ORNL-4191 - the Molten Salt Energy Technologies Web Site
ORNL-4191 - the Molten Salt Energy Technologies Web Site
ORNL-4191 - the Molten Salt Energy Technologies Web Site
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The rate-of-fill interlocks, including <strong>the</strong> pneumatic<br />
instrument components in <strong>the</strong> drain-tank<br />
weighing system, were removed from <strong>the</strong> control<br />
circuits for <strong>the</strong> fuel drain tank helium supply valve.<br />
Experience had shown that <strong>the</strong>se interlocks, intended<br />
to limit <strong>the</strong> rate at which fuel could be<br />
transferred to <strong>the</strong> core, were not required, since<br />
physical restrictions in <strong>the</strong> helium supply positively<br />
prevent filling as fast as <strong>the</strong> design set<br />
point on <strong>the</strong> interlock.<br />
Four new photoengraved graphic panels incorporating<br />
recent circuit changes were installed on <strong>the</strong><br />
control and safety circuit jumper board. The main<br />
control board graphics were also revised to show<br />
changes in <strong>the</strong> fuel off-gas system.<br />
Test circuits were originally provided to check<br />
<strong>the</strong> operability of electronic safety instruments on<br />
fuel loop pressure and overflow tank level. These<br />
were revised to make it possible to observe <strong>the</strong><br />
value of <strong>the</strong> test signal current at which <strong>the</strong> relays<br />
operate.<br />
The measuring range of <strong>the</strong> matrix-type flow element<br />
on <strong>the</strong> upper seal gas flow from <strong>the</strong> coolant<br />
pump was increased from 5 to 12 literdhr. This<br />
was to keep <strong>the</strong> instrument 011 scale at pump bowl<br />
pressures higher than originally anticipated. A new<br />
capillary flow element was designed to replace <strong>the</strong><br />
element that measures <strong>the</strong> reactor cell evacuation<br />
rate, raising <strong>the</strong> range from 1 to 4 liters/min.<br />
To avoid reducing <strong>the</strong> reactor system helium<br />
supply pressure below <strong>the</strong> minimum limit when<br />
large quantities of helium are required for fuel<br />
processing, <strong>the</strong> fuel processing system helium<br />
supply line was removed from <strong>the</strong> 40-psig supply<br />
header and reconnected upstream to <strong>the</strong> 250-psig<br />
main supply header. Pressureregulating instru-<br />
ments were installed.<br />
To provide more information to <strong>the</strong> operator, 20<br />
additional pairs of thrrmocoiiple lead wires were<br />
installed between <strong>the</strong> vent house and <strong>the</strong> data<br />
logger. Connections at <strong>the</strong> patch panel were made<br />
available by removing unused lead wires from some<br />
radiator <strong>the</strong>rmocouples. A new conduit €or <strong>the</strong>se<br />
lead wires was also installed between <strong>the</strong> vent<br />
house and <strong>the</strong> existing cable trough in <strong>the</strong> coolant<br />
drain cel.1.