ORNL-2106 - the Molten Salt Energy Technologies Web Site
ORNL-2106 - the Molten Salt Energy Technologies Web Site
ORNL-2106 - the Molten Salt Energy Technologies Web Site
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LJ<br />
DEVELOPMENT OF NICKEL-MOLYBDENUM<br />
BASE ALLOYS<br />
H. lnouye T. K. Roche<br />
The available supply of HastelIoy B and W<br />
tubing was prepared by redrawing tubing formed<br />
from welded strip, and it is not of high quality.<br />
Since <strong>the</strong>se alloys are characterized by high-<br />
temperature strength and resistance to fused-salt<br />
corrosion, a source of seamless tubing is desired,<br />
and <strong>the</strong>refore considerable effort has been devoted<br />
to <strong>the</strong> study of extrusion techniques for <strong>the</strong> pro-<br />
duction of seamless tubing of <strong>the</strong>se Hastelloys<br />
and o<strong>the</strong>r related alloys.<br />
Extrusion of Hastelloy W<br />
Early attempts to extrude tube blanks of<br />
Hastelloy W failed. In <strong>the</strong>se experiments forged<br />
billets canned in lnconel were extruded at 2050<br />
and 21OCf'F at an extrusion ratio of 7:1. Severe<br />
fracturing of <strong>the</strong> tubing occurred during <strong>the</strong> ex-<br />
trusion process as a result of melting. An<br />
excessive temperature rise as a result of <strong>the</strong> rapid<br />
deformation of <strong>the</strong> material is believed to have<br />
caused <strong>the</strong> difficulty. Recently this alloy was<br />
successfully extruded under conditions identical<br />
to those used earlier, as listed below, except for<br />
<strong>the</strong> extrusion temperature and rate:<br />
5iI let<br />
Billet size<br />
Forged Hastelloy W canned in Inconel<br />
3 in. OD, 1k in. ID, 3 in. long<br />
3.3. FABRICATION RESEARCH<br />
J. H. Coobs<br />
PERIOD ENDlNG JUNE 10, I956<br />
<strong>the</strong> 2050 and 21OOOF used for <strong>the</strong> unsuccessful<br />
extrusions. It was concluded from this work that<br />
Hastelloy W could be extruded on a laboratory<br />
scale by raising <strong>the</strong> extrusion temperature and<br />
lowering <strong>the</strong> extrusion rate to allow time for <strong>the</strong><br />
heat generated in <strong>the</strong> work to dissipate to <strong>the</strong><br />
surroundings. The successful and unsuccessful<br />
tube-blank extrusions are illustrated in Fig. 3.3.1.<br />
Extrusion of Hastelloys 8, W, and X<br />
on a Commercial Scale<br />
An experiment was performed at <strong>the</strong> Huntington<br />
Works of <strong>the</strong> International Nickel Company on<br />
March 27, 19%, to determine <strong>the</strong> feasibility of<br />
producing tube blank extrusions of Hastelloys B,<br />
W, and X on a commercial scale. The experiment<br />
was carried out as a cooperative effort between<br />
<strong>the</strong> Oak Ridge National Laboratory, <strong>the</strong> Inter-<br />
national Nickel Company, and <strong>the</strong> Haynes Stellite<br />
Company.<br />
Forged and machined billets of <strong>the</strong> Hastelloys<br />
were prepared by <strong>the</strong> Haynes Stellite Company.<br />
Based upon extrusion experience on a laboratory<br />
scale at <strong>ORNL</strong>, as described above, a schedule<br />
was prepared for <strong>the</strong> extrusion of <strong>the</strong> Hastelloy B<br />
billets. Since small tube blanks had been prepared<br />
successfully by using a slow extrusion rate at<br />
2200°F, it was proposed that <strong>the</strong>se larger billets<br />
. .<br />
be extruded at as slow a rate as practical. The<br />
extrusion temperature could be lower, of course,<br />
because of <strong>the</strong> larger size of <strong>the</strong> billet. The<br />
results of <strong>the</strong> Hastelloy B extrusions, which are<br />
ummarized in Table 3.3.1, were reported to <strong>ORNL</strong><br />
y <strong>the</strong> International Nickel Company upon com-<br />
ent. The actual extruded<br />
stelloy B are shown in Figs.<br />
elloy W and X billets were not<br />
der <strong>the</strong> direction of <strong>ORNL</strong>, <strong>the</strong> fabri-<br />
se alloys is of interest to <strong>the</strong> overs11<br />
am. The available results<br />
presented in Table 3.3.2.<br />
al conclusions have been<br />
<strong>the</strong> extrusion of 6,9-in.-OD, 10ts<br />
of Hastelloys B, W, and X:<br />
The extrusion temperature of 2200OF used for 1. Forged billets of Hastelloys B, W, and X can<br />
<strong>the</strong> successful extrusion was an increase over be successfully extruded to tube blanks.<br />
159