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ORNL-4191 - the Molten Salt Energy Technologies Web Site

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The rate-of-fill interlocks, including <strong>the</strong> pneumatic<br />

instrument components in <strong>the</strong> drain-tank<br />

weighing system, were removed from <strong>the</strong> control<br />

circuits for <strong>the</strong> fuel drain tank helium supply valve.<br />

Experience had shown that <strong>the</strong>se interlocks, intended<br />

to limit <strong>the</strong> rate at which fuel could be<br />

transferred to <strong>the</strong> core, were not required, since<br />

physical restrictions in <strong>the</strong> helium supply positively<br />

prevent filling as fast as <strong>the</strong> design set<br />

point on <strong>the</strong> interlock.<br />

Four new photoengraved graphic panels incorporating<br />

recent circuit changes were installed on <strong>the</strong><br />

control and safety circuit jumper board. The main<br />

control board graphics were also revised to show<br />

changes in <strong>the</strong> fuel off-gas system.<br />

Test circuits were originally provided to check<br />

<strong>the</strong> operability of electronic safety instruments on<br />

fuel loop pressure and overflow tank level. These<br />

were revised to make it possible to observe <strong>the</strong><br />

value of <strong>the</strong> test signal current at which <strong>the</strong> relays<br />

operate.<br />

The measuring range of <strong>the</strong> matrix-type flow element<br />

on <strong>the</strong> upper seal gas flow from <strong>the</strong> coolant<br />

pump was increased from 5 to 12 literdhr. This<br />

was to keep <strong>the</strong> instrument 011 scale at pump bowl<br />

pressures higher than originally anticipated. A new<br />

capillary flow element was designed to replace <strong>the</strong><br />

element that measures <strong>the</strong> reactor cell evacuation<br />

rate, raising <strong>the</strong> range from 1 to 4 liters/min.<br />

To avoid reducing <strong>the</strong> reactor system helium<br />

supply pressure below <strong>the</strong> minimum limit when<br />

large quantities of helium are required for fuel<br />

processing, <strong>the</strong> fuel processing system helium<br />

supply line was removed from <strong>the</strong> 40-psig supply<br />

header and reconnected upstream to <strong>the</strong> 250-psig<br />

main supply header. Pressureregulating instru-<br />

ments were installed.<br />

To provide more information to <strong>the</strong> operator, 20<br />

additional pairs of thrrmocoiiple lead wires were<br />

installed between <strong>the</strong> vent house and <strong>the</strong> data<br />

logger. Connections at <strong>the</strong> patch panel were made<br />

available by removing unused lead wires from some<br />

radiator <strong>the</strong>rmocouples. A new conduit €or <strong>the</strong>se<br />

lead wires was also installed between <strong>the</strong> vent<br />

house and <strong>the</strong> existing cable trough in <strong>the</strong> coolant<br />

drain cel.1.

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