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ORNL-4191 - the Molten Salt Energy Technologies Web Site

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(Yorkmesh) was % 275°F when <strong>the</strong> particle trap<br />

was first used and -380'F near <strong>the</strong> end of run 12.<br />

The temperatures decrease rapidly when <strong>the</strong> reactor<br />

power is reduced, however, and <strong>the</strong> zeropower<br />

steady-state temperatures are essentially<br />

unchanged. These effects indicate <strong>the</strong> accumulation<br />

of some material, presumably organic, on <strong>the</strong><br />

filtering media that enhances <strong>the</strong> retention of<br />

short-lived fission products.<br />

Main Charcoal Beds. - The performance of <strong>the</strong><br />

charcoal beds in holding up noble-gas fission<br />

products has continued to be satisfactory. The<br />

gradual development of restrictions at <strong>the</strong> inlet<br />

ends of <strong>the</strong> beds has also continued, but this has<br />

not limited <strong>the</strong> reactor operation in any way, since<br />

effective measures can be taken to reduce <strong>the</strong><br />

restriction when necessary.<br />

Run 11 was started in January 1967 with <strong>the</strong><br />

charcoal bed sections 1A and 1B in service with<br />

an initial pressure drop of 2.5 psi at normal offgas<br />

flow. The pressure drop increased very slowly,<br />

reaching 7 psi on March 29, two months after <strong>the</strong><br />

start of <strong>the</strong> run, At that time <strong>the</strong> standby beds,<br />

2A and 2B, were put in service, and <strong>the</strong> restricted<br />

sections were valved out. The pressure drop<br />

across <strong>the</strong>se sections built up from 2.6 to 9 psi<br />

in only ten days. We <strong>the</strong>n cleared <strong>the</strong> restrictions<br />

from all four sections by forcing clean helium<br />

through sections 2A and 2B in <strong>the</strong> normal flow<br />

direction and heating <strong>the</strong> inlet ends of sections<br />

1A and 1B with previously installed6 electric<br />

heaters. These operations did not require a reactor<br />

shutdown but only a temporary lowering of<br />

<strong>the</strong> water level in <strong>the</strong> charcoal bed pit to allow<br />

<strong>the</strong> heaters to function.<br />

After <strong>the</strong> restrictions in both sets of beds had<br />

been cleared, sections 1A and 1B were put back<br />

in service. In <strong>the</strong> ensuing three weeks <strong>the</strong> pressure<br />

drop increased from 2.4 to 3.5 psi. At that<br />

time, we decided to increase <strong>the</strong> helium purge<br />

flow by 1 liter/min to see if <strong>the</strong> xenon poisoning<br />

would be affected by lower concentrations in <strong>the</strong><br />

fuel pump gas space. To accommodate <strong>the</strong> higher<br />

gas flow without an increase in fuel pump pressure,<br />

sections 1A and 1B were valved out and 2A<br />

and 2B were put in service. The next day section<br />

1A had to be reopened to keep <strong>the</strong> fuel pump pressure<br />

at 5 psig. The normal purge flow was restored<br />

after three days, and, just before <strong>the</strong> power<br />

shutdown at <strong>the</strong> end of run 11, <strong>the</strong> partial restric-<br />

61bid., pp. 30-31.<br />

28<br />

tions in all four beds were again removed by heat-<br />

ing sections 1A and 1B and forward blowing sec-<br />

tions 2A and 2B.<br />

Owing to <strong>the</strong> success of <strong>the</strong> heaters in clearing<br />

<strong>the</strong> restrictions from sections 1A and lB, we in-<br />

stalled similar heaters at <strong>the</strong> inlets of sections<br />

2A and 2B during <strong>the</strong> shutdown between runs 11<br />

and 12. The differential pressure transmitter<br />

that senses charcoal bed pressure drop directly<br />

was also replaced. This instrument had failed<br />

earlier, possibly because of <strong>the</strong> pressure differ-<br />

ences imposed during blowouts of <strong>the</strong> charcoal<br />

beds. However, all <strong>the</strong>se pressure differences<br />

were within <strong>the</strong> specified overrange capability of<br />

<strong>the</strong> instrument.<br />

Power operation in run 12 was started with sec-<br />

tions 1A and 1B in service. The gradual increase<br />

in pressure drop made it necessary to change to<br />

sections 2A and 2B after about three weeks. The<br />

pressure drop across <strong>the</strong> second sections reached<br />

an unsatisfactory level after only six days. Then<br />

<strong>the</strong> restrictions were cleared from all four sections<br />

by heating <strong>the</strong> inlet ends. The remainder of run 12<br />

was completed with sections 1A and 1B in service.<br />

The development of flow restrictions at <strong>the</strong> char-<br />

coal beds appears to be related to <strong>the</strong> accumula-<br />

tion of volatile organic matter on <strong>the</strong> steel wool<br />

packing at <strong>the</strong> bed inlets. Physical variations in<br />

this packing probably account for <strong>the</strong> different<br />

times required to plug various individual sections.<br />

The experience in runs 11 and 12 indicates that<br />

<strong>the</strong> restrictions can be effectively removed by<br />

electrically heating <strong>the</strong> inlet ends of <strong>the</strong> beds.<br />

Presumably, this heating drives <strong>the</strong> volatile matter<br />

off <strong>the</strong> steel wool packing in <strong>the</strong> inlets and moves<br />

it far<strong>the</strong>r downstream where <strong>the</strong> flow areas are<br />

larger. There is no evidence from <strong>the</strong> charcoal<br />

temperatures that this material has reduced <strong>the</strong><br />

fission product retention capability of <strong>the</strong> charcoal.<br />

Since <strong>the</strong> heating operations do not affect reactor<br />

performance, <strong>the</strong>re are no plans at present to make<br />

fur<strong>the</strong>r modifications at <strong>the</strong> charcoal beds.<br />

Coolant Off-gas System. - Very slow plugging<br />

of <strong>the</strong> coolant off-gas system at <strong>the</strong> filter that<br />

precedes <strong>the</strong> coolant-loop pressure control valve<br />

has been encountered throughout <strong>the</strong> reactor opera-<br />

tion. The originally installed filter was replaced<br />

in February 1965, during <strong>the</strong> preoperational check-<br />

out of <strong>the</strong> system. Subsequent replacements were<br />

made in March and September 1966 and on March<br />

1, 1967. The replacement on March 1, 1967, re-<br />

quired a reactor power reduction for 7 hr to permit

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