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JAEA-Review-2010-065.pdf:15.99MB - 日本原子力研究開発機構

JAEA-Review-2010-065.pdf:15.99MB - 日本原子力研究開発機構

JAEA-Review-2010-065.pdf:15.99MB - 日本原子力研究開発機構

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1-22<br />

Touch-Down Test of Magnetic Bearing Type Centrifugal<br />

Contactor with Irradiated Touch-Down Bearing<br />

H. Ogino, K. Fujisaku and H. Hirano<br />

Nuclear Cycle Engineering Department, NFCEL, <strong>JAEA</strong><br />

The centrifugal contactor has excellent phase separation<br />

and a smaller hold-up volume than any other contactor type<br />

such as mixer-settler and pulsed column. These<br />

characteristics lead to “rapid start-up and shut-down”,<br />

“compact design” and “less solvent degradation”.<br />

Therefore, the centrifugal contactor is said to be<br />

advantageous for reprocessing a fast breeder fuel of high<br />

burn-up and high Pu-enrichment 1) , and study and<br />

development have been progressed since the 1960s.<br />

In <strong>JAEA</strong>, the rolling bearing type centrifugal contactor<br />

with anti-corrosion design (include air purge system,<br />

ceramic-bearing and others) has been developed and has<br />

achieved to 5,000 hours of operation without significant<br />

troubles. However, the grease becomes deteriorated by<br />

acid mist, temperature and other environmental factors, and<br />

2)<br />

that also affects the service life . To provide a possible<br />

resolution to this technical issue, we have developed the<br />

centrifugal contactor of non-contact journaled construction<br />

3)<br />

using magnetic bearings without grease . A magnetic<br />

bearing has the construction in which the attractive force of<br />

electromagnets is exerted to levitate a rotor without<br />

mechanical contact. Figure 1 shows the overview of<br />

irradiated magnetic bearing type centrifugal contactors and<br />

the structure of magnetic bearing.<br />

We carried out the gamma-ray irradiation test of<br />

centrifugal contactor with magnetic bearing system to<br />

estimate the radiation resistance in 2008. The equipments<br />

stopped several times under irradiation, and were not finally<br />

reactivated of two different factors, one was abrasion of the<br />

touch-down bearing and adhesion to the main shaft (shown<br />

in Fig. 2), the other was a trouble of IC. Accumulated dose<br />

of the equipments was 3.7- 4.7 × 10 8 R. Therefore, the<br />

present work is intended to investigate whether the cause of<br />

the stop with the touch-down bearing is an influence of<br />

gamma-ray irradiation.<br />

Motor<br />

Rotor<br />

Fig. 1 Irradiated magnetic bearing type centrifugal<br />

contactors and structure of magnetic bearing.<br />

<strong>JAEA</strong>-<strong>Review</strong> <strong>2010</strong>-065<br />

Thrust<br />

magnetic bearing<br />

Upper<br />

touch-down<br />

bearing<br />

Radial<br />

magnetic bearing<br />

Lower<br />

touch-down<br />

bearing<br />

Main shaft<br />

- 26 -<br />

The touch-down test were continuously carried out 6 runs<br />

(1run: 5 times touch-down) using the magnetic bearing type<br />

centrifugal contactor to which irradiated the lower<br />

touch-down bearing (a slide bearing formed of polyimide<br />

resin) was put in. So we observed the touch-down bearing,<br />

the main shaft, etc and monitored the control situation of<br />

magnetic-bearing after the touch-down test. Gamma-ray<br />

was irradiated to the lower touch-down bearing up to about<br />

10 9 R at a rate of 17.3 kGy/h at room temperature. Figure<br />

3 shows the observation result after the touch-down test<br />

(6 runs, 1 × 10 9 R). As shown in Fig. 3, neither abrasion of<br />

the touch-down bearing nor adhesion to the main shaft was<br />

observed. Moreover, the problem did not occur to control<br />

situation of the magnetic-bearing. Based on these results,<br />

we concluded that polyimide resin was a material which<br />

could be used under these system requirements. In the<br />

future, we will carry out gamma-ray irradiation test of<br />

improvement equipment which reflected these results again.<br />

Main shaft and adhesion material<br />

Fig. 2 Main shaft of No.1 equipment after the irradiation<br />

test (4.7 × 10 8 R).<br />

Lower touch-down bearing Main shaft<br />

Fig. 3 Main shaft and lower touchdown bearing after the<br />

touch-down test (6 runs, 10 9 R).<br />

References<br />

1) G. J. Bernstein et al., ANL-7969 (1973).<br />

2) T. Washiya et al., Proc. Global 2005 (2005).<br />

3) N. Okamura et al., Proc. Global 2007(2007).

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