ORNL-4191 - the Molten Salt Energy Technologies Web Site
ORNL-4191 - the Molten Salt Energy Technologies Web Site
ORNL-4191 - the Molten Salt Energy Technologies Web Site
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MSRE, details of some of <strong>the</strong> equipment, and descriptions<br />
of specific problems. The demonstrations<br />
involved <strong>the</strong> viewing equipment, <strong>the</strong> remote<br />
cranes, <strong>the</strong> portable maintenance shield, and some<br />
of <strong>the</strong> long-handled tools. Practice sessions on<br />
core sample removal and replacement served both to<br />
train personnel and to shake down <strong>the</strong> equipment.<br />
The planning part of <strong>the</strong> preparation involved<br />
<strong>the</strong> writing or updating of step-by-step procedures<br />
fGr each job. These procedures were used to draw<br />
up lists of requiied tools, equipment, and material,<br />
and to estimate time and manpower requirements.<br />
Possible problem areas were recognized €or prior<br />
testing and mockup practice. Before <strong>the</strong> shutdown<br />
began, <strong>the</strong> procedures were used to provide information<br />
to <strong>the</strong> foremen and <strong>the</strong> working crews.<br />
A large effort was required to put all <strong>the</strong> physical<br />
equipment into readiness. This meant fabrication<br />
of new equipment; cleaning, maintenance, and<br />
repair of existing equipment; and procurr?rnerit of<br />
some special items. Numerous long-handled tools,<br />
containers €or hot pulls, materials for contamination<br />
control, handling equipment, and devices for<br />
shielding, lighting, and viewing were prepared.<br />
Evaluation of Remote Maintenance After Run 11<br />
The maintenance work during this ::hutdown was<br />
done on a two-crew, two-shift-per-day basis, Al-<br />
though <strong>the</strong>re were drawbacks, such as spreading<br />
more thinly <strong>the</strong> knowledgeable personnel and lost<br />
motion at shift change, <strong>the</strong>' work proceeded safely<br />
and smoothly. Radiation levels were about <strong>the</strong><br />
sane as at <strong>the</strong> last shutdown and did not require<br />
any changes in procedure. Some bo<strong>the</strong>rsome de-<br />
!ays wete caused by breakdowns of <strong>the</strong> cranes and<br />
maintenance shield, but <strong>the</strong> schedule was not<br />
seriously affected. Comments on individual jobs<br />
follow.<br />
Removing and replacing <strong>the</strong> sample array in <strong>the</strong><br />
core was <strong>the</strong> most difficult task of <strong>the</strong> shutdown,<br />
involving as it did an extremely intense source<br />
of radiation and contamination. The standpipe<br />
above <strong>the</strong> reactor access flange contained <strong>the</strong><br />
assembly and maintained an inert atmosphere on<br />
it. Before <strong>the</strong> operation a new charcoal filter<br />
was installed iri <strong>the</strong> vent line from <strong>the</strong> standpipe<br />
to prevent iodine releases. The procedure used<br />
previously was changed to minimize <strong>the</strong> time of<br />
exposure for <strong>the</strong> uncontained sample within <strong>the</strong><br />
stkindpipe and to provide complete containment<br />
37<br />
and shielding during <strong>the</strong> transfer of <strong>the</strong> sample<br />
from <strong>the</strong> standpipe to <strong>the</strong> shielded carrier. Two<br />
unanticipated situations arose. The bushing which<br />
supports <strong>the</strong> sample assembly arid which is supposed<br />
to stay locked in position in <strong>the</strong> vessel<br />
outlet strainer actually came out on <strong>the</strong> sample<br />
basket. After visually ascertaining that <strong>the</strong><br />
strainer was not damaged, a new bushing was<br />
inserted. Ulieri difficulty was encountered later<br />
in obtaining a satisfactory seal while replacing<br />
<strong>the</strong> reactor access flange, four bolts were replaced,<br />
and all <strong>the</strong> threads on <strong>the</strong> nut:; were<br />
cleaned by tapping. This permitted an increase<br />
in gasket loading which eliminated <strong>the</strong> leak.<br />
Iiemoval, repair, inspection, and replacement of<br />
a control rod drive went smoothly.<br />
The leaking east space cooler was disconnected<br />
through <strong>the</strong> portable maintenance shield and <strong>the</strong>n<br />
was removed by using <strong>the</strong> crane, television, and<br />
remotely operated maintenance-shield slide from<br />
<strong>the</strong> maintenance control rooin. A new unit, reassembled<br />
on <strong>the</strong> old frame, was reinstalled <strong>the</strong> same<br />
way without excessive difficulty.<br />
The metallurgical specimens which hang in <strong>the</strong><br />
reactor vessel furnace were replaced without difficulty.<br />
The carrier for <strong>the</strong> core samples was<br />
used to transport <strong>the</strong> specimens to <strong>the</strong> hot cell.<br />
'The fresh neutron source was transferred from a<br />
carrier and placed in <strong>the</strong> source t.ube (,on top of<br />
<strong>the</strong> original source) without incident..<br />
Visual inspection in <strong>the</strong> cell was by use of a<br />
periscope, binoculars, and remote television.<br />
Thermocouple junction boxes were tested, and<br />
four <strong>the</strong>rmocouples were plugged into a spare disconnect<br />
box by using long-handled tools through<br />
<strong>the</strong> maintenance shield.<br />
As a result of <strong>the</strong> experience during this shutdown,<br />
procedures were reviewed and revised<br />
where desirable, and some tools and equipment<br />
were revised or overhauled. The television camera<br />
mounts were changed for greater flexibility, and<br />
revisions were made to <strong>the</strong> track and to <strong>the</strong> roller<br />
and guide bearings on <strong>the</strong> maintenance shield.<br />
Repair of Sampler-Enricher and Recovery of Latch<br />
After <strong>the</strong> failure of <strong>the</strong> sampler-enricher drive<br />
unit, a lead carrier was built, and detailed pro-<br />
cedures for <strong>the</strong> removal of <strong>the</strong> delective unit were<br />
prepared and reviewed. The actual removal of<br />
this component was without incident.