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INSIDE LEFT<br />
ENGINE TROUBLE<br />
In the Sussex Express, Tuesday 30th September 1879, the headline read: ‘Alarming explosion at <strong>Lewes</strong> Railway<br />
Station’. On the previous Saturday, the fast London to Hastings train had stopped at <strong>Lewes</strong> at just past<br />
3pm. It was running ten minutes late. As passengers, including local MP William Christie, climbed aboard<br />
the busy carriages, guard Alec Fraser was talking to the platform inspector, Mr Hayden. The 31-year-old<br />
driver, William Rookwood, had just bought a bun from the basket of the refreshment vending lad called<br />
Funnell. The whistle blew but suddenly there were signs that something wasn’t right. The Express reports ‘a<br />
blinding rush of steam, clouds of dense black smoke, a dull sullen deafening sound not unlike the discharge<br />
of an immense piece of ordnance’. The engine, number 174, had burst and was ‘wrecked’. The door to the<br />
smoke box had been blown away, and the wheels twisted off the rail. The stoker lay across the tracks on the<br />
London down platform. Worst of all, on top of a carriage behind the front guard’s brake lay an ‘indistinguishable<br />
mass’. This was the driver, ‘frightfully mutilated’. A ladder was found and a medically trained passenger<br />
climbed up to discover Rookwood barely alive. Brandy was administered, but he died. The traumatised stoker<br />
was taken to the In�rmary with multiple injuries including a fractured skull.<br />
The shocked refreshment boy was covered in black soot, his basket full of pebbles from the track and glass<br />
from broken lemonade and spirit bottles. The Sussex Express reports that a large number of passengers,<br />
‘especially the female portion’ were severely alarmed.<br />
How had this tragedy occurred? Tom Reeves was told by Norman Cousins after a talk he gave that the safety<br />
valve had been tampered with, set for 140psi instead of 120psi, and that there was some speculation that it<br />
might have been an attempt on the life of the MP. But no de�nitive conclusion was reached as to how it happened.<br />
Thanks to Edward Reeves photographic studio (473274).<br />
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