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ORNL-4191 - the Molten Salt Energy Technologies Web Site

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800 and 930 rpm and makes it appear advisable to<br />

separate <strong>the</strong> inner and outer casing frequencies by<br />

suitable changes in <strong>the</strong> wall thicknesses and<br />

diameters of <strong>the</strong> two casings.<br />

A preliminary undamped torsional critical-speed<br />

analysis has been made for <strong>the</strong> pump system, and<br />

<strong>the</strong> results indicate that <strong>the</strong> two torsional critical<br />

speeds that might affect pump operation can be<br />

strongly dependent upon <strong>the</strong> electromagnetic<br />

torsional stiffness of <strong>the</strong> drive motor. We believe<br />

that by changing some of <strong>the</strong> component dimensions<br />

and accounting for inherent system damping, <strong>the</strong><br />

pump will operate satisfactorily between <strong>the</strong> first<br />

and second torsional critical speeds.<br />

Fabrication Methods Survey. - Based on <strong>the</strong><br />

preliminary layout of <strong>the</strong> MSBK fuel salt pump, <strong>the</strong><br />

shaft and inner and outer casings were detailed,<br />

and a survey is being made of potential fabrication<br />

methods to identify fabrication problems. For <strong>the</strong><br />

shaft, it is important to determine <strong>the</strong> straightness<br />

and concentricity tolerances that can be supplied.<br />

These tolerances have considerable effect on <strong>the</strong><br />

provisions that must be made for <strong>the</strong> dynamic<br />

balancing of <strong>the</strong> shaft, which must be done ra<strong>the</strong>r<br />

precisely when <strong>the</strong> pump is to operate above <strong>the</strong><br />

first shaft critical speed. A manufacturer was<br />

found who could fabricate shafts in <strong>the</strong> range 7 to<br />

10 in. outside diameter with a wall thickness as<br />

small as '4 in., and who would guarantee <strong>the</strong><br />

straightness from end to end to 0.005 total indi-<br />

cator reading (TIR) and <strong>the</strong> outside diameter-<br />

inside diameter concentricity to 0.005 in., but at<br />

considerable expense. As <strong>the</strong>se two tolerances<br />

are relaxed, more manufacturing capability is<br />

available, and <strong>the</strong> fabrication costs are reduced;<br />

however, dynamic balancing of <strong>the</strong> shaft becomes<br />

a more important portion of <strong>the</strong> fabrication process.<br />

10 1<br />

An investigation is under way to determine <strong>the</strong><br />

relationship between shaft precision and total<br />

shaft cost (fabrication plus dynamic balancing) as<br />

well as its effect on pump design.<br />

Several manufacturers have been found who are<br />

capable of fabricating <strong>the</strong> inner and outer casings<br />

to <strong>the</strong> tolerances shown on <strong>the</strong> preliminary layout,<br />

but also at considerable expense. The effects on<br />

pump design of relaxing <strong>the</strong> preliminary values of<br />

<strong>the</strong> tolerances are being studied.<br />

O<strong>the</strong>r <strong>Molten</strong>-<strong>Salt</strong> Pumps<br />

Fuel Pump High-Temperature Endurance Test<br />

Facility. - The facility,3 including <strong>the</strong> salt pump,<br />

gas systems, instrumentation, and handling equip-<br />

ment, is being prepared for operation with sodium<br />

fluoroborate (WaBF,). The new drive motor, rated<br />

200 lip at 1800 rpm, was delivered, and <strong>the</strong> existing<br />

motor support was modified to suit <strong>the</strong> new motor.<br />

Also, <strong>the</strong> pump rotary element was retnoved<br />

from <strong>the</strong> facility, disassembled, cleaned, and<br />

reassembled.<br />

<strong>Molten</strong>-<strong>Salt</strong> B'earing Pump Endurance Test<br />

Facility. - A new salt bearing constructed of<br />

Wastelloy N was installed on this pump.4 The<br />

gimbals support for <strong>the</strong> bearing was modified to<br />

reduce <strong>the</strong> possibility of <strong>the</strong> support becoming<br />

disassembled during operation. The bearing and<br />

gimbals arrangement was satisfactorily tested<br />

with oil iis <strong>the</strong> pumped fluid at room temperature.<br />

3<br />

MSK Program Semiann. Pro&. Rept. Feh. 28, 1967,<br />

<strong>ORNL</strong>-41 19, p. 66.<br />

'MSR Program Semianti. [Jrogr. f?cpt. ~ u g 31, . 1966,<br />

OHNL-4037, p. 82.

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