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June 2002 - Rolls-Royce Owners' Club of Australia (Victoria Branch)

June 2002 - Rolls-Royce Owners' Club of Australia (Victoria Branch)

June 2002 - Rolls-Royce Owners' Club of Australia (Victoria Branch)

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The picture shows three holes on the periphery. The centre one is threaded and receives the<br />

retaining bolt which passes<br />

throught the base <strong>of</strong> the main<br />

casing in the control valve area<br />

and the other two are the<br />

repective feed holes to the front<br />

and rear clutches.<br />

Examination <strong>of</strong> the main casing<br />

showed that the area where the<br />

above retaining bolt passes<br />

through the box was<br />

significantly distorted most<br />

probably through over<br />

tightening. This allowed the<br />

central carrier to move around<br />

in the box losing oil pressure to<br />

the front clutch and allowing<br />

the it to slip. Fortunately this was overcome by a thick bearing washer in the mounting hole,<br />

a new bolt and a replacement central bearing carrier. The finished job was reportedly<br />

excellent.<br />

A LITTLE MORE<br />

HOUSEKEEPING<br />

No prizes for identifying this as the<br />

space left after removing the<br />

windscreen washer reservoir on the<br />

right hand side <strong>of</strong> a Spirit engine bay.<br />

These little nooks harbour all sorts <strong>of</strong><br />

things that work their way up from the<br />

road and from droppings by people<br />

working on the engine. A good<br />

vacuum and then a careful wipe with a<br />

metho soaked cloth should be<br />

beneficial. It also allows wiring to be<br />

checked for chafing and loose connections. This car also had both mounting lugs broken <strong>of</strong>f<br />

the reservoir which were glued on with a standard cyanate glue. Whilst out the reservoir was<br />

cleaned <strong>of</strong> 16 years <strong>of</strong> sludge and sediment. The pump intake for the washer was found to be<br />

partially blocked with this stuff and the lines to jets benefitted from a good blow out.<br />

174

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