ORNL-2106 - the Molten Salt Energy Technologies Web Site
ORNL-2106 - the Molten Salt Energy Technologies Web Site
ORNL-2106 - the Molten Salt Energy Technologies Web Site
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<strong>the</strong>rmocouple lead wires which failed had, in-<br />
advertently, been clamped rigidly to <strong>the</strong> end of <strong>the</strong><br />
outer wall of <strong>the</strong> double-walled heat exchanger.<br />
This could have resulted in strains on <strong>the</strong> <strong>the</strong>rmo-<br />
couple wire from <strong>the</strong> <strong>the</strong>rmal expansion of <strong>the</strong><br />
pipes. The loop design has been modified to<br />
correct this condition.<br />
As with loop No. 3, both <strong>the</strong> bearing-housing and<br />
<strong>the</strong> pump-sump purge outlets plugged. The bearing<br />
purge outlet plugged five days after startup, and<br />
<strong>the</strong> sump purge outlet plugged four days later.<br />
The cause of this plugging is still being investi-<br />
gated. The fission-gas absorption traps from loop<br />
No. 3 have been sectioned. An extensive black<br />
deposit was found in <strong>the</strong> inlet of one and a brownish<br />
film was found in <strong>the</strong> o<strong>the</strong>r. This black deposit,<br />
believed to have come from <strong>the</strong> pump lubricating<br />
oil in <strong>the</strong> bearing housing, is to be given radio-<br />
assay and spectrographic analysis to determine<br />
its composition (see Chap. 4.2, "Radiation<br />
Damage"). It is planned to operate future loops<br />
with little or no purging of <strong>the</strong> bearing housing<br />
and reduced purging of <strong>the</strong> pump sump to minimize<br />
<strong>the</strong> probability of plugging. Previously, <strong>the</strong> higher<br />
purging rates were considered necessary to mini-<br />
mize hydraulic-motor-oi I contamination. Experience<br />
indicates that, although some contamination results<br />
from operating with <strong>the</strong> purges plugged, such con-<br />
tamination is not a serious problem during dis-<br />
assembly.<br />
O<strong>the</strong>r major difficulties encountered were a leak<br />
in <strong>the</strong> pump bulkhead, probably through a glass<br />
heater or <strong>the</strong>rmocouple-wire seal, and an excessive<br />
radiation level in he cubicle after shutdown. A<br />
new type of electrical seal for <strong>the</strong> pump bulkhead<br />
is being investigated. The excessive activity of<br />
<strong>the</strong> cubicle after shutdown was caused by <strong>the</strong><br />
deposition of material on <strong>the</strong> purge-outlet-tube<br />
walls during operation. Radiation levels as hi&<br />
as 50 rhr were measured on <strong>the</strong> \-in. pump-purge-<br />
outlet tube. This caused considerable difficulty<br />
in loop removal because it necessitated a relatively<br />
large amount of preparatory wak. The design has<br />
76<br />
now been modified so that all tubes may be pinched<br />
leak-tight, cut, and removed remotely to make<br />
possible <strong>the</strong> removal of <strong>the</strong> activity prior to <strong>the</strong><br />
entry of personnel into <strong>the</strong> cubicle. The only work<br />
which will require entry to <strong>the</strong> cubicle will be <strong>the</strong><br />
removal of <strong>the</strong> air and water lines.<br />
Loop No. 5<br />
D. M. Haines<br />
In-pile loop No. 5 was completed and inserted<br />
in <strong>the</strong> MTR, but could not be filled. This loop<br />
was to have operated for <strong>the</strong> duration of two<br />
MTR operating cycles with a maximum fuel tem-<br />
perature of 1600OF and a temperature differential<br />
of 200OF. The improved <strong>the</strong>rmocouple installa-<br />
tion mentioned above was used in <strong>the</strong> fabrication<br />
of this loop, and <strong>the</strong> rear section was modified to<br />
simplify removal and to provide a second hermetic<br />
seal to back up <strong>the</strong> seal at <strong>the</strong> intermediate bulk-<br />
head to prevent fission-gas leakage. The loop is<br />
being returned to <strong>ORNL</strong> for salvage.<br />
Horizontal-Shaft Sump Pump for In-Pile Loops<br />
W. S. Karn3<br />
An improved prototype (Mark II) of <strong>the</strong> horizontal-<br />
shaft sump pump designed for in-pile loop operation<br />
completed 1000 hr of a 2000-hr endurance test at<br />
4500 rpm and 1500OF. The test was terminated by<br />
shaft seizure, and disassembly showed that <strong>the</strong><br />
seizure was caused by <strong>the</strong> buildup of zirconium<br />
fluoride on <strong>the</strong> shaft slinger. This was <strong>the</strong> first<br />
pump operated at 1500°F, <strong>the</strong> previous pumps being<br />
operated at 1400OF. The vapor pressure of zir-<br />
conium fluoride in <strong>the</strong> fuel mixture (No. 44) NaF-<br />
ZrF4-UF, (53.5-40.6.5 mole %) used in this test<br />
is 2 mm Hg at 1400OF and 4.5 mm Hg at 1500OF.<br />
The increase in vapor pressure is considered to<br />
have been <strong>the</strong> cause of <strong>the</strong> buildup of zirconium<br />
fluoride on <strong>the</strong> slinger. A new pump is to be built<br />
with increased clearances at <strong>the</strong> slinger.<br />
30n assignment from Prott & Whitney Aircraft.