13.04.2013 Views

Paper Technology Journal 19 - Voith

Paper Technology Journal 19 - Voith

Paper Technology Journal 19 - Voith

SHOW MORE
SHOW LESS

Create successful ePaper yourself

Turn your PDF publications into a flip-book with our unique Google optimized e-Paper software.

3<br />

54<br />

Input 900 t/24 h<br />

Spec. effluent DIP 5.00 l/kg<br />

Spec. effluent PM 10.00 l/kg<br />

Furnish:<br />

Newspapers<br />

Magazines<br />

625.00<br />

91.00<br />

687<br />

<strong>19</strong>2111<br />

11.9<br />

Production [kg/min]<br />

Consistency [%]<br />

Volume flow [l/min]<br />

COD concentration [mg/l]<br />

COD load [kg/min]<br />

<strong>19</strong>/05<br />

Drum Pulper<br />

89.2<br />

50.00<br />

178<br />

3697<br />

0.33<br />

MC Screening<br />

Flotation I<br />

Inspection of the vacuum system revealed<br />

a defect in the vacuum pump<br />

plant, which restricted the deaeration capacity.<br />

This was then repaired.<br />

Analysis of chemical interactions<br />

in the stock and water<br />

loops<br />

While inspecting all the main machines<br />

and components, excessive foaming in<br />

the flotation cells with extremely stable<br />

foam and poor removal efficiency was<br />

found. Due to the low content of magazine<br />

papers in the furnish and the resultant<br />

low ash content, only tensides were<br />

used to aid flotation.<br />

Loop I<br />

HW Cleaner<br />

93.1<br />

2.26<br />

4128<br />

3697<br />

14.91<br />

Reject and<br />

Sludge Handling<br />

LC Slot Screening<br />

HC Thickening<br />

3.95<br />

0.10<br />

3949<br />

3697<br />

14.58<br />

2.67<br />

0.10<br />

2669<br />

3697<br />

9.85<br />

1.281<br />

0.10<br />

1281<br />

3697<br />

4.73<br />

558.6<br />

30.00<br />

1862<br />

4682<br />

6.10<br />

0.4<br />

0.015<br />

2885.8<br />

1104<br />

3.<strong>19</strong><br />

COD input 2nd loop<br />

0.00 kg/min<br />

Disperger<br />

Peroxide Bleaching<br />

Loop II<br />

Flotation II<br />

DF Thickening<br />

COD concentration in comparison:<br />

Calculation<br />

1st Loop COD = 4682 mg/l<br />

2nd Loop COD = 1104 mg/l<br />

PM Loop COD = 288 mg/l<br />

Apart from optimizing the spray nozzles<br />

to break down the foam more efficiently,<br />

a combination of tensides and soap was<br />

recommended to aid flotation.<br />

By using less tensides, foam formation<br />

has been reduced and the use of soap<br />

has improved the removal efficiency of<br />

the cells.<br />

Heavy deposits were found ahead of the<br />

machine chest and in the headbox. Chemical-physical<br />

analysis in the laboratory<br />

revealed aluminium sulphate as the main<br />

component of deposits at the machine<br />

chest as well as a silicate mixture in the<br />

headbox. Analysis of the additives and<br />

quantities identified the following situation:<br />

533.7<br />

15.00<br />

3558<br />

1104<br />

3.34<br />

to PM<br />

0.6<br />

0.01<br />

5718<br />

288<br />

1.65<br />

0.0<br />

0.00<br />

8558<br />

0.0<br />

0<br />

PM Loop<br />

Approach Flow<br />

0.5<br />

0.01<br />

5332<br />

288<br />

1.54<br />

PM<br />

Fresh water<br />

533.2<br />

50.00<br />

1066<br />

288<br />

0.15<br />

Measurement<br />

1st Loop COD > 4000 mg/l<br />

2nd Loop COD = 941 mg/l<br />

PM Loop COD = 235 mg/l<br />

● The aluminium sulphate dosing<br />

method was inadequate, resulting in<br />

excessive local dosages and formation<br />

of deposits just after the dosing point.<br />

● The Composil (PAC and anionic<br />

silicate) dual retention system was<br />

correctly operated. Interaction with<br />

the relatively high concentration of<br />

aluminium sulphate led however to<br />

deposits in the headbox and these<br />

were very difficult to remove.<br />

Balancing results and process<br />

model analysis with the focus<br />

on water management<br />

While the analysis work was being undertaken,<br />

about twice as much process wa-

Hooray! Your file is uploaded and ready to be published.

Saved successfully!

Ooh no, something went wrong!