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Asphalt Review - Volume 29 Number 2 (June / July 2010)

Asphalt Review - Volume 29 Number 2 (June / July 2010)

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BITUMEN<br />

STABILISATION IN<br />

SOUTH AFRICA<br />

To understand bitumen stabilisation technology (materials<br />

treated with bitumen emulsion or foamed bitumen), it is<br />

important to know the history of this technology.<br />

BSMs have been used in South Africa for more than 30 years.<br />

The concept of emulsion treatment came to the fore in the<br />

1970s when a newly constructed freeway suffered a catastrophic<br />

premature failure. The failed cemented base material was retreated<br />

with bitumen emulsion and most of those sections are<br />

still in a satisfactory condition today.<br />

The following paper, prepared by DC Collings, Loudon<br />

International, South Africa (davecol@iafrica.com), was also<br />

featured at AAPA’s 13th International Flexible Pavements<br />

Conference.<br />

Condensed version - full version available from Conference<br />

papers 2009 - aapa@asn,com.au<br />

The advent of foamed bitumen in South Africa<br />

During 1993, in pursuit of an alternative to bitumen emulsion,<br />

a Joint Venture (JV) between a large construction company,<br />

a small design firm and a foreign manufacturing company<br />

imported a specialised 400 t/hr foamed bitumen mixing plant<br />

from the foreign company. The mixing plant was duly established<br />

on site in April 1994. The anticipated construction period was<br />

four weeks.<br />

From the outset, everything that could have gone wrong did<br />

go wrong. On the odd occasion when foam was produced, the<br />

resulting bitumen stabilised material allowed the 150mm thick<br />

base layer to be successfully paved. A rudimentary method<br />

for operating the plant was eventually developed, allowing a<br />

satisfactory product to be mixed at an exceedingly slow rate.<br />

Despite this, the road is still in good condition 15 years later,<br />

in spite of the abusive loading it has received from timber<br />

haulage.<br />

Two major benefits did accrue from these expensive lessons:<br />

• foamed bitumen was shown to be a viable and highly<br />

attractive substitute for bitumen emulsion as a stabilising<br />

agent (the product was good, the equipment was flawed);<br />

and<br />

• an in-depth understanding of the problems encountered<br />

when using an expansion chamber to produce foamed<br />

bitumen.<br />

The new “properly engineered” system<br />

Following this project and a short but intensive research<br />

and development effort by the manufacturer’s engineering<br />

design team, the prototype spraybar for producing foamed<br />

bitumen was subjected to a series of trials in Germany in<br />

November 1995. The system was then mounted on a newgeneration<br />

recycler and shipped out to South Africa for<br />

field trials. Six weeks of continuous work followed before<br />

the Germans declared that the system was satisfactory. The<br />

system currently manufactured by this company, some 13<br />

years later, is exactly the same.<br />

Bitumen stabilisation in South Africa<br />

Within a year of completing these trials, four South African<br />

contractors had purchased large recycling machines equipped to<br />

apply foamed bitumen. These contractors quickly identified the<br />

economic advantages to be gained by substituting foamed bitumen<br />

for bitumen emulsion in tenders calling for the construction of<br />

an emulsion treated base (ETB). As a result, several contracts<br />

were awarded in favour of foamed bitumen, in spite of the Road<br />

Authority’s uncertainty as to whether or not foamed bitumen was<br />

indeed as effective as bitumen emulsion.<br />

Subsequent to developing the full-scale system for mounting on<br />

large recyclers, a small laboratory unit was developed to support<br />

the design aspect of this new technology.<br />

TG2 Second Edition and technology development<br />

Following the successful use of foamed bitumen the emulsion<br />

manufacturers supported the development of two documents<br />

through SABITA. However, these imposed a number of<br />

limitations. Subsequently a technical guidelines document<br />

TG2 was developed and released in 2002.<br />

Subsequently experience in South Africa and overseas<br />

highlighted deficiencies in TG2 and work was done to review<br />

those guidelines.<br />

This review took five years to complete with funding<br />

provided by SABITA and Gautrans and the new edition of<br />

TG2 was published in May 2009. It was titled TG 2 Second<br />

Edition, Bitumen Stabilised Materials, A Guideline for the<br />

Design and Construction of Bitumen Emulsion and Foamed<br />

Bitumen Stabilised Materials.<br />

TG2 Second Edition therefore replaces Sabita’s Manuals 14<br />

and 21 as well as the original TG2. Regardless of whether<br />

bitumen emulsion or foamed bitumen is applied as the<br />

stabilising agent, the same mix design and pavement design<br />

procedures are applicable to both and the new method for<br />

classifying BSMs takes no account of which stabilising agent<br />

was used in the mix.<br />

BSM CHARACTERISTICS AND<br />

PERFORMANCE<br />

BSMs are pavement materials that are treated with either<br />

bitumen emulsion or foamed bitumen. The materials treated<br />

are either those recovered from an existing pavement or fresh<br />

materials. Granular materials, previously cement treated<br />

materials or reclaimed asphalt (RA) layers are included.<br />

Where an existing pavement is recycled, old seals or asphalt<br />

surfacing is usually mixed with the underlying layer and<br />

treated to form a new base or sub-base layer.<br />

ROADS JUNE <strong>2010</strong>/JULY <strong>2010</strong> <strong>29</strong>

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