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Commuter Rail AC Electrification Load-Flow Simulation Report - RTD

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<strong>Commuter</strong> <strong>Rail</strong> <strong>AC</strong> <strong>Electrification</strong> <strong>Load</strong>-<strong>Flow</strong> <strong>Simulation</strong> <strong>Report</strong> Revision 1<br />

below the ampacity of the overhead system conductors, as shown in Table 11, and annealing of<br />

the conductors is highly unlikely, the predicted conductor temperatures were not calculated.<br />

Table 11 - Conductor Ampacities and RMS Currents – All System In Service, Two<br />

Transformers in Sandown Substation, Two Transformers in Argo Substation<br />

Substation<br />

Sandown<br />

Argo<br />

Feeder<br />

Approximate Ampacity (A) Maximum RMS Current (A)<br />

Feeder Catenary Feeder Catenary<br />

Track 1-West<br />

3.4 23.2<br />

Track 2-West 3.4 36.0<br />

Track 1-East 23.8 75.6<br />

Track 2-East 23.8 83.8<br />

730 870<br />

Track 1-West 9.4 57.6<br />

Track 2-West 9.4 53.0<br />

Track 1-East 38.6 70.2<br />

Track 2-East 38.6 77.2<br />

Results for two transformers in Sandown substation, and one transformer in Argo substation are<br />

not presented, as the results are not substantially different from the results shown.<br />

8.5 SUBSTATION POWER DEMANDS<br />

The substation transformer power demand for Sandown and Argo substations are shown in the<br />

following Tables. In order to define the transformer continuous and overload ratings, the onesecond<br />

power demands were averaged over 2-hour, 1 hour, 15-minute, and 1-minute time<br />

intervals, as shown in Tables 12 through 14. For the power utility billing interval, 15 minutes,<br />

the power factor is also given.<br />

02/27/2009 FRSC Page 24 of 250

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