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Ph.D. Thesis - Physics

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choices and heat sinking. The wire used for the dc connections and a portion of the rf<br />

line is a 36-gauge phosphor bronze wire, LakeShore Part No. WSL-36-500. The constant<br />

of thermal conductivity is 48 W/(K·m). For a temperature gradient of 294 K across a<br />

wire length of 10 cm, the thermal conductivity is 2 mW. Since this is much less than<br />

the cooling power at 4 K and 40 K (0.8 W and 35 W, respectively), heat gain due to<br />

conduction should be negligible. Actually, the figure is better than this, since the dc wires<br />

were wrapped repeatedly around the 40 K shield (increasing the length and heat-sinking)<br />

before being taped down to the 40 K baffle and then heat-sunk to the 4 K shield using<br />

StyCast thermally-conductive epoxy.<br />

The rf wiring was purposefully made shorter than the dc wires to reduce stray ca-<br />

pacitance. From the exterior feedthrough, a thin wire (to break thermal conductivity) was<br />

taped to the 40 K baffle, then attached to a thicker wire (to increase electrical conductivity),<br />

before being soldered to a thin wire which was heat-sunk with StyCast to the 4 K base-<br />

plate and routed to the trap. This combination was designed to provide as much electrical<br />

conductivity as possible while still breaking the thermal connections.<br />

Upon finishing work inside the cryostat, the system was put under turbo pump vacuum,<br />

leading to ultimate pressure in the high 10 −6 torr range. A 50 Ω heater is installed on the<br />

cold head, and this was engaged to bring the system to a temperature of 380 K for around<br />

24 hours, allowing some oils, water, and other residues to bake off and be removed from the<br />

system. This is done partially to improve the ultimate pressure, and partially to remove<br />

substances which might freeze onto the trap electrodes at 4 K. A pair of charcoal getters<br />

were also installed on the 40 K shield, and were discharged during this time with a wire<br />

whose resistance totaled 150 Ω. A current of 0.06 A through the getters was used.<br />

Finally, a 20 l/s ion pump was installed directly on the outer octagon. This was turned<br />

on before cooldown. There are two main advantages to this. The first is that the system is<br />

completely closed from the “outside world” during cooldown. This prevents cryopumping<br />

from actually pumping material from the turbo pump line into the cryostat. Furthermore,<br />

in case of a malfunction of the turbo or roughing pumps, it prevents oils from being cryop-<br />

umped into the system. The other advantage is that reading the ion pump current enables<br />

one to upper-bound the pressure inside. Since the ion pump is connected directly to room<br />

temperature, we expect the pressure inside the radiation shield to be considerably less than<br />

that measured on the ion pump. It was impressive that the pressure reading on the ion<br />

pump, when the system was fully cooled, read 0.0×10 −9 torr.<br />

The system was equipped with two diode temperature sensors. Each requires a 10 µA<br />

current, and the temperature is inferred from the voltage across the diode. One is anchored<br />

to the cold head, and is called the control sensor. The other can be placed anywhere else,<br />

and is called the free sensor. We chose to place the free sensor directly on the 4 K baseplate,<br />

anchored with StyCast. The free sensor came to a temperature of 4-5 K normally, while<br />

the control sensor was at 11-13 K. It is not known why the temperature was not lower;<br />

176

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