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Analysis and modelling of the seismic behaviour of high ... - Ingegneria

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3. SEISMIC BEHAVIOUR OF BOLTED END PLATE BEAM-TO-COLUMN STEEL JOINTS<br />

larger displacement ductilities to be achieved; pinching phenomena appeared in<br />

<strong>the</strong> last cycles, when brittle failure developed at <strong>the</strong> weld toes <strong>of</strong> <strong>the</strong> tee stub.<br />

62<br />

REACTION FORCE (kN)<br />

REACTION FORCE (kN)<br />

400<br />

300<br />

200<br />

100<br />

0<br />

-100<br />

-200<br />

-300<br />

-400<br />

700<br />

525<br />

350<br />

175<br />

0<br />

-175<br />

-350<br />

-525<br />

-700<br />

C1A1-2<br />

C1A2-2<br />

0 3 6 9 12 15<br />

DISPLACEMENT (mm)<br />

C1B1-3<br />

C1B2-3<br />

0 1.5 3 4.5 6 7.5<br />

DISPLACEMENT (mm)<br />

Figure 3.14. Experimental response <strong>of</strong> (a) C1A1-2 <strong>and</strong><br />

C1A2-2; (b) C1B1-3 <strong>and</strong> C1B2-3 Coupled Tee stubs<br />

Pinching somehow depends on <strong>the</strong> relative thickness <strong>of</strong> <strong>the</strong> connection plate to <strong>the</strong><br />

column flange, <strong>and</strong> increased with <strong>the</strong> increase <strong>of</strong> this ratio. However, all <strong>the</strong><br />

coupled Tee stub specimens showed less important pinching than <strong>the</strong> isolated<br />

corresponding isolated Tee stubs. On <strong>the</strong> one h<strong>and</strong>, <strong>the</strong> C1A1-2 specimen, which<br />

(a)<br />

(b)

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