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ORNL-2106 - the Molten Salt Energy Technologies Web Site

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<strong>the</strong>rmocouple lead wires which failed had, in-<br />

advertently, been clamped rigidly to <strong>the</strong> end of <strong>the</strong><br />

outer wall of <strong>the</strong> double-walled heat exchanger.<br />

This could have resulted in strains on <strong>the</strong> <strong>the</strong>rmo-<br />

couple wire from <strong>the</strong> <strong>the</strong>rmal expansion of <strong>the</strong><br />

pipes. The loop design has been modified to<br />

correct this condition.<br />

As with loop No. 3, both <strong>the</strong> bearing-housing and<br />

<strong>the</strong> pump-sump purge outlets plugged. The bearing<br />

purge outlet plugged five days after startup, and<br />

<strong>the</strong> sump purge outlet plugged four days later.<br />

The cause of this plugging is still being investi-<br />

gated. The fission-gas absorption traps from loop<br />

No. 3 have been sectioned. An extensive black<br />

deposit was found in <strong>the</strong> inlet of one and a brownish<br />

film was found in <strong>the</strong> o<strong>the</strong>r. This black deposit,<br />

believed to have come from <strong>the</strong> pump lubricating<br />

oil in <strong>the</strong> bearing housing, is to be given radio-<br />

assay and spectrographic analysis to determine<br />

its composition (see Chap. 4.2, "Radiation<br />

Damage"). It is planned to operate future loops<br />

with little or no purging of <strong>the</strong> bearing housing<br />

and reduced purging of <strong>the</strong> pump sump to minimize<br />

<strong>the</strong> probability of plugging. Previously, <strong>the</strong> higher<br />

purging rates were considered necessary to mini-<br />

mize hydraulic-motor-oi I contamination. Experience<br />

indicates that, although some contamination results<br />

from operating with <strong>the</strong> purges plugged, such con-<br />

tamination is not a serious problem during dis-<br />

assembly.<br />

O<strong>the</strong>r major difficulties encountered were a leak<br />

in <strong>the</strong> pump bulkhead, probably through a glass<br />

heater or <strong>the</strong>rmocouple-wire seal, and an excessive<br />

radiation level in he cubicle after shutdown. A<br />

new type of electrical seal for <strong>the</strong> pump bulkhead<br />

is being investigated. The excessive activity of<br />

<strong>the</strong> cubicle after shutdown was caused by <strong>the</strong><br />

deposition of material on <strong>the</strong> purge-outlet-tube<br />

walls during operation. Radiation levels as hi&<br />

as 50 rhr were measured on <strong>the</strong> \-in. pump-purge-<br />

outlet tube. This caused considerable difficulty<br />

in loop removal because it necessitated a relatively<br />

large amount of preparatory wak. The design has<br />

76<br />

now been modified so that all tubes may be pinched<br />

leak-tight, cut, and removed remotely to make<br />

possible <strong>the</strong> removal of <strong>the</strong> activity prior to <strong>the</strong><br />

entry of personnel into <strong>the</strong> cubicle. The only work<br />

which will require entry to <strong>the</strong> cubicle will be <strong>the</strong><br />

removal of <strong>the</strong> air and water lines.<br />

Loop No. 5<br />

D. M. Haines<br />

In-pile loop No. 5 was completed and inserted<br />

in <strong>the</strong> MTR, but could not be filled. This loop<br />

was to have operated for <strong>the</strong> duration of two<br />

MTR operating cycles with a maximum fuel tem-<br />

perature of 1600OF and a temperature differential<br />

of 200OF. The improved <strong>the</strong>rmocouple installa-<br />

tion mentioned above was used in <strong>the</strong> fabrication<br />

of this loop, and <strong>the</strong> rear section was modified to<br />

simplify removal and to provide a second hermetic<br />

seal to back up <strong>the</strong> seal at <strong>the</strong> intermediate bulk-<br />

head to prevent fission-gas leakage. The loop is<br />

being returned to <strong>ORNL</strong> for salvage.<br />

Horizontal-Shaft Sump Pump for In-Pile Loops<br />

W. S. Karn3<br />

An improved prototype (Mark II) of <strong>the</strong> horizontal-<br />

shaft sump pump designed for in-pile loop operation<br />

completed 1000 hr of a 2000-hr endurance test at<br />

4500 rpm and 1500OF. The test was terminated by<br />

shaft seizure, and disassembly showed that <strong>the</strong><br />

seizure was caused by <strong>the</strong> buildup of zirconium<br />

fluoride on <strong>the</strong> shaft slinger. This was <strong>the</strong> first<br />

pump operated at 1500°F, <strong>the</strong> previous pumps being<br />

operated at 1400OF. The vapor pressure of zir-<br />

conium fluoride in <strong>the</strong> fuel mixture (No. 44) NaF-<br />

ZrF4-UF, (53.5-40.6.5 mole %) used in this test<br />

is 2 mm Hg at 1400OF and 4.5 mm Hg at 1500OF.<br />

The increase in vapor pressure is considered to<br />

have been <strong>the</strong> cause of <strong>the</strong> buildup of zirconium<br />

fluoride on <strong>the</strong> slinger. A new pump is to be built<br />

with increased clearances at <strong>the</strong> slinger.<br />

30n assignment from Prott & Whitney Aircraft.

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