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Garden Whistle Apr 2012 - Sandman.org.nz

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The <strong>Garden</strong> <strong>Whistle</strong> - <strong>Apr</strong>il <strong>2012</strong><br />

A<br />

5<br />

Soldering it all together<br />

A jig was made by taking a small block of wood.<br />

Into this was drilled a 1/8 hole into which was inserted<br />

a short length of 1/8 dowel .<br />

The buffer face is placed over the dowel to rest on the<br />

block of wood.<br />

Then place over this ,the hollow rectangle with the<br />

partly cut away and trimmed off square, check that all<br />

is arranged okay. Solder it all together with a hot iron.<br />

The wood will burn , avoid using MDF for the jig<br />

A<br />

Once soldered the buffer head was roughly trimmed<br />

off, then filed to give it some shape .<br />

The 1/8 square bar had a slot cut into it, once again to<br />

allow space to get a file in.<br />

6<br />

To ease the soldering ,and stop the assembly falling apart<br />

when heated, small balls of wet tissue paper can be placed<br />

around delicate parts to act as a heat sink, and keep parts<br />

in place<br />

A<br />

B<br />

The peg was changed in the<br />

jig to a much shorter one.<br />

The formed head was then<br />

placed back on the jig. The<br />

slotted 1/8 bar was the fed<br />

into the head<br />

A<br />

B<br />

C<br />

7<br />

8<br />

and pushed in to the face. The assembly was then<br />

checked for squareness . All was soldered in place<br />

with a hot iron .This forms the shank.<br />

To replicate mid production buffers ,a gusset was required.<br />

(Choose which is to be the top)<br />

For this the 3/32 x 1/32 strip was used. One end is<br />

filed square to fit then soldered in place ,the step is<br />

then repeated for the gusset on the other side.<br />

These were trimmed and filed to shape later when<br />

satisfied they were in the correct place.<br />

( this part of the exercise can be frustrating as parts<br />

may want to let go ,use of a heat sink and patience<br />

was required ,it all works out in the end)<br />

A strip op 3/32 x 1/32 strip was soldered to the bottom<br />

of the buffer head, two holes of 1mm were then<br />

drilled in it to provide a location for the bridle to fit.<br />

The ‘U’ was then cut out of the face and shaped.<br />

Page 19

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