ORNL-4191 - the Molten Salt Energy Technologies Web Site
ORNL-4191 - the Molten Salt Energy Technologies Web Site
ORNL-4191 - the Molten Salt Energy Technologies Web Site
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failure that brought run 12 to an end. Between<br />
March 1 and August 5 <strong>the</strong>re were 11.1 operations,<br />
as follows:<br />
<strong>Salt</strong> samples 71<br />
Freeze-valve samples of cover gas 6<br />
Exposure of graphite to salt and cover gas<br />
Beryllium additions 6<br />
Uranium additions 27<br />
Of <strong>the</strong> salt samples, 14 were 50-g samples and 2<br />
were taken in special three-compartment capsules.<br />
The special samples are described in <strong>the</strong> section<br />
“Reactor Chemistry,” These operations brought<br />
<strong>the</strong> total, since <strong>the</strong> sampler-enricher was installed<br />
in March 1965, to 114 uranium enrichments and<br />
279 samples and special exposures.<br />
The uranium additions, <strong>the</strong> first made with <strong>the</strong><br />
reactor critical, provided information on mixing<br />
between salt in <strong>the</strong> sample enclosure and <strong>the</strong><br />
main circulating stream. Response of <strong>the</strong> ieactivity<br />
(Fig. 1.7) revealed a time constant close<br />
to that for mixing between <strong>the</strong> pump bowl and <strong>the</strong><br />
main stream, indicating rapid melting of <strong>the</strong> enriching<br />
salt and good circulation through <strong>the</strong><br />
sample enclosure.<br />
Near <strong>the</strong> end of run 11 <strong>the</strong> manipulator arm and<br />
boot assembly was replaced after a small leak<br />
appeared in one ply of <strong>the</strong> boot. The arm was<br />
quite contaminated (300 r/hr at 3 in.), but it was<br />
successfully decontaminated and saved for possible<br />
future use (see p. 40). At <strong>the</strong> start of<br />
run 12, one ply of <strong>the</strong> boot was ruptured when excessive<br />
differential pressure was inadvertently<br />
applied, and again <strong>the</strong> assembly V J ~ replaced.<br />
S<br />
This time a slightly different boot was used. The<br />
new boot was thicker and more durable (at <strong>the</strong><br />
expense of ease of manipulation), and <strong>the</strong> outside<br />
was coated with a white plastic spray which effectively<br />
improved viewing in <strong>the</strong> sampler by decreasing<br />
light absorption.<br />
One of <strong>the</strong> beryllium addition capsules was<br />
dropped while it was being removed from <strong>the</strong> 1-C<br />
area with <strong>the</strong> manipulator. The capsule fell onto<br />
<strong>the</strong> gate of <strong>the</strong> operational valve, where it was<br />
retrieved by a inagnet lowered on a cable.<br />
Enriching capsules occasionally jammed iii <strong>the</strong><br />
transport container until <strong>the</strong> difficulty was eliminated<br />
by increasing <strong>the</strong> length of <strong>the</strong> cavity in <strong>the</strong><br />
disposable portiori to give more room for <strong>the</strong> long<br />
capsule and attached key.<br />
1<br />
32<br />
The neoprene seals on <strong>the</strong> 1-C access port began<br />
to show increased leakage, possibly due to<br />
radiation damage. Fission products, mostly <strong>the</strong><br />
species found in cover-gas sarnples, produced<br />
radiation levels in area 3A of several hundred<br />
rads per hour. Before run 12, <strong>the</strong> radiation in this<br />
area was reduced a factor of 10 by using <strong>the</strong> manip-<br />
ulator to wipe down surfaces with damp sponges.<br />
In run 12, increased leakage from <strong>the</strong> buffer zone<br />
between <strong>the</strong> seals on <strong>the</strong> 1-C access port was<br />
met by increasing <strong>the</strong> size of <strong>the</strong> helium supply<br />
flow restrictor so that a satisfactory buffer pressure<br />
could be maintained. Operation of <strong>the</strong> pneumatic<br />
clamps on <strong>the</strong> 1-C access door occasionally re-<br />
sulted in gaseous fission products being vented<br />
through <strong>the</strong> operator vent line. A small charcoal<br />
filter was added to prevent this activity from<br />
reach;-ng <strong>the</strong> stack.<br />
As described on p. 15, a situation developed on<br />
August 5 that led to a shutdown of <strong>the</strong> reactor and<br />
replacement of <strong>the</strong> 1-C assembly. It now appears<br />
that <strong>the</strong> trouble started when <strong>the</strong> latch hung at<br />
<strong>the</strong> maintenance valve. Indications were that both<br />
isolation valves were fully open and that <strong>the</strong><br />
capsule key was hanging properly in <strong>the</strong> latch at<br />
<strong>the</strong> outset; so <strong>the</strong> exact cause of <strong>the</strong> hangup is<br />
not known. But <strong>the</strong>re is convincing evidence that<br />
<strong>the</strong> drive cable was severed by <strong>the</strong> operational-<br />
valve gate while <strong>the</strong> latch was at <strong>the</strong> maintenance<br />
valve. The length of <strong>the</strong> latch and remaining drive<br />
cable (Fig. 1.3) equals <strong>the</strong> distance from <strong>the</strong><br />
maintenance valve up to <strong>the</strong> gate of <strong>the</strong> operational<br />
valve, and <strong>the</strong> cable end appeared to have been<br />
cut. It was believed that <strong>the</strong> operational valve<br />
was practically closed before substantial resist-<br />
ance was felt, but it would have been easy to<br />
mistake <strong>the</strong> torque and motion involved in shear-<br />
ing <strong>the</strong> cable and seating <strong>the</strong> valve for simply<br />
seating <strong>the</strong> valve. (The tiandwlieel torque re-<br />
quired to shear <strong>the</strong> cable was subsequently cal-<br />
culated to be less than 100 in.-lb.)<br />
Once before, in December 1965, <strong>the</strong> latch ap-<br />
parently hung up at one of <strong>the</strong> isolation valves,<br />
causing <strong>the</strong> drive cable to coil up in <strong>the</strong> 1-C area<br />
and in <strong>the</strong> drive unit. Following that occasion,<br />
<strong>the</strong> travel of <strong>the</strong> valve gates on opening was in-<br />
creased slightly, and when <strong>the</strong> 1-C assembly was<br />
removed after <strong>the</strong> recent trouble, <strong>the</strong> valve gates<br />
were observed to completely clear <strong>the</strong> sample tube.<br />
The valves were also observed to function reli-<br />
ably, so no changes were made.