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dk nkf - Nordisk Konservatorforbund Danmark

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sold to the Falkland Islanders and remained as a<br />

floating storehouse. This was extremely fortunate<br />

because she would almost certainly have been sold<br />

for scrap if she had been too expensive to repair in<br />

the Northern hemisphere.<br />

In 1937 the harbour master became concerned<br />

about her condition. He ordered that she should be<br />

removed from the harbour and scuttled in a nearby<br />

cove (see Figure 11). There she stayed until, in<br />

1970, she was salvaged and returned to the Great<br />

Western Dockyard in Bristol, the dockyard that<br />

Brunel had built for her construction. Owned by<br />

a trust, operating as an independent museum, she<br />

was partially restored between 1970 and the mid<br />

1990s. At this point the trustees decided that she<br />

should in future be treated as a museum object, and<br />

that the traditional shipyard approaches used in her<br />

restoration should be replaced with conservation<br />

methods.<br />

Fort Brockhurst Bridge, by contrast, was built by<br />

the army from a kit of parts in 1862. Several similar<br />

examples, dating from the period, are located<br />

nearby. The bridge provides access over a moat to<br />

Fort Brockhurst, one of a number of forts built in<br />

the 1860s to protect Portsmouth and its strategically<br />

important harbour. The fort remains physically<br />

largely unaltered, although it currently serves as a<br />

store for objects from English Heritage’s extensive<br />

reserve collections. These include stonework,<br />

textiles, jewellery, and furniture from many periods.<br />

It was crucial that the fort retain safe vehicular<br />

access.<br />

Condition and Treatment ~<br />

Fort Brockhurst Bridge<br />

The bridge had lasted for almost 150 years before<br />

receiving conservation treatment. As can be seen in<br />

Figure 2, the bridge was re-inforced on at least two<br />

occasions before receiving full conservation and<br />

restoration to its original function in 2004.<br />

The bridge was constructed from a combination of<br />

wrought and cast iron. Generally, cast iron was used<br />

for elements such as the support columns, hand-rail<br />

stanchions, bridge-deck plates and the landing beam<br />

of the drawbridge. Riveted wrought-iron beams were<br />

Figure 3. Corrosion of the wrought iron<br />

used where tensile strength was required. The owners<br />

of the bridge, English Heritage, had specified the<br />

design life of the treatment should be as long as was<br />

reasonably practicable. For this reason, it was decided<br />

to dismantle everything except the cast iron columns<br />

and treat the bridge in the conservation workshops.<br />

The main conservation issues to be addressed were<br />

corrosion of the wrought iron and some fracturing<br />

of the cast-iron elements.<br />

The main structural elements of the bridge were<br />

composite riveted wrought iron I-beams. These<br />

were constructed from plates and angles.<br />

The horizontal plates, particularly the upper ones,<br />

were heavily corroded. It was decided to de-rivet<br />

the beam and to cut down plate No. 2 to become a<br />

new plate No. 1. A new plate No. 2 was made from<br />

mild steel because wrought iron is in very short<br />

supply in the UK and it can be next to impossible<br />

to obtain high-quality replacement material in the<br />

large sizes.<br />

The engineers had determined that if more than 60%<br />

of the thickness of a material remained then it could<br />

be left un-repaired. Minor areas that were below this<br />

threshold (small holes for example) were repaired<br />

by welding in small patches or the application of<br />

weld metal to build up the required thickness.<br />

Cast-iron elements were visually inspected and dye<br />

penetration tests were conducted if fractures were<br />

suspected. Fractured cast-iron elements were metal-<br />

stitched together.<br />

All iron elements were cleaned to SA3 and zinc<br />

metal-sprayed.<br />

207

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