to treatment<br />
but shortly after 1 p.m. <strong>the</strong> passenger stopped<br />
breathing. The ship’s crew was swiftly to organise<br />
resuscitation. Their efforts were supplemented by a<br />
registered nurse and an anaes<strong>the</strong>tist from amongst<br />
<strong>the</strong> passengers. The crew’s efforts to revive <strong>the</strong><br />
passenger continued until <strong>the</strong> helicopter containing<br />
a doctor and paramedic arrived and took over.<br />
Although <strong>the</strong> attempts to resuscitate <strong>the</strong> passenger<br />
continued for a fur<strong>the</strong>r hour <strong>the</strong>y were not successful.<br />
Observations:<br />
Although on this occasion <strong>the</strong> crew’s efforts did not save <strong>the</strong> passenger’s life, <strong>the</strong>y did<br />
everything possible for him. In addition in <strong>the</strong> heat <strong>of</strong> <strong>the</strong> crisis <strong>the</strong>y still found time to<br />
look after his wife and attend to her needs, comfort her during <strong>the</strong> ordeal and keep her<br />
fully informed <strong>of</strong> what was happening and <strong>the</strong> efforts being made to save her husband.<br />
The passenger’s wife later wrote to <strong>the</strong> company praising <strong>the</strong> efforts <strong>of</strong> all on board and<br />
commending <strong>the</strong>m for <strong>the</strong>ir efforts and support.<br />
This incident illustrates <strong>the</strong> benefits <strong>of</strong> maintaining good communication between <strong>the</strong><br />
crew and <strong>the</strong> friends and relatives <strong>of</strong> a sick or injured passenger. It is essential to keep<br />
friends and relatives fully advised <strong>of</strong> all developments and <strong>the</strong> action being taken to help<br />
<strong>the</strong> passenger. Bad communication can increase<br />
anxiety and create distrust, leaving friends and<br />
relatives feeling that <strong>the</strong> ship’s staff could or should<br />
be doing more, which could in <strong>the</strong> future lead to<br />
acrimony and litigation.<br />
Issue Date: 01/01/02<br />
Case No. 25478<br />
150 151
Personal Injury/Illness<br />
Explosion in Battery Locker<br />
The Incident:<br />
The vessel involved in this<br />
incident was a purpose-designed<br />
sail training vessel built in 1991.<br />
The vessel carried a substantial<br />
bank <strong>of</strong> lead acid batteries to<br />
power emergency systems, radios<br />
and fire detection systems. The<br />
batteries were housed in a locker<br />
on <strong>the</strong> port side <strong>of</strong> <strong>the</strong> main deck<br />
below <strong>the</strong> wheelhouse.<br />
In addition to a permanent crew<br />
<strong>the</strong> vessel carried 31 students<br />
who, in addition to pursuing<br />
academic studies, assisted in <strong>the</strong><br />
sailing and maintenance <strong>of</strong> <strong>the</strong><br />
vessel. On <strong>the</strong> morning <strong>of</strong> <strong>the</strong><br />
incident a party <strong>of</strong> students had<br />
been assigned <strong>the</strong> task <strong>of</strong> scaling<br />
and painting <strong>the</strong> port side <strong>of</strong> <strong>the</strong><br />
deck house. During <strong>the</strong> work<br />
an explosion occurred in <strong>the</strong><br />
battery locker. The blast threw<br />
one student overboard. Despite<br />
an extensive air and sea search he<br />
was never recovered.<br />
Observations:<br />
The student who died had been removing rust accumulations from<br />
around <strong>the</strong> battery locker door with a rotary grinding machine. The<br />
battery locker door was secured by four lugs and wing nuts. In order<br />
to grind <strong>of</strong>f rust around <strong>the</strong> lugs <strong>the</strong> student loosened <strong>the</strong> wing nuts<br />
and lifted <strong>the</strong>m clear <strong>of</strong> <strong>the</strong> lugs. Sparks from <strong>the</strong> grinding machine<br />
entered <strong>the</strong> locker and ignited an accumulation <strong>of</strong> hydrogen gas causing<br />
<strong>the</strong> explosion.<br />
The battery locker door was marked with <strong>the</strong> word ‘batteries’ in large<br />
red letters. Signs were fitted inside <strong>the</strong> locker to alert personnel to<br />
<strong>the</strong> presence <strong>of</strong> corrosive acid and <strong>the</strong> dangers <strong>of</strong> corrosive acid burns.<br />
There were no external warning signs prohibiting naked lights and<br />
smoking, nor was <strong>the</strong>re any warning <strong>of</strong> <strong>the</strong> explosive risk.<br />
Subsequent investigations revealed that <strong>the</strong> locker’s ventilation<br />
arrangements consisted <strong>of</strong> a single 20 mm diameter vent pipe which<br />
made no provisions for through ventilation. This was inadequate to<br />
dissipate <strong>the</strong> quantity <strong>of</strong> hydrogen gas given <strong>of</strong>f at high charge rates.<br />
Root Cause:<br />
Unsafe wing practices.<br />
Issue Date: 01/01/02<br />
Case No. 26355<br />
152 153
Personal Injury/Illness<br />
Hasty Exit Brings Slide <strong>of</strong> Despair<br />
The Incident:<br />
In this case a passenger fell <strong>of</strong>f his motorbike whilst<br />
disembarking from a ferry via <strong>the</strong> vessel’s ramp.<br />
The accident occurred as <strong>the</strong> front tyre made<br />
contact with <strong>the</strong> ramp. This resulted in <strong>the</strong> bike<br />
sliding from under <strong>the</strong> claimant.<br />
The passenger sustained an injury to his right hand<br />
and <strong>the</strong> motorbike sustained damage to <strong>the</strong> body<br />
work on <strong>the</strong> upper and lower right hand side. The<br />
rear bike pedal was also snapped <strong>of</strong>f.<br />
Observations:<br />
It is alleged that <strong>the</strong> accident occurred due to<br />
<strong>the</strong> combination <strong>of</strong> <strong>the</strong> highly polished surface <strong>of</strong><br />
<strong>the</strong> aluminium ramp, which was wet due to <strong>the</strong><br />
prevailing wea<strong>the</strong>r, and <strong>the</strong> motorbike’s speed.<br />
It is recommended that an anti-slip paint or o<strong>the</strong>r<br />
means, e.g. raised t<strong>read</strong>s, be applied to ramps and<br />
o<strong>the</strong>r passenger access areas as a preventative<br />
measure.<br />
Speed restriction signs should be displayed in<br />
prominent positions.<br />
Root Cause:<br />
Inadequate speed restrictions.<br />
Financial Cost:<br />
US$2,333.39<br />
Issue Date: 01/01/02<br />
Case No. 49748<br />
154 155
Personal Injury/Illness<br />
Passenger Impatience Leads to Injury<br />
The Incident:<br />
This incident concerns a serious injury suffered by<br />
a middle aged male passenger while disembarking<br />
from a harbour ferry. The passenger was a<br />
construction worker who had used <strong>the</strong> ferry service<br />
for several weeks before <strong>the</strong> incident to travel to<br />
and from work.<br />
During <strong>the</strong> crossing he occupied a seat near <strong>the</strong><br />
bows <strong>of</strong> <strong>the</strong> ferry on <strong>the</strong> lower deck. As <strong>the</strong> vessel<br />
approached its berth an announcement was made<br />
to passengers asking <strong>the</strong>m to remain seated until<br />
<strong>the</strong> ferry had ber<strong>the</strong>d and <strong>the</strong> gangway had been<br />
lowered. Despite this <strong>the</strong> passenger, along with<br />
many o<strong>the</strong>rs, left his seat to join a mass <strong>of</strong> people<br />
eager to disembark at <strong>the</strong> earliest moment. As <strong>the</strong><br />
vessel came alongside <strong>the</strong> man somehow came to<br />
fall between <strong>the</strong> vessel and <strong>the</strong> dock suffering severe<br />
crush injuries to his pelvis. The exact cause <strong>of</strong> his fall<br />
has never been adequately explained however <strong>the</strong>re<br />
has been speculation that <strong>the</strong> passenger had ei<strong>the</strong>r<br />
tried to disembark by an unorthodox manner or<br />
had somehow been pushed over <strong>the</strong> bulwark by <strong>the</strong><br />
pressure <strong>of</strong> <strong>the</strong> crowd.<br />
Observations:<br />
The ferry ber<strong>the</strong>d at a purposedesigned<br />
terminal. It was<br />
equipped with permanent<br />
gangways, which are hinged<br />
at deck level and lowered<br />
like a drawbridge onto <strong>the</strong><br />
dock, which was level with <strong>the</strong><br />
deck. There is solid bulwark<br />
extending to deckhead level<br />
for over two meters ei<strong>the</strong>r side<br />
<strong>of</strong> <strong>the</strong> gangway. Beyond that<br />
<strong>the</strong>re is a conventional solid<br />
bulwark to waist height which is<br />
supplemented by an additional rail<br />
approximately 30cm above <strong>the</strong><br />
bulwark cap in all areas except<br />
adjacent to mooring bits.<br />
Prior to docking <strong>the</strong> crew<br />
routinely make an announcement<br />
warning passengers to remain<br />
seated and <strong>the</strong> passenger decks<br />
are liberally supplied with<br />
multilingual notices to that effect.<br />
The passenger sued claiming<br />
substantial damages alleging that<br />
<strong>the</strong> owners failed to erect railings<br />
in <strong>the</strong> region <strong>of</strong> <strong>the</strong> mooring<br />
bulwarks to prevent passengers<br />
falling <strong>of</strong>f <strong>the</strong> ferry and that <strong>the</strong><br />
owner failed to take appropriate<br />
steps to ensure that passengers<br />
remain seated while <strong>the</strong> ferry<br />
was in motion. The court in Hong<br />
Kong gave judgement on case in<br />
November 2000. Judge Seagroaat<br />
found that <strong>the</strong> bulwarks near<br />
<strong>the</strong> mooring bits where <strong>the</strong>re<br />
are no additional railings was<br />
high enough to protect <strong>the</strong><br />
passengers disembarking properly<br />
at <strong>the</strong> appropriate time. More<br />
importantly however, <strong>the</strong><br />
Judge carefully considered <strong>the</strong><br />
duties and obligations on vessel<br />
owners on crowd control. In<br />
his judgement, Judge Seagroaat<br />
commented that passengers who<br />
leave <strong>the</strong>ir seats despite oral and<br />
written warnings to <strong>the</strong> contrary<br />
know, as any reasonable person<br />
knows, that <strong>the</strong> reason for such<br />
warnings or advice is that <strong>the</strong>re is<br />
always a risk <strong>of</strong> sudden movement<br />
<strong>of</strong> <strong>the</strong> ferry or <strong>of</strong> it hitting <strong>the</strong><br />
pontoon with some force <strong>the</strong>reby<br />
causing passengers to loose <strong>the</strong>ir<br />
balance and fall. Anyone who<br />
ignores such warnings does so at<br />
his or her own risk.<br />
The Judge went on to say that<br />
he did not think <strong>the</strong> defendants<br />
could do anything to deter such<br />
action o<strong>the</strong>r than by announced<br />
and visible warnings. He did<br />
not consider it practicable or<br />
reasonable to require <strong>the</strong> size<br />
<strong>of</strong> <strong>the</strong> crew to be increased to<br />
such proportions as to be able to<br />
physically restrain adult persons<br />
hellbent on early disembarkation.<br />
Consequently he found <strong>the</strong> ferry<br />
operators were not liable for <strong>the</strong><br />
passenger’s injuries.<br />
Root Cause:<br />
Inadequate access.<br />
Issue Date: 01/01/02 Case No.<br />
28627<br />
156 157
Personal Injury/Illness<br />
Certainly not a toast to good health<br />
The Incident:<br />
A steward onboard <strong>the</strong> vessel, washing <strong>the</strong> dishes as usual, poured<br />
some concentrated industrial detergent into an empty green mineral<br />
water bottle, to assist in measuring <strong>the</strong> correct quantity to be put into<br />
<strong>the</strong> dishwashing machine. The partly filled drinking water bottle was<br />
<strong>the</strong>n placed without any label indicating <strong>the</strong> contents with cleaning<br />
chemicals, near <strong>the</strong> galley sink.<br />
The next day, <strong>the</strong> unlabelled mineral water bottle, partly filled with<br />
detergent was put in <strong>the</strong> refrigerator, obviously being mistaken<br />
for drinking water. Subsequently it was placed on <strong>the</strong> lunch table.<br />
Unfortunately <strong>the</strong> liquid was odourless and <strong>the</strong> unsuspecting seaman<br />
poured it into a glass and took a few quick sips. He immediately<br />
became aware <strong>of</strong> an acute burning sensation in his mouth and<br />
throat. Fortunately, <strong>the</strong> yacht was in port and he was sent ashore<br />
to <strong>the</strong> local clinic, however it was not equipped to handle such<br />
serious cases and <strong>the</strong> seaman had to be transported to a hospital<br />
in a nearby larger town. By <strong>the</strong>n, he was suffering from breathing<br />
problems, had a swollen tongue and a purple face. The hospital<br />
managed to administer suitable treatment and confirmed that <strong>the</strong><br />
seaman had suffered internal burns. His permanent disability was<br />
assessed at 7% and as a result <strong>of</strong> his injuries, he will suffer from a<br />
bitonal voice and slow digestion.<br />
Observations:<br />
The use <strong>of</strong> a drinking water bottle for handling<br />
chemicals and also its careless stowage without any<br />
warning labels was <strong>the</strong> root cause <strong>of</strong> <strong>the</strong> incident.<br />
Fur<strong>the</strong>rmore, its storage within an area (<strong>the</strong> galley)<br />
where it was easily mistaken for drinking water was<br />
ano<strong>the</strong>r major contributing factor. Chemicals should<br />
only be stored in containers specifically designated<br />
and adequately marked for <strong>the</strong> purpose. They should<br />
not be handled in any containers that can be easily<br />
mistaken for anything else. Only <strong>the</strong> required quantity<br />
should be used and <strong>the</strong> remaining quantity, if possible,<br />
must be returned to its storage container. The mixing<br />
containers should be cleaned appropriately and<br />
stowed back in <strong>the</strong>ir designated place..<br />
Financial Cost:<br />
The total cost <strong>of</strong> this claim was USD 69,000<br />
Trading Area:<br />
Europe<br />
Issue Date: 16/03/10<br />
Case No. 56506<br />
158 159
Navigation<br />
Familiarity Breeding Contempt<br />
The Incident:<br />
This case involved two high speed passenger ferries<br />
owned and operated by <strong>the</strong> same company, which<br />
collided in reduced visibility.<br />
During <strong>the</strong> course <strong>of</strong> <strong>the</strong> early morning, both vessels<br />
had successfully carried out a number <strong>of</strong> runs<br />
between <strong>the</strong>ir designated ports. One vessel <strong>the</strong>n<br />
commenced a scheduled new run that involved a<br />
reciprocal course to <strong>the</strong> o<strong>the</strong>r vessel in a relatively<br />
narrow channel. Both Masters were aware that <strong>the</strong><br />
prevailing fog patches were reducing <strong>the</strong> visibility to<br />
50 metres or less.<br />
At <strong>the</strong> time <strong>of</strong> entering <strong>the</strong> same fog patch, <strong>the</strong><br />
Masters each detected <strong>the</strong> o<strong>the</strong>r vessel on radar. Over<br />
<strong>the</strong> VHF, one Master requested a “green to green”<br />
passing but <strong>the</strong> o<strong>the</strong>r Master declined requesting “red<br />
to red” and at <strong>the</strong> same time put his helm to hard a<br />
starboard and reduced engine revolutions.<br />
Shortly <strong>the</strong>reafter <strong>the</strong> vessels collided. Fortunately,<br />
<strong>of</strong> <strong>the</strong> combined total <strong>of</strong> 127 passengers and 7 crew<br />
<strong>the</strong>re were no injuries.<br />
Observations:<br />
The principal factors causing <strong>the</strong> collision were <strong>the</strong><br />
excessive speeds <strong>of</strong> both vessels and <strong>the</strong> short radar<br />
ranges utilised by <strong>the</strong> Masters immediately prior to<br />
<strong>the</strong> collision. Investigations showed that <strong>the</strong> vessels<br />
had a combined closing speed <strong>of</strong> 36 knots yet both<br />
radars were set on <strong>the</strong> 0.75n.m. range. This resulted<br />
in <strong>the</strong> maximum duration <strong>of</strong> 75 seconds from <strong>the</strong><br />
time <strong>the</strong> echo appeared at <strong>the</strong> edge <strong>of</strong> <strong>the</strong> screen<br />
to <strong>the</strong> time <strong>of</strong> impact. There were a number <strong>of</strong><br />
additional contributory factors including a failure<br />
to comply with <strong>the</strong> Rules for <strong>the</strong> Prevention <strong>of</strong><br />
Collisions at Sea, a failure to follow <strong>the</strong> company’s<br />
own procedures and <strong>the</strong> lack <strong>of</strong> a suitably qualified<br />
lookout on ei<strong>the</strong>r vessel.<br />
The speed <strong>of</strong> both vessels was excessive for <strong>the</strong><br />
conditions and <strong>the</strong> basic principle <strong>of</strong> frequently<br />
scanning greater radar ranges in order to permit <strong>the</strong><br />
early detection <strong>of</strong> o<strong>the</strong>r vessels in restricted visibility<br />
was not followed. The manning scales on board<br />
both vessels meant that <strong>the</strong> Masters were <strong>the</strong> only<br />
suitably qualified mariners on board, thus placing<br />
a great burden on both men at times <strong>of</strong> reduced<br />
visibility. The company had in place procedures<br />
and recommendations for courses to be followed,<br />
specifically designed to prevent end on situations<br />
and <strong>the</strong>se were not adhered to.<br />
Root Cause:<br />
Failure to comply with collision regulations.<br />
Issue Date: 01/01/02<br />
Case No. 39495<br />
160 161
Navigation<br />
If Only <strong>the</strong>y had Tried Something Different<br />
The Incident:<br />
A passenger vessel with 26 passengers and 12 crew<br />
on board ran aground in unsurveyed waters. At<br />
<strong>the</strong> time <strong>of</strong> <strong>the</strong> grounding <strong>the</strong> Master was alone<br />
on <strong>the</strong> bridge and <strong>the</strong> vessel was in automatic<br />
navigation mode. In this mode, course adjustments<br />
were initiated by a GPS linked to an electronic<br />
chart system which transmitted course alteration<br />
information to <strong>the</strong> auto pilot.<br />
A number <strong>of</strong> passengers received minor injuries as<br />
a result <strong>of</strong> <strong>the</strong> initial impact.<br />
Observations:<br />
The investigation deemed that <strong>the</strong> most likely<br />
cause <strong>of</strong> this incident was a discrepancy between<br />
<strong>the</strong> vessel’s true position and that determined by<br />
<strong>the</strong> GPS. Because total reliance was placed on<br />
<strong>the</strong> GPS with no o<strong>the</strong>r means used to verify <strong>the</strong><br />
vessel’s position, <strong>the</strong> discrepancy went unnoticed.<br />
In addition, it was clear that with <strong>the</strong> Master being<br />
alone on <strong>the</strong> bridge, a proper lookout could not<br />
be kept and this is all <strong>the</strong> more pertinent as <strong>the</strong><br />
vessel was navigating in uncharted waters. The<br />
investigation also raised concerns over <strong>the</strong> fatigue<br />
<strong>the</strong> Master may have been suffering, brought on by<br />
his intensive work routine.<br />
O<strong>the</strong>r navigational irregularities were highlighted<br />
including <strong>the</strong> fact <strong>the</strong> electronic chart system in use<br />
was not approved, in that <strong>the</strong> computer was not<br />
dedicated to <strong>the</strong> vessel’s navigation system but was<br />
also used for <strong>the</strong> ship’s administration.<br />
This case study is based on <strong>the</strong> investigation report<br />
prepared by <strong>the</strong> Australian Transport Safety Bureau.<br />
Root Cause:<br />
Incorrect navigational procedures.<br />
Issue Date: 31/08/05<br />
Case No. 12345<br />
This incident shows that no matter how<br />
technologically advanced a vessel’s navigation<br />
system is, <strong>the</strong>re is no substitute for good old<br />
fashioned seamanship!<br />
162 163
Navigation<br />
Paperwork Leads to Grounding<br />
The Incident:<br />
This incident occurred on <strong>the</strong> inland waterways <strong>of</strong> sou<strong>the</strong>rn Australia. A passenger<br />
excursion vessel on a river passage collided with <strong>the</strong> river bank in good conditions and<br />
broad daylight. Fortunately little damage was done and passenger injuries were limited to<br />
a few cuts and bruises.<br />
Subsequent investigation revealed that <strong>the</strong> Mate was not paying attention to his duties.<br />
He was trying to catch up with his paperwork and was not looking where he was going.<br />
Observations:<br />
In recent years ever-increasing amounts <strong>of</strong> legislation<br />
have increased <strong>the</strong> administrative workload on<br />
board ship. Ships’ <strong>of</strong>ficers are spending increasing<br />
amounts <strong>of</strong> time on paperwork. Owners must<br />
however ensure that <strong>the</strong>ir <strong>of</strong>ficers’ attention is not<br />
distracted from <strong>the</strong>ir principal responsibilities in<br />
relation to <strong>the</strong> safe navigation <strong>of</strong> <strong>the</strong> ship and safety<br />
<strong>of</strong> life on board. Duties should be arranged so that<br />
adequate time is allowed for <strong>the</strong> completion <strong>of</strong><br />
paperwork in a manner that will not interfere with<br />
an <strong>of</strong>ficer’s primary responsibilities.<br />
Root Cause:<br />
Failure to perform correct lookout.<br />
Financial Cost:<br />
Although no claims arose from this occurrence<br />
<strong>the</strong> costs for a precautionary investigation to<br />
protect <strong>the</strong> owners from potential injury claims<br />
from passengers and any possible inquiry by <strong>the</strong><br />
regulatory authorities exceeded US$5,000.<br />
Issue Date: 01/01/02<br />
Case No. 24492<br />
164 165
Navigation<br />
Collision Alongside<br />
The Incident:<br />
The claim involved three passenger<br />
vessels, two <strong>of</strong> which collided,<br />
whilst performing unberthing/<br />
berthing operations in a river.<br />
Two <strong>of</strong> <strong>the</strong> vessels were ber<strong>the</strong>d<br />
alongside a quay. To allow <strong>the</strong><br />
inner vessel, with passengers on<br />
board, to sail <strong>the</strong> outer vessel<br />
manoeuvred “crabways” to<br />
starboard. When <strong>the</strong> route was<br />
clear <strong>the</strong> inner vessel sailed.<br />
During this time <strong>the</strong> third vessel<br />
was approaching <strong>the</strong> same quay<br />
from astern <strong>of</strong> <strong>the</strong> o<strong>the</strong>r two<br />
vessels. The outer vessel began<br />
to return to <strong>the</strong> berth by moving<br />
“crabways” to port and did not<br />
observe <strong>the</strong> closing third vessel.<br />
A collision occurred between<br />
<strong>the</strong> second vessel on its port aft<br />
corner and <strong>the</strong> third vessel on its<br />
starboard fore corner.<br />
Minor bruises were noted on<br />
some <strong>of</strong> <strong>the</strong> passengers on <strong>the</strong><br />
third vessel and damage occurred<br />
to <strong>the</strong> second vessel.<br />
Observations:<br />
• The approaching vessel assumed both vessels ahead were<br />
clearing <strong>the</strong> berth but never made contact to confirm<br />
• Nei<strong>the</strong>r vessel made any effort to ascertain <strong>the</strong><br />
actions <strong>of</strong> <strong>the</strong> o<strong>the</strong>r vessels in <strong>the</strong> vicinity<br />
• Complacency on <strong>the</strong> part <strong>of</strong> <strong>the</strong> vessel returning to <strong>the</strong> berth<br />
• No effective port control<br />
This claim reiterates <strong>the</strong> importance <strong>of</strong> keeping an efficient look out at all times, especially<br />
whilst performing manoeuvres in close proximity to fixed and floating objects. If in doubt<br />
contact should be made with <strong>the</strong> o<strong>the</strong>r vessels to confirm <strong>the</strong>ir intentions.<br />
Root Cause:<br />
Insufficient communication.<br />
Financial Cost:<br />
Approximately €35,000.<br />
Issue Date: 11/04/07<br />
Case No. 46260<br />
166 167
Navigation<br />
Intermittent Main Engine Fault Leads to Dock Damage<br />
The Incident:<br />
This incident occurred when a harbour ferry failed to respond to <strong>the</strong><br />
main engine controls with <strong>the</strong> result that she collided with <strong>the</strong> dock.<br />
The ferry had been approaching <strong>the</strong> berth at slow speed when <strong>the</strong><br />
Master tried to engage astern power. At this point he lost bridge<br />
control <strong>of</strong> <strong>the</strong> main engines with <strong>the</strong> result that <strong>the</strong> vessel continued<br />
forward, colliding with <strong>the</strong> piles at <strong>the</strong> end <strong>of</strong> <strong>the</strong> jetty.<br />
Observations:<br />
Investigation into <strong>the</strong> accident revealed that a similar problem had<br />
been encountered by <strong>the</strong> Master <strong>of</strong> <strong>the</strong> vessel during <strong>the</strong> previous<br />
shift. On that occasion power had been restored by jiggling <strong>the</strong> key<br />
in <strong>the</strong> engine control selector switch panel. Apart from completing a<br />
defects report no fur<strong>the</strong>r investigation or repair work was undertaken.<br />
The vessel remained in passenger service and no special precautions<br />
were taken during <strong>the</strong> berthing operation to minimise <strong>the</strong> risk from<br />
sudden control failure. After <strong>the</strong> accident <strong>the</strong> control switches were<br />
replaced. Had <strong>the</strong> problem been properly investigated immediately<br />
and appropriate corrective action taken, this accident need not have<br />
occurred. In this case <strong>the</strong> two Captains would have benefited from<br />
clear guidelines on removing <strong>the</strong> vessel from service.<br />
Root Cause:<br />
Insufficient maintenance system.<br />
Financial Cost:<br />
The cost <strong>of</strong> repairs to <strong>the</strong> dock exceeded US$15,000.<br />
Issue Date: 01/01/02<br />
Case No. 22685<br />
168 169
Section 5<br />
Offshore Vessels<br />
171
Offshore Vessels<br />
Personal Injury/Illness<br />
A Scenic View but a Dangerous Place to Stand<br />
The Incident:<br />
The Member’s tug was standing by an anchored<br />
dumb barge which was being loaded with sawn<br />
timber. The tug Master noted that in <strong>the</strong> rough sea<br />
conditions, <strong>the</strong> barge was dragging her anchor and<br />
starting to drift towards shallow water. The decision<br />
was made to tow <strong>the</strong> barge back out to clear water.<br />
The Chief Officer and Chief Engineer were<br />
instructed to pass <strong>the</strong> tow line to <strong>the</strong> barge, but in<br />
<strong>the</strong> wea<strong>the</strong>r conditions <strong>the</strong>y experienced difficulty.<br />
The cook was observing <strong>the</strong> operation and,<br />
characteristically, <strong>of</strong>fered his assistance. With <strong>the</strong><br />
cook’s help <strong>the</strong> line was successfully made fast. The<br />
Master <strong>the</strong>n took <strong>the</strong> strain on <strong>the</strong> tow line. The<br />
configuration <strong>of</strong> <strong>the</strong> tug, tow line and barge was such<br />
that <strong>the</strong> line was in contact with <strong>the</strong> tug’s towing<br />
pins. As <strong>the</strong> strain on <strong>the</strong> tow line was increased, <strong>the</strong><br />
towing pin failed and <strong>the</strong> tow line struck <strong>the</strong> cook<br />
who was standing in close proximity. The force <strong>of</strong><br />
<strong>the</strong> blow threw him overboard and his body was<br />
never recovered.<br />
Observations:<br />
This fatality arose because <strong>the</strong><br />
cook was standing in entirely <strong>the</strong><br />
wrong place when <strong>the</strong> strain was<br />
being taken up on <strong>the</strong> tow line.<br />
From <strong>the</strong> diagram it can be seen<br />
that <strong>the</strong> o<strong>the</strong>r two crew members<br />
were safely standing clear and<br />
were never in any danger.<br />
The investigation into this incident<br />
did not determine <strong>the</strong> events or<br />
signals that were made between<br />
<strong>the</strong> Chief Officer and <strong>the</strong><br />
Master once <strong>the</strong> tow had been<br />
successfully made fast, however it<br />
is abundantly clear that <strong>the</strong> cook<br />
was allowed to place himself in<br />
danger. The Chief Officer should<br />
not have given <strong>the</strong> all fast signal<br />
to <strong>the</strong> Master until all crew had<br />
cleared <strong>the</strong> danger area.<br />
Whilst <strong>the</strong> cook’s voluntary<br />
efforts in his willingness to<br />
assist his fellow crew mates are<br />
commendable, this incident<br />
shows how naivety can have<br />
disastrous consequences.<br />
Catering and engineering staff are<br />
not necessarily natural seamen<br />
and do not always appreciate<br />
<strong>the</strong> dangers that tow lines pose,<br />
nor <strong>the</strong> destruction that can take<br />
place when a line under strain<br />
fails through whatever cause. It<br />
would appear that in this case no<br />
guidance at all was given to <strong>the</strong><br />
cook – if it was and ignored <strong>the</strong>n<br />
a formal order should have been<br />
given and towing not commenced<br />
until everyone was standing clear<br />
and <strong>the</strong>reafter kept clear until<br />
operations were over.<br />
Root Cause:<br />
Poor operational practice.<br />
Issue Date: 31/10/05<br />
Case No. 47261<br />
172 173
Personal Injury/Illness<br />
Short Cuts do not Always Result in a Quick Job<br />
The Incident:<br />
This incident resulted in <strong>the</strong><br />
death <strong>of</strong> a seaman whilst securing<br />
a container on deck.<br />
A single 20 foot container<br />
weighing about 10 tonnes had<br />
been loaded onto <strong>the</strong> deck <strong>of</strong><br />
an Anchor Handling Tug.<br />
The crew were engaged in<br />
securing <strong>the</strong> container by means<br />
<strong>of</strong> a 3 inch polypropylene<br />
mooring rope which was secured<br />
at one end and <strong>the</strong>n led around<br />
<strong>the</strong> container. The loose end was<br />
placed on <strong>the</strong> drum end <strong>of</strong> an<br />
anchor handling winch and <strong>the</strong><br />
slack was being taken up.<br />
The rope parted and struck<br />
<strong>the</strong> victim in <strong>the</strong> face. He<br />
was immediately evacuated<br />
to hospital. Never regaining<br />
consciousness he died fifteen<br />
days later.<br />
Observations:<br />
Investigations showed <strong>the</strong> rope to be old and in a<br />
poor condition brought about by its age, heat and<br />
exposure to sunlight. The conclusion drawn was that<br />
<strong>the</strong> rope was severed as it passed over <strong>the</strong> sharp<br />
edge <strong>of</strong> <strong>the</strong> container. The victim was positioned<br />
by <strong>the</strong> warping drum obscured from <strong>the</strong> winch<br />
operator’s view.<br />
The method used to secure <strong>the</strong> container was<br />
inefficient and inherently dangerous. The vessel<br />
was fitted with more than an adequate number <strong>of</strong><br />
dedicated securing rings and fixing points which<br />
would have enabled a correct method <strong>of</strong> securing to<br />
have been used.<br />
This incident highlights <strong>the</strong> dangers <strong>of</strong> taking shortcuts,<br />
poor work practices and <strong>the</strong> use <strong>of</strong> old rope.<br />
Root Cause:<br />
Poor working practices.<br />
Financial Cost:<br />
The cost <strong>of</strong> <strong>the</strong> claim was US$33,000.<br />
Issue Date: 25/08/03<br />
Case No. 36103<br />
174 175
Personal Injury/Illness<br />
Prevention is Necessary as <strong>the</strong>re is No Cure<br />
The Incident:<br />
A tug belonging to one <strong>of</strong> <strong>the</strong><br />
Club’s Members was stationed<br />
<strong>of</strong>f Point Noire Congo when<br />
one <strong>of</strong> <strong>the</strong> crew took seriously ill<br />
one evening. He was transferred<br />
to a nearby rig and, after<br />
assessment by a doctor, was<br />
transferred ashore to hospital<br />
where he later died. The<br />
diagnosis was a severe strain <strong>of</strong><br />
cerebral malaria.<br />
On passage to <strong>the</strong> next port,<br />
ano<strong>the</strong>r crew member was taken<br />
ill with a mild strain <strong>of</strong> malaria and<br />
was repatriated.<br />
A few days later, <strong>the</strong> Master took<br />
ill and <strong>the</strong> vessel was diverted to<br />
<strong>the</strong> nearest port but unfortunately<br />
he died before medical assistance<br />
could be arranged. His death was<br />
caused by malaria.<br />
The families <strong>of</strong> <strong>the</strong> deceased took<br />
legal action against <strong>the</strong> Members<br />
for failing to provide adequate antimalarial<br />
protection for <strong>the</strong> crew.<br />
Observations:<br />
An expert in tropical medications examined this case and confirmed that<br />
<strong>the</strong> Members had not taken appropriate measures to ensure <strong>the</strong> health<br />
and safety <strong>of</strong> <strong>the</strong> crew. The anti-malarial medicine made available was<br />
<strong>of</strong> <strong>the</strong> wrong type for <strong>the</strong> area <strong>the</strong> vessel was operating in, and it was<br />
concluded that if <strong>the</strong> correct medication had been made available <strong>the</strong><br />
fatalities would have been avoided.<br />
In <strong>the</strong> malarial regions <strong>of</strong> <strong>the</strong> world, different strains <strong>of</strong> <strong>the</strong> infection build<br />
up resistance to <strong>the</strong> various medications available and it is important that<br />
medical advice is obtained for <strong>the</strong> area in question prior to <strong>the</strong> vessel<br />
arriving.<br />
The Ship Captain’s Medical<br />
Guide and Marine Guidance<br />
Note 257 (M) (published by <strong>the</strong><br />
UK’s Maritime and Coastguard<br />
Agency) contain advice on <strong>the</strong><br />
precautions to be taken and <strong>the</strong><br />
medicines available. The Health<br />
Authorities <strong>of</strong> <strong>the</strong> Members’<br />
country <strong>of</strong> domicile will be able<br />
to give advice on <strong>the</strong> type <strong>of</strong><br />
preventative medicines to be<br />
administered whilst <strong>the</strong> vessel is in<br />
a malarial region.<br />
Root Cause:<br />
Inadequate medical procedures.<br />
Issue Date: 06/02/06<br />
Case No.35489<br />
176 177
Personal Injury/Illness<br />
Safety Goggles - Not Just for Hindsight<br />
The Incident:<br />
This incident occurred on board an anchor handling<br />
supply vessel operating <strong>of</strong>f <strong>the</strong> west coast <strong>of</strong> Africa.<br />
The second engineer was supervising <strong>the</strong> cleaning<br />
<strong>of</strong> <strong>the</strong> mechanism <strong>of</strong> <strong>the</strong> vessel’s towing pins as part<br />
<strong>of</strong> <strong>the</strong> vessel’s routine maintenance programme.<br />
The cleaning was being carried out using a<br />
high-pressure water jet. The operator <strong>of</strong> <strong>the</strong> highpressure<br />
jet was wearing protective clothing in<br />
accordance with <strong>the</strong> manufacturer’s instructions.<br />
During <strong>the</strong> cleaning operation <strong>the</strong> second engineer<br />
who was wearing no protective clothing was hit in<br />
<strong>the</strong> left eye at a distance <strong>of</strong> about one metre by <strong>the</strong><br />
jet <strong>of</strong> water from <strong>the</strong> high-pressure washer.<br />
His vision was affected and a few days later was<br />
examined by an ophthalmologist in Point Noire<br />
in <strong>the</strong> Congo. The ophthalmologist diagnosed a<br />
simple eye irritation. The ophthalmologist treated<br />
<strong>the</strong> engineer for approximately two months with<br />
antiseptic eye lotions without improvement.<br />
During this period <strong>the</strong>re was no discernible<br />
improvement in his condition. The engineer<br />
completed his normal tour <strong>of</strong> duty. On his return<br />
home <strong>the</strong> second engineer consulted his own<br />
doctors who immediately diagnosed a detached<br />
retina. The <strong>of</strong>ficer underwent immediate eye<br />
surgery but because <strong>of</strong> <strong>the</strong> delay <strong>the</strong> doctors were<br />
unable to restore his vision.<br />
Observations:<br />
This accident would have been avoided if <strong>the</strong> second<br />
engineer had set a good example to <strong>the</strong> crew by<br />
wearing goggles while in <strong>the</strong> vicinity <strong>of</strong> <strong>the</strong> work.<br />
Masters should be given clear guidelines about<br />
reporting on-going medical problems to head<br />
<strong>of</strong>fice. The fact that <strong>the</strong> second engineer’s condition<br />
did not improve quickly should have been cause<br />
for concern. If <strong>the</strong> second engineer had been<br />
repatriated earlier he may not have lost <strong>the</strong> sight <strong>of</strong><br />
his eye.<br />
Root Cause:<br />
Human Error.<br />
Financial Cost:<br />
Although <strong>the</strong> engineer received benefits from<br />
his State’s welfare system <strong>the</strong> cost to <strong>the</strong> owners<br />
exceeded US$25,000.<br />
Issue Date:01/01/02<br />
Case No.21940<br />
178 179
Navigation<br />
Close Quarters Manoeuvring Results in Sinking<br />
The Incident:<br />
This anchor handling supply vessel had been<br />
chartered to deploy anchors for a pipelaying barge<br />
operating in shallow water. In addition to <strong>the</strong> new<br />
pipeline <strong>the</strong>re was an old pipeline and an unmarked<br />
subsea wellhead in <strong>the</strong> vicinity. While retrieving one<br />
<strong>of</strong> <strong>the</strong> barge’s anchors <strong>the</strong> anchor handler hit <strong>the</strong><br />
wellhead, breaching <strong>the</strong> engine room. The vessel’s<br />
pumps could not keep up with <strong>the</strong> ingress <strong>of</strong> water<br />
and it sank to <strong>the</strong> seabed impaled on <strong>the</strong> wellhead.<br />
Observations:<br />
A few days before <strong>the</strong> incident occurred <strong>the</strong> barge<br />
Master had given <strong>the</strong> Master a new chart <strong>of</strong> <strong>the</strong><br />
working area. Although <strong>the</strong> well’s position was<br />
accurately shown to within a metre <strong>the</strong> depth<br />
information was incorrect, leading <strong>the</strong> Master to<br />
believe that he would have an underkeel clearance<br />
<strong>of</strong> approximately two metres when in fact he had<br />
none. The barge was equipped with a sophisticated<br />
positioning system utilising differential GPS which<br />
was accurate to +/- 3 metres. Additional equipment<br />
on board <strong>the</strong> anchor handler allowed <strong>the</strong> surveyors<br />
on <strong>the</strong> barge to monitor <strong>the</strong> position <strong>of</strong> <strong>the</strong> anchor<br />
handler’s stern roller, enabling <strong>the</strong>m to position <strong>the</strong><br />
anchors with great accuracy. The anchor handler<br />
however was not given a monitor and had no way<br />
<strong>of</strong> accessing this information. The wellhead was<br />
not buoyed and <strong>the</strong> Master had no visual reference<br />
o<strong>the</strong>r than <strong>the</strong> barge. As a result he had been<br />
manoeuvring solely on <strong>the</strong> orders <strong>of</strong> <strong>the</strong> barge.<br />
Modern position fixing systems permit many<br />
operations to take place in closer proximity to<br />
navigational hazards than was possible in <strong>the</strong> past.<br />
Offshore personnel must however remain aware <strong>of</strong><br />
<strong>the</strong> practical problems in accurately manoeuvring<br />
a large anchor handler without visual reference. In<br />
this case <strong>the</strong> anchor had been positioned only 30<br />
metres from <strong>the</strong> wellhead, with <strong>the</strong> result that <strong>the</strong><br />
Master was required to manoeuvre his vessel within<br />
less than half a ship’s length <strong>of</strong> <strong>the</strong> hazard without<br />
<strong>the</strong> benefit <strong>of</strong> a visual reference or a GPS monitor.<br />
This incident could have been avoided if divers<br />
had checked <strong>the</strong> depth over <strong>the</strong> wellhead and its<br />
position had been marked with a buoy.<br />
Root Cause:<br />
Inadequate third party procedures.<br />
Financial Cost:<br />
The anchor handler valued at approximately US$3<br />
million was a total loss. In addition to this <strong>the</strong> costs<br />
<strong>of</strong> removing <strong>the</strong> wreck from <strong>the</strong> wellhead and<br />
disposing <strong>of</strong> it exceeded US$2.25 million.<br />
Issue Date:01/01/02<br />
Case No.21777<br />
180 181
Navigation<br />
A Good Case for Adequate Bridge Manning<br />
The Incident:<br />
This claim involved a small dredger operating a<br />
three times a week service between two local<br />
ports. She was manned by a senior and junior<br />
Master, two engineers and two ABs who were split<br />
into two teams <strong>of</strong> three, operating a six on, six <strong>of</strong>f<br />
watchkeeping rota.<br />
At <strong>the</strong> time in question <strong>the</strong> junior Master, at <strong>the</strong><br />
request <strong>of</strong> <strong>the</strong> senior Master, had taken <strong>the</strong> bridge<br />
watch early upon <strong>the</strong> vessel’s departure from <strong>the</strong><br />
berth at 1745.<br />
As <strong>the</strong> vessel proceeded down a buoyed channel<br />
<strong>the</strong> VTS observed that <strong>the</strong> vessel was straying to<br />
port <strong>of</strong> her advised track and unsuccessful efforts<br />
were made to alert <strong>the</strong> vessel. Shortly <strong>the</strong>reafter<br />
<strong>the</strong> vessel should have made a substantial alteration<br />
<strong>of</strong> course to port, but did not make <strong>the</strong> turn,<br />
instead headed across <strong>the</strong> main shipping channel<br />
and towards a pier and shallow waters. The VTS<br />
again tried to make contact with <strong>the</strong> vessel to<br />
advise <strong>of</strong> <strong>the</strong> impending danger but no response<br />
was received. After narrowly missing a marina <strong>the</strong><br />
vessel collided with a pier, causing severe structural<br />
damage. Fortunately no injuries were sustained.<br />
Observations:<br />
The <strong>of</strong>ficial investigation into <strong>the</strong> cause <strong>of</strong> this<br />
incident found that <strong>the</strong> junior Master had very little<br />
recollection <strong>of</strong> events. It was concluded that his<br />
performance was greatly reduced through a possible<br />
combination <strong>of</strong> tiredness, alcohol consumption<br />
prior to taking over <strong>the</strong> watch and <strong>the</strong> taking <strong>of</strong><br />
prescribed medication. In addition, at <strong>the</strong> time <strong>of</strong> <strong>the</strong><br />
incident he was <strong>the</strong> sole watchkeeper on <strong>the</strong> bridge<br />
after <strong>the</strong> AB had left following an altercation.<br />
The vessel complied with <strong>the</strong> minimum manning<br />
requirements <strong>of</strong> <strong>the</strong> governing authority however<br />
<strong>the</strong> rest periods as required by <strong>the</strong> Hours <strong>of</strong><br />
Work regulations were not being fully met for<br />
a number <strong>of</strong> reasons. The junior Master had<br />
been ashore immediately prior to <strong>the</strong> vessel’s<br />
departure consuming alcohol and he was also<br />
taking anti-depressants.<br />
As is <strong>the</strong> case with <strong>the</strong>se incidents, <strong>the</strong> causation<br />
was a collection <strong>of</strong> factors, not least <strong>of</strong> all bridge<br />
manning that did not comply with <strong>the</strong> regulations,<br />
<strong>the</strong> sole bridge watchkeeper having consumed<br />
sufficient alcohol to exceed <strong>the</strong> legal road driving<br />
limits and an element <strong>of</strong> tiredness due to poor use<br />
<strong>of</strong> <strong>of</strong>f-duty periods.<br />
Members are advised to ensure that <strong>the</strong>ir vessels<br />
are manned so that all regulatory requirements can<br />
be met and Masters instructed accordingly. This case<br />
has shown that familiarity with a navigating area is<br />
not an excuse for allowing standards to slip.<br />
Root Cause:<br />
Inadequate Navigation Lookout.<br />
Financial Cost:<br />
US$795,000<br />
Issue Date: 27/10/05<br />
Case No. 41728<br />
182 183
Navigation<br />
Keeping a Proper Lookout at ALL Times<br />
The Incident:<br />
This incident involved a harbour tug which collided with a moored tanker.<br />
The tug had completed one assignment and was crossing <strong>the</strong> port to its next job. The<br />
skipper was assisted on <strong>the</strong> bridge by a deck hand, who prior to <strong>the</strong> incident had a<br />
prolonged toilet break. The skipper made a final alteration <strong>of</strong> course towards <strong>the</strong> vessel<br />
she was to assist. Shortly afterwards <strong>the</strong> tug collided head on with a vessel moored at<br />
<strong>the</strong> terminal. This caused damage to some sections <strong>of</strong> <strong>the</strong> tanker’s shell plating and <strong>the</strong><br />
vessel had to be taken out <strong>of</strong> service for repairs. Fortunately no-one was hurt.<br />
Observations:<br />
The Master and crew man stated that <strong>the</strong>y had<br />
fallen asleep in <strong>the</strong> period between <strong>the</strong> alteration <strong>of</strong><br />
course and <strong>the</strong> collision, although this was at most<br />
six minutes. Notwithstanding <strong>the</strong> reason, <strong>the</strong> fact<br />
is that an effective lookout was not kept on <strong>the</strong> tug<br />
and it is very fortunate that <strong>the</strong> result <strong>of</strong> <strong>the</strong> collision<br />
was not a lot worse than it was.<br />
The importance <strong>of</strong> keeping a good lookout at all<br />
times on all types <strong>of</strong> vessels when underway cannot<br />
be over emphasised. It also raises <strong>the</strong> ever present<br />
question <strong>of</strong> fatigue which must not be ignored.<br />
Root Cause:<br />
Inadequate navigational lookout.<br />
Financial Cost:<br />
The claim was settled for US$200,000<br />
Issue Date: 30/08/05<br />
Case No. 46140<br />
184 185
Navigation<br />
A Moment’s Lapse <strong>of</strong> Concentration Causes Collision<br />
The Incident:<br />
The supply vessel in question<br />
had been chartered by a drilling<br />
contractor to service a semisubmersible<br />
rig. The barge Master<br />
<strong>of</strong> <strong>the</strong> rig had instructed <strong>the</strong><br />
supply vessel to act as safety boat<br />
on <strong>the</strong> starboard side <strong>of</strong> <strong>the</strong> rig<br />
while service personnel worked<br />
on a flare boom. The supply<br />
vessel was being manoeuvred in<br />
close proximity to <strong>the</strong> rig by an<br />
experienced Master.<br />
Some <strong>of</strong> <strong>the</strong> supply vessel’s crew<br />
were using a hose to wash down<br />
<strong>the</strong> bridge and accommodation<br />
block. Water from <strong>the</strong>ir hose<br />
came into <strong>the</strong> bridge through an<br />
open bridge wing door, splashing<br />
<strong>the</strong> radar and o<strong>the</strong>r electrical<br />
equipment. The Master left <strong>the</strong><br />
aft controls to close <strong>the</strong> door but<br />
in that short period <strong>the</strong> vessel<br />
moved astern and <strong>the</strong> port<br />
quarter came into contact with<br />
<strong>the</strong> centre starboard column <strong>of</strong><br />
<strong>the</strong> semi-submersible.<br />
Observations:<br />
This incident highlights <strong>the</strong> risks <strong>of</strong> a momentary<br />
lapse <strong>of</strong> attention on <strong>the</strong> part <strong>of</strong> <strong>the</strong> <strong>of</strong>ficer in charge<br />
when manoeuvring in very close proximity to o<strong>the</strong>r<br />
vessels or structures. The incident would not have<br />
occurred if <strong>the</strong> Master had ignored <strong>the</strong> distraction<br />
and not left <strong>the</strong> controls. The Master should have<br />
used <strong>the</strong> deck loudhailer system to draw <strong>the</strong><br />
attention <strong>of</strong> <strong>the</strong> crew to <strong>the</strong> problem.<br />
Root Cause:<br />
Human error.<br />
Financial Cost:<br />
Repairs to <strong>the</strong> rig alone cost US$55,000 and by <strong>the</strong><br />
time surveyors’ fees and o<strong>the</strong>r costs had been taken<br />
into account <strong>the</strong> total cost to <strong>the</strong> owner was over<br />
US$60,000.<br />
Issue Date:01/01/02<br />
Case No.23178<br />
186 187
Navigation<br />
Thruster Failure Causes Rig Damage<br />
The Incident:<br />
This vessel was one <strong>of</strong> two anchor handlers shifting a semisubmersible<br />
rig. Conditions were not ideal. A strong wind was<br />
blowing on <strong>the</strong> port bow <strong>of</strong> <strong>the</strong> rig and a current <strong>of</strong> over 1 knot<br />
setting onto that side. The anchor handler was ordered to retrieve<br />
<strong>the</strong> no. 2 anchor on <strong>the</strong> port side which was run out at an angle <strong>of</strong><br />
about 60° from <strong>the</strong> rig’s centre line. The anchor was lifted clear <strong>of</strong> <strong>the</strong><br />
bottom and hauled up to <strong>the</strong> stern roller. The tug <strong>the</strong>n manoeuvred<br />
slowly astern towards <strong>the</strong> rig while <strong>the</strong> anchor chain was being<br />
recovered by <strong>the</strong> windlass on <strong>the</strong> rig. As <strong>the</strong> tug approached <strong>the</strong> rig<br />
<strong>the</strong> barge Master asked that it swing aft to a position on <strong>the</strong> beam<br />
<strong>of</strong> <strong>the</strong> rig in order to give a better clearance to <strong>the</strong> no. 1 port side<br />
anchor wire. This brought <strong>the</strong> wind onto <strong>the</strong> beam <strong>of</strong> <strong>the</strong> anchor<br />
handler. To hold this position required full power from <strong>the</strong> bow<br />
thruster which started to overheat and eventually tripped out,<br />
with <strong>the</strong> result that <strong>the</strong> bow fell <strong>of</strong>f <strong>the</strong> wind. The loss <strong>of</strong> <strong>the</strong> bow<br />
thruster made <strong>the</strong> supply vessel difficult to manoeuvre. Attempts<br />
were made to pass <strong>the</strong> anchor pennant wire to <strong>the</strong> barge crane,<br />
however <strong>the</strong> shark’s jaws malfunctioned and <strong>the</strong> pennant wire could<br />
not be released. The tug, pinned by <strong>the</strong> anchor wire at <strong>the</strong> stern,<br />
was swept down onto <strong>the</strong> rig by wind and tide. She landed heavily on<br />
<strong>the</strong> port side ranging up and down causing severe damage.<br />
Observations:<br />
This incident shows how a number <strong>of</strong> factors can<br />
<strong>of</strong>ten combine to create a serious incident. It also<br />
emphasises <strong>the</strong> need to ensure that equipment<br />
is properly maintained in full working order,<br />
particularly when close quarters manoeuvring is<br />
envisaged. Although this was <strong>the</strong> first time <strong>the</strong><br />
shark’s jaws had failed, overheating was a recurrent<br />
problem with <strong>the</strong> bow thruster which had never<br />
been properly repaired. In this case failure <strong>of</strong> ei<strong>the</strong>r<br />
<strong>the</strong> bow thruster or <strong>the</strong> shark’s jaws alone would<br />
not have resulted in a collision, but when <strong>the</strong> effects<br />
<strong>of</strong> <strong>the</strong> two were combined when <strong>the</strong> vessel was in<br />
close proximity to <strong>the</strong> rig it became inevitable.<br />
Root Cause:<br />
Insufficient maintenance<br />
programme.<br />
Financial Cost:<br />
The rig was out <strong>of</strong> action for<br />
10½ days. The claim for damage<br />
and loss <strong>of</strong> use exceeded <strong>the</strong><br />
tug’s limitation fund under <strong>the</strong><br />
1976 Convention. The claim was<br />
settled for <strong>the</strong> limitation fund<br />
but never<strong>the</strong>less <strong>the</strong> total cost<br />
exceeded US$450,000. The tug<br />
itself suffered heavy damage as a<br />
result <strong>of</strong> <strong>the</strong> collision.<br />
Issue Date:01/01/02<br />
Case No.23047<br />
188 189
Navigation<br />
Tidal Calculation Error Results in Bridge Damage<br />
The Incident:<br />
A coastal tug towing a barge<br />
carrying 6,000 tons <strong>of</strong> cargo<br />
encountered difficulties<br />
manoeuvring on <strong>the</strong> way up<br />
river at her destination. The tug<br />
lost control <strong>of</strong> <strong>the</strong> barge which<br />
collided with a swing railway<br />
bride causing damage valued at<br />
US$180,000.<br />
The tug had brought <strong>the</strong> barge<br />
up <strong>the</strong> coast, arriving <strong>of</strong>f <strong>the</strong> river<br />
mouth at midday. Before starting<br />
up <strong>the</strong> river <strong>the</strong> tug Master<br />
shortened up <strong>the</strong> tow, bringing<br />
<strong>the</strong> tow line right in until only <strong>the</strong><br />
bridle remained out board - this<br />
brought <strong>the</strong> swim bow <strong>of</strong> <strong>the</strong><br />
barge close up to <strong>the</strong> stern <strong>of</strong><br />
<strong>the</strong> tug. The tug and barge <strong>the</strong>n<br />
proceeded at slow speed up <strong>the</strong><br />
north arm <strong>of</strong> <strong>the</strong> Fraser river,<br />
aiming to arrive below <strong>the</strong> Arthur<br />
Laing Bridge after <strong>the</strong> ebb had<br />
started to flow. Arrangements<br />
had been made for a harbour tug<br />
to rendezvous with <strong>the</strong> flotilla<br />
at this point to assist <strong>the</strong>m in<br />
rounding <strong>the</strong> bend and passing<br />
through <strong>the</strong> Marpole swing<br />
railway bridge. Despite <strong>the</strong> lead<br />
tug plying full helm and maximum<br />
power <strong>the</strong> flotilla failed to<br />
complete <strong>the</strong> turn and <strong>the</strong> barge<br />
struck <strong>the</strong> swing span protection<br />
pier, causing serious damage.<br />
Observations:<br />
The reasons why <strong>the</strong> barge<br />
did not negotiate <strong>the</strong> turn<br />
successfully have never been fully<br />
explained. There were however<br />
a number <strong>of</strong> factors which<br />
contributed to <strong>the</strong> accident.<br />
Both tug skippers had carried out<br />
this operation many times before.<br />
Perhaps because <strong>of</strong> this <strong>the</strong>re<br />
was no communication between<br />
<strong>the</strong> skippers when <strong>the</strong>y met and<br />
no instructions were given by <strong>the</strong><br />
lead tug.<br />
This unsatisfactory situation was<br />
compounded by <strong>the</strong> fact that <strong>the</strong><br />
barge completely blocked <strong>the</strong><br />
coastal tug’s view astern, with <strong>the</strong><br />
result that its skipper was unable<br />
to see where <strong>the</strong> assist tug was<br />
pushing. The primary function <strong>of</strong><br />
<strong>the</strong> assist tug is to help hold <strong>the</strong><br />
barge close to <strong>the</strong> north side <strong>of</strong><br />
<strong>the</strong> channel. If <strong>the</strong> assist tug pushes<br />
too far aft on <strong>the</strong> barge’s side it<br />
counteracts <strong>the</strong> lead tug’s efforts<br />
to pull <strong>the</strong> barge’s head round.<br />
Tidal streams upriver are less<br />
predictable than at <strong>the</strong> river<br />
mouth. The flotilla may have<br />
arrived at <strong>the</strong> turn too early,<br />
before <strong>the</strong> flood had ceased.<br />
The last <strong>of</strong> <strong>the</strong> flood tends to flow<br />
from north to south across <strong>the</strong><br />
basin between <strong>the</strong> bridges, which<br />
would have set <strong>the</strong> flotilla sideways<br />
down on to <strong>the</strong> railway bridge.<br />
The incident could have been<br />
avoided by delaying <strong>the</strong> flotilla’s<br />
arrival until <strong>the</strong> ebb was flowing<br />
strongly and by proper planning<br />
and better communication<br />
between <strong>the</strong> tug skippers.<br />
Root Cause:<br />
Inadequate operational planning.<br />
Issue Date: 01/01/02<br />
Case No.16344<br />
190 191
Navigation<br />
Master’s Failure to take Control Causes Dock Damage<br />
The Incident:<br />
A large cargo handling crane constructed in China was being transported to a new berth<br />
in South East Asia on <strong>the</strong> deck <strong>of</strong> a large ocean-going barge. Pilotage was compulsory at<br />
<strong>the</strong> port <strong>of</strong> destination and as <strong>the</strong> tug and barge combination approached its berth <strong>the</strong><br />
vessel was effectively being controlled by <strong>the</strong> pilot. To assist <strong>the</strong> tug Master a company<br />
superintendent had been stationed on <strong>the</strong> barge itself and was in radio contact with <strong>the</strong><br />
tug. In <strong>the</strong> final stages <strong>of</strong> <strong>the</strong> approach it became apparent to <strong>the</strong> superintendent that<br />
<strong>the</strong> angle <strong>of</strong> approach was too steep and <strong>the</strong> speed was too great. This information was<br />
passed to <strong>the</strong> Captain <strong>of</strong> <strong>the</strong> tug who requested <strong>the</strong> pilot abort <strong>the</strong> berthing manoeuvre.<br />
The pilot refused to do so. The Master did not take control <strong>of</strong> <strong>the</strong> situation and allowed<br />
<strong>the</strong> manoeuvre to continue. The barge made heavy contact with <strong>the</strong> dock, causing<br />
damage to <strong>the</strong> fendering system.<br />
Observations:<br />
National laws and Port bye-laws normally hold<br />
vessels strictly liable for damage done to harbour<br />
works. The relevant law in this case provided “any<br />
damage done to wharves ..... by a vessel whe<strong>the</strong>r<br />
due to <strong>the</strong> incompetence or carelessness <strong>of</strong> <strong>the</strong><br />
authority pilot .... shall be made good by <strong>the</strong> owner,<br />
Master or agent <strong>of</strong> <strong>the</strong> vessel”.<br />
In any event pilots invariably contract on terms<br />
which severely limit <strong>the</strong>ir liability or absolve <strong>the</strong>m<br />
entirely <strong>of</strong> responsibility for <strong>the</strong>ir actions. A pilot’s<br />
function is to advise and assist <strong>the</strong> vessel’s Master,<br />
who remains ultimately responsible for <strong>the</strong> handling<br />
<strong>of</strong> his vessel. The Master should have taken control<br />
and aborted <strong>the</strong> manoeuvre.<br />
Root Cause:<br />
Human error.<br />
Financial Cost:<br />
The Port Authority’s claim exceeded US$50,000.<br />
On this occasion however <strong>the</strong>y did accept that <strong>the</strong><br />
pilot was largely to blame and <strong>the</strong> agreed to settle<br />
for two thirds <strong>of</strong> <strong>the</strong> actual repair costs. The pilot<br />
concerned was subsequently sacked.<br />
Issue Date:01/01/02<br />
Case No.23774<br />
192 193
Navigation<br />
Grounding/Pollution because <strong>of</strong> Bad Lookout<br />
The Incident:<br />
This incident involves <strong>the</strong><br />
accidental grounding <strong>of</strong><br />
a rig standby vessel in an<br />
environmentally sensitive<br />
area. The vessel which was<br />
carrying 160 tons <strong>of</strong> oil at<br />
<strong>the</strong> time suffered extensive<br />
bottom damage and her engine<br />
room was flooded. Pollution<br />
prevention measures were<br />
immediately put in place and <strong>the</strong><br />
vessel was finally salvaged.<br />
Observations:<br />
The vessel had been returning to her home port<br />
with <strong>the</strong> Master as sole watchkeeper. As he<br />
approached land <strong>the</strong> Master moved to <strong>the</strong> after<br />
end <strong>of</strong> <strong>the</strong> wheelhouse to make a radio telephone<br />
call. What <strong>the</strong> Master believed would be a short call<br />
proved more complex than expected. The Master<br />
lost track <strong>of</strong> time and <strong>the</strong> vessel continued under<br />
autopilot, eventually driving itself hard aground<br />
at full speed at <strong>the</strong> base <strong>of</strong> cliffs adjacent to <strong>the</strong><br />
port. This incident occurred as a direct result <strong>of</strong><br />
<strong>the</strong> Master’s failure to keep a proper lookout and<br />
maintain a safe navigational watch. The accident<br />
could have been avoided by augmenting <strong>the</strong> bridge<br />
watch to cope safely with <strong>the</strong> additional workload as<br />
<strong>the</strong> vessel closed <strong>the</strong> land.<br />
Root Cause:<br />
Failure to maintain proper lookout.<br />
Financial Cost:<br />
The cost <strong>of</strong> salving and repairing <strong>the</strong> vessel<br />
exceeded US$2.3 million. Anti-pollution measures<br />
added a fur<strong>the</strong>r US$50,000 to <strong>the</strong> bill.<br />
Issue Date:01/01/02<br />
Case No.12868<br />
194 195
Navigation<br />
Knock for Knock Clause Fails to Protect Owner from Rig Damage Claim<br />
The Incident:<br />
The incident occurred as a supply vessel was<br />
backloading drill casing from a semi-submersible<br />
rig. The vessel was backed up to <strong>the</strong> rig with her<br />
stern into <strong>the</strong> prevailing current and <strong>the</strong> wind on<br />
her port quarter. The vessel was being held in<br />
position by her engines and bow thruster.<br />
During cargo transfer operations <strong>the</strong> port engine<br />
pitch control failed and although its control was<br />
set to give forward thrust, <strong>the</strong> pitch moved to<br />
full astern. Despite <strong>the</strong> Master’s prompt actions<br />
in declutching <strong>the</strong> engine and applying full ahead<br />
power on <strong>the</strong> starboard engine, <strong>the</strong> vessel collided<br />
with and seriously damaged <strong>the</strong> rig leg.<br />
Observations:<br />
This incident highlights <strong>the</strong><br />
risks inherent in close quarters<br />
manoeuvring. In this particular<br />
situation <strong>the</strong>re was little more<br />
that <strong>the</strong> Master could have done<br />
to avoid <strong>the</strong> collision. The vessel’s<br />
pitch control was arranged in <strong>the</strong><br />
‘conventional’ manner with <strong>the</strong><br />
fail-safe position being full astern.<br />
For rig supply vessels however<br />
<strong>the</strong> greatest danger arises when<br />
<strong>the</strong> vessel is backed up to a rig<br />
and for this reason it is generally<br />
considered good practice for <strong>the</strong>se<br />
vessels’ pitch controls to fail-safe to<br />
<strong>the</strong> full ahead position. Although<br />
<strong>the</strong>re was a knock-for-knock clause<br />
in <strong>the</strong> charterparty its effect was<br />
restricted to claims between <strong>the</strong><br />
owners <strong>of</strong> <strong>the</strong> supply vessel and<br />
<strong>the</strong> charterers in relation to <strong>the</strong>ir<br />
respective personnel and property.<br />
In this case <strong>the</strong> rig was not <strong>the</strong><br />
charterer’s property and <strong>the</strong> rig’s<br />
owners were not bound by those<br />
contractual terms. If <strong>the</strong> knockfor-knock<br />
clause had been worded<br />
in such a way as to include <strong>the</strong><br />
contractors and sub-contractors <strong>of</strong><br />
each party, <strong>the</strong>n <strong>the</strong> owners <strong>of</strong> <strong>the</strong><br />
supply boat would not have had to<br />
pay for <strong>the</strong> damage to <strong>the</strong> rig.<br />
Financial Cost:<br />
Repairs to <strong>the</strong> rig were carried<br />
out concurrently with a routine<br />
refit. Never<strong>the</strong>less by <strong>the</strong> time<br />
surveyors’ fees and classification<br />
survey costs had been taken into<br />
account <strong>the</strong> total cost rose to<br />
almost US$160,000.<br />
Issue Date:01/01/02<br />
Case No.25250<br />
196 197
Miscellaneous<br />
When is a Master Off Duty<br />
The Incident:<br />
Whilst alongside a lay-by berth<br />
on <strong>the</strong> UK east coast, <strong>the</strong> Master<br />
<strong>of</strong> an oil rig supply vessel was<br />
informed by charterers that<br />
<strong>the</strong> vessel was not required<br />
for working until <strong>the</strong> following<br />
morning. As usual on this vessel<br />
under such circumstances <strong>the</strong><br />
Chief Officer went on duty for<br />
<strong>the</strong> night and deck and engine<br />
port watches were set.<br />
The Master went ashore and<br />
returned some time later in <strong>the</strong><br />
evening having consumed three<br />
or four pints <strong>of</strong> beer. Some<br />
hours after his return an incident<br />
occurred that necessitated police<br />
attendance. However, despite <strong>the</strong><br />
incident not involving <strong>the</strong> Master<br />
he was breathalysed by <strong>the</strong> police<br />
and arrested and charged on<br />
suspicion <strong>of</strong> being a pr<strong>of</strong>essional<br />
Master <strong>of</strong> a ship while on duty<br />
with a proportion <strong>of</strong> alcohol in his<br />
breath which exceeded <strong>the</strong><br />
prescribed limits <strong>of</strong> 35 micrograms<br />
<strong>of</strong> alcohol in 100 millilitres <strong>of</strong><br />
blood, contrary to Section 78.1(a)<br />
<strong>of</strong> <strong>the</strong> United Kingdom’s “Railways<br />
and Transport Safety Act 2003”.<br />
A fur<strong>the</strong>r test at <strong>the</strong> police station<br />
confirmed that he was over <strong>the</strong><br />
prescribed limit.<br />
A forensic toxicology report<br />
indicated that <strong>the</strong> Master would<br />
have been below <strong>the</strong> prescribed<br />
limit at 08:00 <strong>the</strong> following day<br />
when he was due to come back<br />
on duty. Fur<strong>the</strong>rmore, <strong>the</strong> amount<br />
<strong>of</strong> alcohol consumed did not put<br />
him in breach <strong>of</strong> his Company’s<br />
Drug and Alcohol Regulations.<br />
The case was tried in <strong>the</strong> local<br />
Magistrates Court before a<br />
District Judge.<br />
The case turned on whe<strong>the</strong>r <strong>the</strong><br />
Master was ‘always on duty’ and<br />
particularly whe<strong>the</strong>r he was always<br />
on duty for <strong>the</strong> purposes <strong>of</strong> <strong>the</strong> Act.<br />
The Act did not define ‘duty’ and<br />
fur<strong>the</strong>rmore ‘duty’ is not defined<br />
elsewhere. It is <strong>of</strong>ten thought that a<br />
Master is always on duty from <strong>the</strong><br />
moment he/she signs on a vessel to<br />
<strong>the</strong> moment he/she signs <strong>of</strong>f. It was<br />
argued that a Master’s duty was not<br />
unlimited in its b<strong>read</strong>th or scope;<br />
to find o<strong>the</strong>rwise would confuse<br />
performance and discharge <strong>of</strong> duty<br />
with <strong>the</strong> existence <strong>of</strong> a status or<br />
responsibility. Fur<strong>the</strong>rmore, to do<br />
so would fail to distinguish between<br />
<strong>the</strong> different facets <strong>of</strong> a Master’s<br />
duties, which include duties by<br />
common law, statute, regulation,<br />
custom and by contract.<br />
It was argued on behalf <strong>of</strong> <strong>the</strong><br />
Master that <strong>the</strong> correct definition<br />
<strong>of</strong> ‘duty’ for <strong>the</strong> purposes <strong>of</strong> <strong>the</strong><br />
Act is:-<br />
“Whilst on duty means, in <strong>the</strong><br />
course <strong>of</strong> his employment as a<br />
pr<strong>of</strong>essional Master <strong>of</strong> a ship,<br />
performing or being liable to be<br />
called onto perform a safety critical<br />
function, in <strong>the</strong> operation <strong>of</strong> <strong>the</strong><br />
ship, which it is his duty to perform.”<br />
The Judge accepted this definition,<br />
accepted that <strong>the</strong> Master had<br />
not performed any ‘safety critical<br />
functions’ at <strong>the</strong> time he was ‘over<br />
<strong>the</strong> prescribed limit’ and acquitted<br />
<strong>the</strong> Master accordingly.<br />
Whilst <strong>the</strong> definition <strong>of</strong> ‘duty’ put<br />
forward on behalf <strong>of</strong> <strong>the</strong> Master<br />
was accepted by <strong>the</strong> Court,<br />
<strong>the</strong> facts <strong>of</strong> <strong>the</strong> case assisted<br />
<strong>the</strong> Master’s defence, and in<br />
particular:-<br />
The vessel was laid up with<br />
no orders to sail until <strong>the</strong><br />
following morning.<br />
1. The Chief Officer was certified<br />
to act as Master on this<br />
particular vessel.<br />
2. The level <strong>of</strong> alcohol consumed,<br />
whilst over <strong>the</strong> prescribed limit,<br />
was relatively low.<br />
3. The Master complied with<br />
all company regulations and<br />
procedures as regards alcohol.<br />
4. The vessel complied with all<br />
<strong>the</strong> local harbour regulations<br />
and bye-laws.<br />
5. Toxicology tests showed that<br />
<strong>the</strong> Master would have been<br />
sober upon taking up his duties<br />
<strong>the</strong> following morning.<br />
The outcome could have been<br />
different had any <strong>of</strong> <strong>the</strong>se facts<br />
been different, for example, had<br />
<strong>the</strong> Master been breathalysed and<br />
found to be over <strong>the</strong> limit one<br />
hour before sailing.<br />
Therefore whilst it is up to individual<br />
companies to decide whe<strong>the</strong>r <strong>the</strong>y<br />
run dry ships, those that do not still<br />
need to ensure <strong>the</strong>ir staff are fully<br />
aware <strong>of</strong> <strong>the</strong>ir obligations under<br />
<strong>the</strong> Act in addition to any company<br />
procedures that may be in place,<br />
because <strong>the</strong> Master being removed<br />
from his vessel by <strong>the</strong> authorities<br />
can have serious commercial<br />
implications beyond those personal<br />
consequences suffered by <strong>the</strong><br />
Master himself.<br />
Although this case has arisen<br />
under <strong>the</strong> law in <strong>the</strong> UK, similar<br />
legislation exists in many countries<br />
around <strong>the</strong> world and it is<br />
appropriate to circulate it widely.<br />
Issue Date: 15/05/07<br />
Case No. 50052<br />
198 199
Miscellaneous<br />
Early Request for Club Assistance could have Buoyed up Members Defence<br />
The Incident:<br />
During a transit <strong>of</strong> <strong>the</strong> Suez<br />
Canal our Member’s vessels were<br />
alleged to have hit and severely<br />
damaged a navigation buoy.<br />
The first notice that <strong>the</strong> owners had<br />
was a letter from <strong>the</strong> Suez Canal<br />
Authority alleging that <strong>the</strong>ir vessel<br />
had damaged a navigational mark<br />
and inviting <strong>the</strong>m to attend a joint<br />
survey. Our Member contacted<br />
<strong>the</strong> tug Master and <strong>the</strong> pilot, both<br />
<strong>of</strong> whom denied that <strong>the</strong>re had<br />
been any contact. In view <strong>of</strong> this<br />
our Member wrote back to <strong>the</strong><br />
Authority denying liability. A few<br />
weeks later <strong>the</strong>y were shocked to<br />
find that <strong>the</strong> Suez Canal Authority<br />
had unilaterally deducted Egyptian<br />
£89,000 from <strong>the</strong>ir deposit.<br />
At that point <strong>the</strong> Member contacted <strong>the</strong> Club who instructed its<br />
correspondent lawyers in Egypt to defend <strong>the</strong> Member’s interests.<br />
Our lawyers advised that <strong>the</strong>ir past experience was that once <strong>the</strong><br />
deduction had been made and it had been recorded in <strong>the</strong> accounts<br />
<strong>of</strong> <strong>the</strong> Canal Authority, it was almost impossible to persuade<br />
<strong>the</strong>m to re-open <strong>the</strong> case. We were able to demonstrate that our<br />
Member’s vessel’s passed <strong>the</strong> buoy in <strong>the</strong> early hours <strong>of</strong> <strong>the</strong> morning<br />
and that <strong>the</strong> damage was not reported until mid-afternoon. In <strong>the</strong><br />
intervening period <strong>the</strong> entire southbound convoy passed <strong>the</strong> location<br />
<strong>of</strong> <strong>the</strong> buoy and also some <strong>of</strong> <strong>the</strong> northbound ships, any <strong>of</strong> which<br />
could have done <strong>the</strong> damage. The Canal Authority prevented our<br />
correspondents from taking statements from <strong>the</strong> pilot or any o<strong>the</strong>r<br />
canal personnel. They refused to provide any documents, reports<br />
or o<strong>the</strong>r evidence to substantiate <strong>the</strong>ir claim that our Member was<br />
responsible for <strong>the</strong> loss.<br />
The Canal Authorities remained intransigent and faced with an<br />
expensive legal battle which might not be resolved for ten years or<br />
more, <strong>the</strong> Members decided not to pursue <strong>the</strong> matter.<br />
Observations:<br />
Members should be aware that in many parts <strong>of</strong><br />
<strong>the</strong> world Canal Authorities, Harbour Authorities<br />
and o<strong>the</strong>r quasi-governmental bodies enjoy special<br />
status where <strong>the</strong> normal rules <strong>of</strong> business dealing<br />
may not apply. Members encountering problems<br />
with such bodies are advised to obtain assistance<br />
from <strong>the</strong> Club at an early stage while <strong>the</strong> matter is<br />
still open to discussion.<br />
Financial Cost:<br />
The costs to our Member exceeded US$26,000.<br />
Issue Date: 01/01/02<br />
Case No. 21744<br />
200 201
Miscellaneous<br />
A Good Case for Tracking<br />
The Incident:<br />
A Member’s tug was towing a barge laden with coal between ports in South East Asia.<br />
Late one evening whilst on passage she was boarded by a gang <strong>of</strong> ten men, two <strong>of</strong><br />
whom were armed. The crew were tied up and <strong>the</strong> towline to <strong>the</strong> barge cut. The crew<br />
were <strong>the</strong>n taken near to <strong>the</strong> shore in <strong>the</strong> pirates’ speed boat and left to swim ashore,<br />
unharmed. The speed boat returned to <strong>the</strong> barge. The pirates <strong>the</strong>n turned <strong>the</strong> tug<br />
through 180 degrees, presumably heading for a port at which <strong>the</strong>y could disguise <strong>the</strong> tug.<br />
Unknown to <strong>the</strong> pirates, <strong>the</strong> Member had installed a tracking device on <strong>the</strong> tug. Upon her<br />
failure to arrive at <strong>the</strong> discharge port as expected, an investigation was carried out and<br />
it soon became clear to <strong>the</strong> Member what had occurred. The authorities were advised<br />
and within 36 hours both <strong>the</strong> tug and barge (which had been drifting at <strong>the</strong> mercy <strong>of</strong> <strong>the</strong><br />
elements) were located and arrangements made to recover <strong>the</strong>m.<br />
Observations:<br />
The Member’s foresight in equipping <strong>the</strong> tug with<br />
a satellite tracking system prevented a major claim.<br />
The cost <strong>of</strong> installation was recovered from this one<br />
unsuccessful attempt at hijacking <strong>the</strong> tug.<br />
The speed in which recovery was possible clearly<br />
demonstrates <strong>the</strong> value <strong>of</strong> <strong>the</strong> tracking equipment.<br />
The Club would encourage all Members who<br />
operate such vulnerable craft, to consider seriously<br />
installing a satellite tracking system.<br />
Financial Cost:<br />
No claim arose out <strong>of</strong> this incident and<br />
fortuitously all <strong>the</strong> crew were unharmed.<br />
Issue Date: 14/06/0<br />
Case No. 12345<br />
202 203
Miscellaneous<br />
Corrosion Causes Sinking <strong>of</strong> Laid-Up Vessel<br />
The Incident:<br />
This 14 year old vessel had been inactive for three years. She was laid<br />
up unmanned at a shipyard belonging to an associated company. One<br />
morning <strong>the</strong> vessel’s agent noticed that she was listing 15° to port and<br />
reported this to <strong>the</strong> yard. Yard personnel were mobilised to investigate<br />
<strong>the</strong> listing <strong>of</strong> <strong>the</strong> vessel however prior to any remedial action being<br />
possible <strong>the</strong> vessel capsized, landing on her port side on a s<strong>of</strong>t mud<br />
bottom. As <strong>the</strong>re was no-one on board at <strong>the</strong> time she capsized <strong>the</strong>re<br />
were no injuries. Shortly after <strong>the</strong> capsize an oil sheen started to<br />
appear on <strong>the</strong> surface. The Port Authority and <strong>the</strong> shipyard mobilised<br />
<strong>the</strong>ir pollution clean-up team. An oil boom was placed around <strong>the</strong><br />
vicinity <strong>of</strong> <strong>the</strong> capsized vessel and dispersant was sprayed on <strong>the</strong><br />
escaping oil. The Port Authority issued a wreck removal order. The<br />
vessel was salvaged ten days later.<br />
Observations:<br />
An investigation into <strong>the</strong> cause <strong>of</strong> <strong>the</strong> sinking traced <strong>the</strong><br />
source <strong>of</strong> sea water ingress to a small sea water pipe<br />
between <strong>the</strong> sea suction strainer and <strong>the</strong> refrigeration<br />
cooling water pump. During <strong>the</strong> period <strong>the</strong> vessel was<br />
laid up an elbow progressively corroded away at <strong>the</strong><br />
welded seams on ei<strong>the</strong>r side until it was so weakened<br />
that it fell <strong>of</strong>f. The subsequent ingress <strong>of</strong> sea water<br />
slowly flooded <strong>the</strong> engine room space, initially causing<br />
<strong>the</strong> vessel to sink deeper into <strong>the</strong> water and <strong>the</strong>n, as<br />
<strong>the</strong> starboard bilge grounded on <strong>the</strong> uneven bottom,<br />
to list and ultimately capsize.<br />
The loss would have been avoided if good practice<br />
had been followed and all sea valves had been closed<br />
when <strong>the</strong> vessel was laid up. The leak would also have<br />
been detected if <strong>the</strong> owners had made arrangements<br />
with <strong>the</strong> shipyard for regular housekeeping<br />
inspections to be carried out by yard personnel.<br />
Root Cause:<br />
Inadequate Procedure.<br />
Financial Cost:<br />
The owners were fortunate that heavy lifting<br />
equipment was al<strong>read</strong>y available in <strong>the</strong> port, <strong>the</strong>reby<br />
avoiding heavy mobilisation costs. Never<strong>the</strong>less<br />
raising <strong>the</strong> vessel still cost over US$125,000 and <strong>the</strong><br />
cost <strong>of</strong> anti-pollution measures reached US$20,000.<br />
Sea water had destroyed all <strong>the</strong> electrical equipment<br />
and installations and much <strong>of</strong> <strong>the</strong> machinery,<br />
with <strong>the</strong> result that <strong>the</strong> vessel required complete<br />
refurbishment.<br />
Issue Date: 01/01/02<br />
Case No.27691<br />
204 205
Section 6<br />
Harbour Craft<br />
207
Harbour Craft<br />
Personal Injury/Illness<br />
Face <strong>the</strong> Danger<br />
The Incident:<br />
The following accident report issued by <strong>the</strong> MAIB<br />
concerns an incident where a deckhand suffered<br />
multiple fractures to his arm whilst connecting a<br />
tug’s towing wire:<br />
“The tug’s tow rope messenger was led through a<br />
Panama lead, around <strong>the</strong> bits at a 100˚ angle and<br />
on to <strong>the</strong> winch end whipping drum. The drum<br />
end seaman was standing with his back to <strong>the</strong><br />
working part <strong>of</strong> <strong>the</strong> rope and <strong>the</strong> supervisor,<br />
as he hauled on <strong>the</strong> rope.<br />
Unfortunately <strong>the</strong> tug was not paying out slack at<br />
a controlled speed and, feeling <strong>the</strong> strain <strong>of</strong> <strong>the</strong><br />
jerking motion, <strong>the</strong> drum end seaman attempted to<br />
apply more turns to <strong>the</strong> whipping drum. During this<br />
process, <strong>the</strong> messenger rope snapped back, and <strong>the</strong><br />
whiplash <strong>of</strong> <strong>the</strong> working part connected with, and<br />
broke, <strong>the</strong> drum end seaman’s arm.<br />
The supervisor, who was standing in <strong>the</strong> precarious<br />
position <strong>of</strong> <strong>the</strong> bight <strong>of</strong> <strong>the</strong> rope, escaped injury.<br />
Had <strong>the</strong> rope come clear <strong>of</strong> <strong>the</strong> bits, <strong>the</strong> outcome<br />
for him could have been extremely serious.”<br />
Conclusion:<br />
Messenger rope arrangement<br />
1. Stand facing <strong>the</strong> danger: always put <strong>the</strong> winch<br />
between <strong>the</strong> operative and <strong>the</strong> potential danger<br />
zone. This, in itself, creates a safety barrier, allows<br />
full visual contact with <strong>the</strong> mooring team and<br />
surroundings, allows controlled surging on <strong>the</strong><br />
drum end and keeps <strong>the</strong> operative clear <strong>of</strong> <strong>the</strong><br />
working part.<br />
2. Be aware <strong>of</strong> <strong>the</strong> dangers <strong>of</strong> sharp nips – <strong>the</strong>se<br />
cause excess strain on machinery, fittings and<br />
ropes – and use fairleads wherever possible.<br />
3. During our first day at sea, most <strong>of</strong> us were made<br />
aware <strong>of</strong> <strong>the</strong> dangers <strong>of</strong> standing in bights <strong>of</strong> rope;<br />
a brief lapse <strong>of</strong> attention to this ordinary practice<br />
can so easily cause grief.<br />
4. Watch out for shipmates and <strong>the</strong>ir work<br />
practices. Ships operate on efficient teamworking,<br />
part <strong>of</strong> which involves looking out for<br />
our shipmates and recognising potential dangers<br />
to <strong>the</strong>m. It is so much easier to stop bad habits<br />
than to patch up broken bodies.<br />
Issue Date: 24/10/07<br />
Case No. 12349<br />
208 209
Personal Injury/Illness<br />
Girting Capsizes Small Tug<br />
The Incident:<br />
This incident occurred as a small passenger vessel<br />
was being towed from a river into a harbour basin.<br />
This dead tow was being performed by a harbour<br />
tug acting as lead tug and a tug/workboat which<br />
was made fast aft. The Masters <strong>of</strong> <strong>the</strong> two tugs had<br />
agreed that <strong>the</strong> towlines would be shortened <strong>of</strong>f <strong>the</strong><br />
basin entrance and that <strong>the</strong> lead tug would <strong>the</strong>n tow<br />
<strong>the</strong> vessel into <strong>the</strong> basin with <strong>the</strong> workboat holding<br />
<strong>the</strong> stern <strong>of</strong> <strong>the</strong> passenger vessel up into <strong>the</strong> ebb<br />
tide, which was running downriver at approximately<br />
3 knots. As <strong>the</strong>y commenced <strong>the</strong> final stage <strong>of</strong> <strong>the</strong><br />
tow <strong>the</strong> tug/workboat was girted and capsized,<br />
drowning its skipper.<br />
Observations:<br />
Once <strong>the</strong> towline had been shortened and <strong>the</strong><br />
slack had been picked up <strong>the</strong> lead tug called <strong>the</strong><br />
workboat to confirm that <strong>the</strong>y were <strong>read</strong>y to<br />
proceed. On receiving <strong>the</strong> all-clear <strong>the</strong> lead tug<br />
progressively applied power, turning <strong>the</strong> tow into line<br />
with <strong>the</strong> approach. Power had been brought up to<br />
approximately half ahead when <strong>the</strong> tug received a<br />
VHF message asking it to stop. Almost simultaneously<br />
crew members on board <strong>the</strong> tow shouted to <strong>the</strong> lead<br />
tug that <strong>the</strong> workboat had capsized.<br />
Based on information from <strong>the</strong> survivor and<br />
witnesses on <strong>the</strong> tow, it appears that <strong>the</strong> workboat<br />
skipper had intended to let <strong>the</strong> his boat drift into<br />
line with <strong>the</strong> stern <strong>of</strong> <strong>the</strong> passenger vessel as <strong>the</strong><br />
slack on <strong>the</strong> towline was taken up. It seems that <strong>the</strong><br />
workboat did not turn as fast as expected for when<br />
<strong>the</strong> weight came on <strong>the</strong> workboat was still lying at<br />
an angle <strong>of</strong> about 140° to <strong>the</strong> fore and aft line <strong>of</strong><br />
<strong>the</strong> tow. It appears that <strong>the</strong> skipper realising <strong>the</strong><br />
danger abruptly put his engines full ahead intending<br />
to swing his vessel into line with <strong>the</strong> tow. Before<br />
<strong>the</strong> workboat could turn <strong>the</strong> tow started to pull<br />
<strong>the</strong> workboat along with it. The workboat listed<br />
to starboard and a combination <strong>of</strong> <strong>the</strong> workboat’s<br />
engines, <strong>the</strong> river current and <strong>the</strong> forward motion<br />
<strong>of</strong> <strong>the</strong> tow dragged <strong>the</strong> starboard quarter under,<br />
with <strong>the</strong> result that <strong>the</strong> workboat capsized. The<br />
eye <strong>of</strong> <strong>the</strong> towline from <strong>the</strong> passenger vessel to <strong>the</strong><br />
workboat had been placed over <strong>the</strong> bitts. There was<br />
no means <strong>of</strong> releasing <strong>the</strong> towline in an emergency.<br />
Root Cause:<br />
Equipment design failure.<br />
Financial Cost:<br />
The workboat, although eventually refloated, was<br />
a constructive total loss. The measures taken to<br />
prevent pollution toge<strong>the</strong>r with <strong>the</strong> fees <strong>of</strong> lawyers<br />
and consultants exceeded US$14,000. The skipper’s<br />
family was compensated by <strong>the</strong> State Workers’<br />
Compensation scheme.<br />
Footnote: Following <strong>the</strong> incident ano<strong>the</strong>r<br />
Member <strong>of</strong> <strong>the</strong> Club designed an automatic quick<br />
release towing hook specifically for small craft/<br />
workboats. Full details <strong>of</strong> <strong>the</strong> ‘Detach-Matic’<br />
hook can be obtained from Navimar Corporation<br />
Ltee in Quebec, Canada, telephone number<br />
(418) 692 4830.<br />
Issue Date: 01/01/02<br />
Case No. 23773<br />
210 211
Personal Injury/Illness<br />
Personal Injury/Illness<br />
Delayed Action has Painful Result<br />
Handling <strong>of</strong> Heavy Cargo Load Without Rope Tails Leads to Crushed Fingers<br />
The Incident:<br />
This claim involved a work boat<br />
which developed an engine<br />
fault. The fault was reported<br />
to <strong>the</strong> General Manager, who<br />
subsequently arranged for <strong>the</strong><br />
company fitter to attend, although<br />
he could not do so immediately.<br />
The following morning, before <strong>the</strong><br />
fitter had attended and carried<br />
out <strong>the</strong> repairs, a new boatman<br />
took <strong>the</strong> boat out onto <strong>the</strong> water.<br />
Whilst manoeuvring alongside<br />
ano<strong>the</strong>r vessel <strong>the</strong> engine went<br />
astern instead <strong>of</strong> ahead, contrary<br />
to <strong>the</strong> control lever, and <strong>the</strong> boat<br />
landed heavily against <strong>the</strong> vessel<br />
causing <strong>the</strong> boatman to fall. This<br />
incident resulted in <strong>the</strong> crewman<br />
suffering multiple rib fractures and<br />
a broken arm.<br />
Observations:<br />
This incident would not have<br />
occurred if procedures had<br />
been in place to deal with <strong>the</strong><br />
reported fault. In particular<br />
no positive steps had been<br />
taken to prevent <strong>the</strong> boat from<br />
being used prior to <strong>the</strong> fault<br />
being rectified. The General<br />
Manager reportedly gave verbal<br />
instructions not to use <strong>the</strong> boat,<br />
but this clearly was not sufficient.<br />
When any item <strong>of</strong> machinery is<br />
known to be defective, positive<br />
action must be taken to prevent<br />
fur<strong>the</strong>r use until <strong>the</strong> problem<br />
has been rectified. This applies<br />
to all types <strong>of</strong> equipment no<br />
matter how important it is to a<br />
vessel’s operation.<br />
Root Cause:<br />
Inadequate maintenance<br />
procedures.<br />
Issue Date: 19/05/08<br />
Case No. 39892<br />
The Incident:<br />
This incident occurred on board<br />
a harbour craft servicing ships in<br />
<strong>the</strong> anchorage at Singapore. The<br />
vessel had carried a load <strong>of</strong> stores<br />
and spare gear out to <strong>the</strong> oceangoing<br />
vessel and was backloading<br />
a 14 ton piece <strong>of</strong> machinery. The<br />
small vessel was rolling slightly in<br />
<strong>the</strong> swell and while conditions<br />
were not ideal it was considered<br />
safe for <strong>the</strong> operation to proceed.<br />
The machine was lowered from<br />
<strong>the</strong> ocean-going ship to just<br />
above deck level where it was<br />
suspended while our Member’s<br />
crew adjusted its position. One<br />
<strong>of</strong> <strong>the</strong> crew members involved<br />
inadvertently placed his hand<br />
in a position where it could be<br />
trapped and realising <strong>the</strong> danger<br />
immediately tried to retract it,<br />
but his hand was caught by <strong>the</strong><br />
load. Fortunately he was able to<br />
pull his hand clear before <strong>the</strong> full<br />
pressure <strong>of</strong> <strong>the</strong> load came to bear.<br />
Never<strong>the</strong>less he suffered serious<br />
crush injuries to <strong>the</strong> middle and<br />
index fingers <strong>of</strong> his right hand.<br />
Observations:<br />
This incident illustrates <strong>the</strong><br />
dangers that crew members can<br />
be exposed to if <strong>the</strong>y have to<br />
work in close proximity to heavy<br />
loads being landed on deck. If this<br />
load had been fitted with rope<br />
tails it would have allowed <strong>the</strong><br />
crew members to remain at a safe<br />
distance from <strong>the</strong> load while final<br />
positioning was carried out.<br />
Root Cause:<br />
Inadequate safety procedures.<br />
Issue Date: 01/01/02<br />
Case No. 20766<br />
212 213
Operations<br />
Size does matter<br />
The Incident:<br />
This incident occurred when two tugs were employed<br />
in shifting a floating dry dock <strong>of</strong> approximately 3,400<br />
tonnes into deep water so that she could be ballasted<br />
down to sail out a vessel within.<br />
The operation required <strong>the</strong> dock to be manoeuvred<br />
across <strong>the</strong> port approach channel, down which a<br />
supply vessel was navigating. In order to give this<br />
vessel more sea room, <strong>the</strong> tugs towing <strong>the</strong> dock eased<br />
<strong>of</strong>f. The dock <strong>the</strong>n started to drift towards vessels<br />
moored at a nearby berth and despite <strong>the</strong> best efforts<br />
<strong>of</strong> <strong>the</strong> tugs, <strong>the</strong> dock continued towards <strong>the</strong> moored<br />
vessels, eventually making contact with one.<br />
Observations:<br />
Two factors played a part in <strong>the</strong> cause <strong>of</strong><br />
this incident. The bollard pull <strong>of</strong> <strong>the</strong> tugs was<br />
considered insufficient for <strong>the</strong> size <strong>of</strong> <strong>the</strong> dock.<br />
A strong current was flowing at <strong>the</strong> time <strong>of</strong> <strong>the</strong><br />
operation and <strong>the</strong> tugs were not <strong>of</strong> sufficient<br />
power to regain control. Secondly, nei<strong>the</strong>r <strong>the</strong><br />
dry dock operations department nor <strong>the</strong> tug<br />
masters took it upon <strong>the</strong>mselves to inform <strong>the</strong><br />
port control <strong>of</strong> <strong>the</strong> operation.<br />
Had this been done, <strong>the</strong> manoeuvre would<br />
have probably been delayed until <strong>the</strong> channel<br />
was clear or <strong>the</strong> inbound vessel prevented<br />
from entering <strong>the</strong> channel.<br />
Financial Cost:<br />
Whilst damage claimed was extensive we<br />
eventually concluded settlement in <strong>the</strong><br />
modest sum <strong>of</strong> US$14,737.<br />
Trading Area:<br />
Europe and Middle East<br />
Issue Date: 03/02/10<br />
Case No. 44485<br />
All in all <strong>the</strong> operation was very poorly planned.<br />
214 215
Section 7<br />
Barges<br />
217
Barges<br />
Operations<br />
You Get What You Pay For<br />
The Incident:<br />
This incident involved a dumb barge loading<br />
containers using her own gear. Whilst positioning a<br />
20 foot container on <strong>the</strong> barge <strong>the</strong> eye plate used<br />
to secure <strong>the</strong> topping lift block sheared away from<br />
<strong>the</strong> tripod mast. The container, derrick boom and<br />
gear all fell onto containers al<strong>read</strong>y loaded on <strong>the</strong><br />
barge. Three 40 foot and two 20 foot containers<br />
in addition to <strong>the</strong> one being loaded were damaged.<br />
Fortunately <strong>the</strong>re were no injuries to any <strong>of</strong> <strong>the</strong><br />
crew or stevedores.<br />
Observations:<br />
Investigations showed that <strong>the</strong> eye plate appears to<br />
have been repaired some time prior to <strong>the</strong> incident<br />
and <strong>the</strong> standard <strong>of</strong> <strong>the</strong> welding was very poor.<br />
There was minimal penetration in places and <strong>the</strong><br />
remainder <strong>of</strong> <strong>the</strong> welding was uneven. The surveyor<br />
was <strong>of</strong> <strong>the</strong> opinion that <strong>the</strong> repair work had been<br />
carried out by poorly trained personnel. Needless<br />
to say this is entirely unacceptable, especially<br />
when <strong>the</strong> safe working load (SWL) <strong>of</strong> <strong>the</strong> derrick<br />
(approximately 30 tons) is taken into consideration.<br />
Whenever major repairs are carried out on lifting<br />
gear or <strong>the</strong> associated fittings, a specialist company<br />
should be used that employs fully trained staff. Upon<br />
completion <strong>of</strong> <strong>the</strong>se repairs <strong>the</strong> gear should be<br />
pro<strong>of</strong> tested and a record entered in <strong>the</strong> Register <strong>of</strong><br />
Lifting Appliances and Cargo Handling Gear.<br />
Root Cause:<br />
Inadequate maintenance procedures.<br />
Financial Cost:<br />
US$14,541<br />
Issue Date: 22/02/07<br />
Case No. 43088<br />
218 219
Contact Us<br />
London Office<br />
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Charles Hume<br />
Chief Executive<br />
Email: charles.hume@shipowners.co.uk<br />
Skype: charles.hume<br />
Ralph Coton<br />
Business Services Director<br />
Email: ralph.coton@shipowners.co.uk<br />
Skype: ralph.d.coton<br />
Ian Edwards<br />
Underwriting Services Development Manager<br />
Email: ian.edwards@shipowners.co.uk<br />
Skype: ian.edwards11<br />
Adam Howe<br />
Underwriting Manager<br />
Email: adam.howe@shipowners.co.uk<br />
Skype: adam.howe18<br />
Britt Pickering<br />
Claims Manager<br />
Email: britt.pickering@shipowners.co.uk<br />
Skype: britt.pickering<br />
Louise Hall<br />
Loss Prevention Manager - London<br />
Email: louise.hall@shipowners.co.uk<br />
Skype: louise.hall4<br />
Simon Swallow<br />
Commercial Director<br />
Email: simon.swallow@shipowners.co.uk<br />
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Lawrence Aspinall<br />
Finance Director<br />
Email: lawrence.aspinall@shipowners.co.uk<br />
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Mark Harrington<br />
Underwriting Manager<br />
Email: mark.harrington@shipowners.co.uk<br />
Skype: mark.harrington83<br />
William Tobin<br />
Underwriting Manager<br />
Email: william.tobin@shipowners.co.uk<br />
Skype: william.tobin3<br />
Kevin Lowe<br />
Finance Manager<br />
Email: kevin.lowe@shipowners.co.uk<br />
Skype: kevin.lowe2983<br />
The <strong>Shipowners</strong>’ Protection Limited<br />
St Clare House, 30-33 Minories,<br />
London, EC3N 1BP<br />
Tel: +44 (0) 207 488 0911<br />
Fax: +44 (0) 207 480 5806<br />
Email: info@shipowners.co.uk<br />
David Heaselden<br />
Principal Officer / Director<br />
Loss Prevention Manager<br />
Email: david.heaselden@shipowners.com.sg<br />
Skype: davidh2009<br />
Steve Randall<br />
General Manager / Director<br />
Email: steve.randall@shipowners.com.sg<br />
Skype: sd.randall<br />
<strong>Shipowners</strong>’ Asia Pte Ltd<br />
6 Temasek Boulevard<br />
#36-05 Suntec Tower 4<br />
Singapore 038986<br />
Tel: +65 (65) 930420<br />
Fax: +65 (65) 930449<br />
Email: info@shipowners.com.sg<br />
www.shipownersclub.com<br />
Rosemary Adams<br />
General Manager / Head <strong>of</strong> Underwriting Vancouver Branch<br />
Email: rosemary.adams@shipownersclub.ca<br />
Skype: rosemary.adams<br />
<strong>Shipowners</strong>’ North America Protection Limited<br />
1157-409 Granville Street<br />
Vancouver, British Columbia<br />
V6C 1T2<br />
Tel: +1 604 681 5999<br />
Fax: +1 604 681 3946<br />
www.shipownersclub.com<br />
Luxembourg Office<br />
Pascal Herrmann<br />
General Manager<br />
Email: pascal.herrmann@shipowners.lu<br />
The <strong>Shipowners</strong>’ Mutual Protection<br />
& Indemnity Association<br />
16 Rue Notre-Dame<br />
L-2240 Luxembourg<br />
Tel: +352 229 7101<br />
Fax: +352 229 7102<br />
Email: info@shipowners.lu<br />
www.shipownersclub.com<br />
www.shipownersclub.com<br />
220
The <strong>Shipowners</strong>’ Protection Limited<br />
St Clare House, 30-33 Minories, London EC3N 1BP<br />
Tel: +44 (0)20 7488 0911 Fax: +44 (0)20 7480 5806<br />
Email: info@shipowners.co.uk<br />
www.shipownersclub.com<br />
October 2010