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Lessons Learnt In 45 Years<br />

of Condition Monitoring<br />

Ray Beebe Monash University Gippsland Campus (Australia)<br />

The author was inspired by the concept of condition monitoring to help prevent unnecessary overhauls when<br />

he started as a young engineer in power generation in 1964. In parallel with a general engineering and middle<br />

management career in several power plants in Australia and the UK, he developed and applied vibration and<br />

performance analysis for pumps, steam turbines, boilers and heat exchangers. His experience and passion for<br />

sharing knowledge led to presentation of many in-house and public courses and his first book. That in turn led<br />

him to Monash University in 1992 and a second award-winning book in 2003. In that role, he reflected on his<br />

experiences and has written 70+ papers, many of which have been chosen for conferences and technical journals<br />

around the world. The lessons learnt stand forever, but not all are well-known. This paper of brief case studies in<br />

narrative style is intended to entertain, inform and even inspire.<br />

Introduction: the starting years<br />

Yallourn Power Station was initially built in the watch of Sir John Monash, citizen soldier (WW1 Lt-General) and<br />

engineer. It was the biggest one in the State from 1924 up to 1966. Such places tended to have the best engineers<br />

and I was fortunate to have two excellent bosses there. They had responded to a request from the manager of<br />

maintenance. He was apparently holding a sheaf of fault reports, overtime returns, spare parts usage reports, on<br />

a turbine that had just come back into service after a major stripdown. “There has to be a better way than this” was<br />

his cry. Research in POWER and ASME papers led to the Valves Wide Open test being applied. My involvement<br />

in testing 60MW and 120MW turbines there gave me the topic for my engineering course dissertation.<br />

Performance tests were also performed on the boiler feed pumps and used as a guide to overhaul.<br />

Measurement and analysis of machine vibration as a guide to its internal condition was very basic. We had a<br />

Philips velocity transducer and a readout box that gave overall vibration in thousandths of an inch. For some<br />

machines of rotation speed below 900 r/min, a multiplier of 1.5 was used: nobody explained why (later I learnt<br />

that it was because velocity transducers have a natural frequency below about 900 c/min). We could examine the<br />

output on a CRO, and tell if most of the vibration was at rotation frequency and if there was any “high frequency”<br />

present. This was adequate as most of the problems were caused by unbalance due to wear.<br />

Two methods were used for balancing in the field. The timed-oscillation method required only a stop watch and<br />

graph paper (Beebe, 2001). The other used a manually tunable filter that fired a stroboscope to detect previously<br />

chalked numbers around the rotor. The usual vector calculations followed.<br />

Lesson #1 Choose your bosses well<br />

Lesson #2 When a plant is new and/or the major asset makes it easier to get proposals<br />

for monitoring etc. accepted.<br />

After further training attachments, I was assigned to Hazelwood Power Station in 1966. It had three 200MW units in<br />

service, but would grow by a unit each year to reach eight, its current size. The boilers were essentially identical,<br />

but there were two makes of steam turbines and boiler feed pumps.<br />

The vibration measurement program was as at Yallourn, but more use was made of the balancing instrument to<br />

find relative phase angles of the 1X vibration to give a crude operation deflection shape. For routine monitoring of<br />

the steam turbines, permanent numbers were painted around the rotor line at a visible section.<br />

Case study 1<br />

A strange vibration was experienced on the newest machine at the generator drive end bearing. When runup<br />

following a shutdown, the machine vibration was unacceptably high. The operators tripped it and ran for some<br />

hours on turning gear (low speed rotation at 30 r/min). Back on line, the vibration was now acceptable. This<br />

happened repeatedly: sometimes all would be OK after a shutdown, sometimes not. Vibration measurements<br />

with our crude instruments on line in both states showed that the vibration amplitude and phase angle differed on<br />

every run! All I could say was “these symptoms indicate that there is something loose inside the generator rotor<br />

around that end”.<br />

Stripdown was arranged and the generator rotor examined closely. Nothing was found. Eventually, a message<br />

came from the OEM saying that one of the rotors – this one - was non-standard. At the end of manufacture, the<br />

rotor centres were bored out to about 100mm diameter, and the hole packed tightly with rubber bungs. Flaws<br />

were found in one of the rotors and a length was bored to a bigger diameter…. but bungs of the same size were<br />

inserted – see Figure 1. You can guess the effect of these masses moving around! They were removed -“no<br />

longer our practice” - and after an expensive 38 weeks off line, all ran well.<br />

Vol 24 No 2

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