ORNL-2106 - the Molten Salt Energy Technologies Web Site
ORNL-2106 - the Molten Salt Energy Technologies Web Site
ORNL-2106 - the Molten Salt Energy Technologies Web Site
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<strong>the</strong> first 200OF and B0F/sec for <strong>the</strong> next 10OOF.<br />
The final 100°F drop is at a slower rate in order<br />
to allow <strong>the</strong> outlet temperature to level out<br />
properly. The transition from power to iso<strong>the</strong>rmal<br />
operation is accomplished at a rate of 10°F/sec<br />
for <strong>the</strong> first 100°F, S°F/sec for <strong>the</strong> final 1OOOF.<br />
The radiator has been cycled 20 times, ahd <strong>the</strong>.<br />
cycling program is continuing.<br />
The air pressure drop datalo obtained for York<br />
radiator No. 9 substantially agree with <strong>the</strong> data<br />
for York radiators Nos. 1 and 2, and <strong>the</strong> heat<br />
transfer data substantially agree with <strong>the</strong> datalo<br />
for Cambridge radiators Nos. 1 and 2. Thus far<br />
<strong>the</strong> NaK pressure drop has increased 119% above<br />
<strong>the</strong> initial level (219% of ,<strong>the</strong> initial value). This<br />
radiator is <strong>the</strong> first 500-kw radiator of <strong>the</strong> revised<br />
designll to be tested, and it is identical to York<br />
radiator No. 7 illustrated in Fig. 1.4.8 of <strong>the</strong> sub-<br />
sequent section, “Small Heat Exchanger Tests,”<br />
of this chapter.<br />
<strong>ORNL</strong> heat exchangers Nos. 1 and 2, type<br />
IHE-3 (ref. 12), were removed from intermediate<br />
heat exchanger test stand B and are undergoing<br />
metallurgical inspection. Preliminary results of<br />
this insp,ection reveal that heat exchanger No. 1<br />
(NaK-to-fuel heat exchanger) failed in <strong>the</strong> hot end<br />
between <strong>the</strong> header,weld and tube bends (see<br />
Chap. 3.4, “Welding and hating Investigations”).<br />
Severecorrosion was evident on <strong>the</strong> fuel side of <strong>the</strong><br />
tubes. Five tubes had obvious cracks in <strong>the</strong><br />
tension side. The frequency and severity of <strong>the</strong><br />
cracks were most pronounced in <strong>the</strong> end row of<br />
tubes where <strong>the</strong> distance between <strong>the</strong> tube bends<br />
and header was <strong>the</strong> shortest. A maximum of 15 mils<br />
of moss-transferred deposit was measured on <strong>the</strong><br />
NaK side of this heat exchanger (Fig. 1.4.7). No<br />
evidence of mass transfer was detected in heat ex-<br />
changer No. 2 (fuel-to-NaK heat exchanger). Mass<br />
transfer buildup would account for he NaK pres-<br />
sure drop increase experienced during noniso<strong>the</strong>rmal<br />
operation. Pressure drop was not measured in <strong>the</strong><br />
individual heat exchangers. However, if it is<br />
assumed, on <strong>the</strong> basis of <strong>the</strong> mass-transfer evi-<br />
dence, that al l <strong>the</strong> pressuredrop increase occurred<br />
in heat exchanger No. 1, <strong>the</strong> total pressure drop<br />
l0J, C. Amos, ANP Quar. Pmg. Rep. March 10, 1956,<br />
<strong>ORNL</strong>-2061, p 54.<br />
llE. R. Dytko et aL, ANP Quat. Pmg. Rep. March 10,<br />
1956, <strong>ORNL</strong>-2061, P 52.<br />
12R. D. Peak et al., ANP Quar. frog. Rep. Dec. 10,<br />
1955, <strong>ORNL</strong>-2012, P 41.<br />
PERIOD ENOlNG JUNE 10, 7956<br />
TUBE INSIDE WALL<br />
3.004 -<br />
DD02 -<br />
D.003<br />
0.004 __<br />
KO05<br />
0.006 -<br />
OL07<br />
-%-<br />
0 I<br />
- 5 --<br />
_. _-<br />
0*04 _. 4 -<br />
0.042<br />
O.Ot3<br />
-- 0.014<br />
- 0.015<br />
0.046<br />
Fig. 1.4.7. Maximum Mass Transfer Found in<br />
NaK Circuit of NaK-to-Fuel Heat Exchanger (<strong>ORNL</strong><br />
No. l), Type IHE-3, Which Operated 1825 hr in<br />
Intermediate Heat Exchanger Test Stand B. (M<br />
WirktaPtidR)<br />
increase for this heat exchanger was approximately<br />
180%.<br />
Black, Sivalls and Bryson Nos. 1 and 2 heat ex-<br />
chcingers, type IHE-3, were installed in test stand<br />
B, and test operations were resumed. The stand is<br />
currently operating on a constant-power endurance<br />
run to provide corrosion information for comparison<br />
with <strong>the</strong> data for <strong>ORNL</strong> heat exchangers Nos. 1 and<br />
2. During shutdown of <strong>the</strong> test stand, instrumenta-<br />
tion was added to allow separate measurements of<br />
heat exchanger pressure drop. After 362 hr of<br />
power operation, <strong>the</strong> NaK pressure drop has in-<br />
creased 140% in heat exchanger No. 1 (NaK-to-fuel).<br />
No increase has occurred in heat exchanger No. 2<br />
Cambridge radiators Nos. 1 and 2, which have<br />
operated for 820 hr under noniso<strong>the</strong>rmal conditions,<br />
have experienced a NaK pressure drop increase<br />
of 84% A tabulation of <strong>the</strong> NaK pressure drop<br />
variations that have occurred in he various heat<br />
exchanger tests is presented in Table 1.4.3.<br />
Construction work on stand C, to be used as an<br />
ART prototype radiator test stand, is continuing.<br />
57