ORNL-1771 - Oak Ridge National Laboratory
ORNL-1771 - Oak Ridge National Laboratory
ORNL-1771 - Oak Ridge National Laboratory
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2.5 kg can be prepared in this equipment. During<br />
the quarter, 27 preparations that yielded about 70 kg<br />
of material were made.<br />
Repeated attempts to prepare NaF-KF-Li F mix-<br />
tures containing 14 wt % UF, and 1 wt % UF, by<br />
reduction of UF, with uranium metal yielded mix-<br />
tures containing 5 to 7 wt % UF, by chemical<br />
analysis. These results, along with those reported<br />
elsewhere in this document, seem to show that in<br />
systems containing KF, reduction of UF, by ura-<br />
nium metal is markedly incomplete. Pending clari-<br />
fication of this point, production of material con-<br />
taining 5 wt % UF, and 10 wt % UF, is under way,<br />
Production Facility<br />
J. P. Blakely F. L. Daley<br />
Materials Chemistry Division<br />
During the past quarter, 1760 kg of processed<br />
fluorides was produced in the 250.lb facility for<br />
external and internal distribution. A breakdown of<br />
the production according to composition is given<br />
below:<br />
Amount<br />
Processed<br />
(ks)<br />
NoF-ZrF4-UF4 (50-46-4 mole %) 79 1<br />
NaF-ZrF, (50-50 mole 76) 565<br />
NoF-ZrF4-UF4 (50-43.56.5 mole %) 404<br />
Pratt & Whitney Aircraft Division received 27 kg<br />
of NaF-ZrF, (50-50 mole %) and 113 kg of NaF-<br />
ZrF,-UF, (50-46-4 mole 96). Battelle Memorial<br />
Institute received 46 kg of NaF-ZrF,-UF, (50-46-4<br />
mole %) and 68 kg of NaF-ZrF, (50-50 mole %)-<br />
The remaining processed material was distributed<br />
to various requesters in the ANP Program.<br />
The difficulties associated with the long stripping<br />
times and large hydrogen volumes required for pra-<br />
duction of rigorously pure fluoride melts from the<br />
raw materials available have not yet been over-<br />
come.32 Attempts to shorten the time required by<br />
increasing the hydrogen flow rate from 4 to 15<br />
liters/min and thus decrease labor und maintenance<br />
costs were not successful. Under these conditions<br />
._.__i_______.l-<br />
32F, F. Blankenship and G. J. Nessle, ANP Qum.<br />
Prr,g. Rep. June IO, 1954, <strong>ORNL</strong>-1729, p 61.<br />
PERIOD ENDING SEPTEMBER 70, 1954<br />
the gas inlet tubes plugged quite frequently and<br />
the HF concentration in the exit hydrogen fell<br />
much below the value obtained at lower flow rates.<br />
The over-all purification time was not appreciably<br />
shortened by the fourfold increase in hydrogen<br />
passed.<br />
Sublimation of crude ZrF, at a temperature lower<br />
than that previously used by Y-12 personnel did<br />
not appreciably improve the purity of the ZrF,<br />
product. Accordingly, the NaF-ZrF, melts produced<br />
iri the near future will be prepared from the<br />
(NaF)x*ZrF, that is available in moderately pure<br />
form from a commercial source; hafnium-free ZrF4<br />
will be used to adjust the composition as required,<br />
since this material is available in a high state of<br />
purity,<br />
Electrolytic purification of NaF-ZrF4 mixtures<br />
has been shown to be complete, and the process<br />
requires much less time than does the hydrogen<br />
stripping process. Accordingly, one of the units<br />
in the production facility is being modified slightly<br />
to test this method on Q large scale. It is antici-<br />
pated that the use of the purer taw materials and<br />
the electrolytic purification process will consider-<br />
ably decrease the cost of fuel preparation.<br />
In-Pile Loop Loading<br />
J. E. Eorgan<br />
Materials Chemistry Division<br />
The first in-pile loop was loaded on June 11 with<br />
a fuel concentrate, NaF-ZrF,-UF, (62.5- 12.5-25.0<br />
mole %), prepared from enriched uranium by Y-12<br />
personnel. The loading apparatus and confrols<br />
performed satisfactorily, and the transfer of ma-<br />
terial to the loop went smoothly. However, the<br />
electrical contact which should have indicated<br />
when the loop was filled to operating level was<br />
not activated even after 120% of the calculated<br />
charge had been added.<br />
Subsequent examination of the loop showed that<br />
a weld had given way where the loop was connected<br />
to the pump bowl, and it seems certain that this<br />
leak was present during the filling operation. The<br />
U235 is being salvaged from the loop. Examination<br />
of the filling apparatus revealed that all but 68 g<br />
of a total of 5837 g of the material was transferred<br />
to the loop.<br />
79